Jump to content
SAU Community

Recommended Posts

hey guys. today I ended up replacing the stock dump pipe with a 3inch stainless steel pipe. While I was in the process of removing the old pipe I accidentally snapped two of the 13mm bolts on the back of the turbo :D Thankfully It was the top two bolts so I should be able to squeeze my little pistol drill in there without removing the turbo. I was just wondering what size drill bit I'd be best off using to drill the snapped bolts out.

Link to comment
https://www.sau.com.au/forums/topic/301589-replaced-stock-dump-pipe/
Share on other sites

Ended up buying some screw extractors. I don't know if that's what an 'easy-out' is but they didn't work at all. I ended up snapping one but luckily managed to get it out of the hole i'd drilled. After getting fed up with trying to get the 2 snapped bolts out i made a few calls and ended up taking the turbo to Edsway Engineering over at coopers plains. I can't speak highly enough of the guy that works there. Not only was he on holidays and came in just for me but it only cost me $20 to extract the 2 bolts out and re-thread the holes. The addy is 20/248 musgrave rd, coopers plains for anyone interested. And is it just me or is it friggin hard to bolt the oil and coolant lines back to the turbo? I must of spent at least an hour trying to line everything up.

Ended up buying some screw extractors. I don't know if that's what an 'easy-out' is but they didn't work at all. I ended up snapping one but luckily managed to get it out of the hole i'd drilled. After getting fed up with trying to get the 2 snapped bolts out i made a few calls and ended up taking the turbo to Edsway Engineering over at coopers plains. I can't speak highly enough of the guy that works there. Not only was he on holidays and came in just for me but it only cost me $20 to extract the 2 bolts out and re-thread the holes. The addy is 20/248 musgrave rd, coopers plains for anyone interested. And is it just me or is it friggin hard to bolt the oil and coolant lines back to the turbo? I must of spent at least an hour trying to line everything up.

That totally blows

Thats pretty good for a business to do that.

I have "Rigid" brand screw extractors, never found a snapped bolt they couldn't remove, cost me a fortune for the set but they are worth it in the end of the day.

Best way to solve the problems with those oil lines? braided lines!

Yep the oil and water lines can be a bitch to put back on, hopefully you put thte copper washes back in to otherwise they will end up leaking if they already havent.Next time get some freeze spray in a can (and put it on first before you even undo any of the nuts) similar to inox/wd40 it freezes the bolt or stud so shrinking it slightly and to 'crack' (Not literally) the join, then it gets down into the thread to then act a a lube, its good guys only about $15 a can from auto places.

Hey I've just started up my car since putting the turbo back on and the new dump pipe and there seems to be a bit of steam/smoke coming from the turbo area. i got a new gasket for the turbo flange to dump pipe and just reused the gasket from the turbo to exhaust manifold as it seemed in good condition. I reconnected all the oil and water lines properly so im wondering where this smoke could be coming from? Im afraid to start it up again now

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Yeah the rule of thumb with an LS is 7psi per 1000rpm. That is decidedly not enough at 6800rpm. I mainly looked for the scenarios where knock started to be picked up and it was later in the session when things were hotter, and oil was thinner, and the pressure was lower than it should be. (i.e very horrible). I am hoping with thicker oil (I was running Penrite ten tenths 10-40, the manual specifies 10-30) that does not leak that it's much improved at that time!!! I am using Project Mu Club Racer CR pads. I'm also using the Project Mu 335C fluid. The symptoms imply that it was fluid that boiled, but no bubbles seemed pretty weird to me when I bled it today. I want to try Castrol SRF as it has a much higher wet temp but, well, I have new Project Mu fluid lol... so I should at least use that. The pedal on track was really noticable. It went from basically normal feeling to instantly near-floor. The car did pull up as before, it was just very much nearly at the floor before the brakes engaged. At that point I pretty much decided the day was very done, it did *kinda* come back during that very slow cooldown lap into the pits. Felt perfectly fine driving home.
    • f**king around with the bro
    • Ludenham   44.2 tops day no issues  
    • Then today, I went to visit a man with an r33 hat Peter and Road and Race sorted the alignment. As it is being set up for general track/hillclimbs etc it has a heap of caster (7o), less camber than I am used to (1o front and 2o rear, as the caster looks after that in turns without the braking downsides), 3mm front toe out and 0 toe rear. Will see how that goes and track tyre wear to see if it does need more camber, but adjsustment is also limited with nismo arms and adjustable bushes at only 1 end. It does have a bent inner tie rod on the driver's side front but as it came up within spec I'll just leave that as is. So, that is getting close to my chapter of this story....could of tidy ups then a shakedown in early October before it finds a new home.
    • So, it went to Unigroup for a run in and tune on Friday, everything went (generally) well. In terms of fixes, the engine was good and there were no leaks. It needed plugs (I hadn't checked them because the coil pack cover was on a new engine and I couldn't imagine they weren't new.....but turns out the temporary plugs to just keep it sealed up were in there.....new plugs gapped to 0.8 and it was fine from there. Also, there was a little preload on the clutch slave which caused some slip. I haven't had the box off so I don't know what the clutch looks like; my guess it is brand new and the pedal had not been adjusted....backed that off a bit and it held fine. Last thing will have Dose crying....the idle especially when cold is a bit difficult between the cams, forward plenum, atmo blow off valve and an 80s air management system. It is fine when hot but a little uneven when cold, will see if I can sort or at least improve that one cold morning. Other than that, tuning went fine. It made 245 but was pulled back to 227 which 2 opportunities to improve in future. 1. The factory CAS is not great and was jumping around at high RPM, so Mark took 2 degrees out up top (that is why it stops making power and lost 20kw). Very safe this way and the extra power is available but will require a more modern ECU and better cam (or even better crank) sensor 2. The 2871 in factory housings is very big for a low mount, and the internal wastegate is too small, so it was creeping from mid range all the way to redline....the duty cycle on the boost controller is turned down a little for safety. That is much harder to fix, it would need a large external gate and that would require a whole bunch of other changes, so it will go as it is for now. It feels nice and healthy and safe, so should be good for about a billion laps like this.
×
×
  • Create New...