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R32 bonnet carpet cover, in good condition $30

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R32 bash plate sits underneath car, stock, plastic $20

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R32 boot, little dent at the top, no spoiler $50 or make anoffer

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R32 3inch jasma cat back EXTREMELY QUIET, have passedroadworthy with this $350, has all heatshields and hangers in very good condition

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Stock r32 cat $50

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Stock r32 front pipe $50, have a stock dump as well $50

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Rb20 gearbox crossmember r32 $50 each, have 2 in stock

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Type m pod driver side $50

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Various clutch masters and slaves $20 each for rb20 r32

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Stock sway bar rear sway bar for r32 $20

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R32 boss kit, used to fit nardi, good condition, also comeswith stock bit to make it fit $50

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Passenger side vent in awesome condition $50

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Middle vent with plastic surround $50

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R32 passenger side control arm $50 with good ball joint

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Stock r32 steering wheel, was used to pass roadworthy $50

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Cluster type m $50

Cluster surround $30

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Rb20det stock ecu $120

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R32 stock airbox mangled but good for clearing defects $50or make an offer coems with apexi filter

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Located in north western suburbs Melbourne

Pm or call 0413 926794

Best to call, don’t have a skyline no more so don’t come onhere

safc sold

centre vent surround sold (centre vent is no longer available as i mistaked it for silvia)

exhaust sold

bash plate sold

clutch slave and master all gone

everything else available

  • 3 weeks later...

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  • Latest Posts

    • f**king around with the bro
    • Ludenham   44.2 tops day no issues  
    • Then today, I went to visit a man with an r33 hat Peter and Road and Race sorted the alignment. As it is being set up for general track/hillclimbs etc it has a heap of caster (7o), less camber than I am used to (1o front and 2o rear, as the caster looks after that in turns without the braking downsides), 3mm front toe out and 0 toe rear. Will see how that goes and track tyre wear to see if it does need more camber, but adjsustment is also limited with nismo arms and adjustable bushes at only 1 end. It does have a bent inner tie rod on the driver's side front but as it came up within spec I'll just leave that as is. So, that is getting close to my chapter of this story....could of tidy ups then a shakedown in early October before it finds a new home.
    • So, it went to Unigroup for a run in and tune on Friday, everything went (generally) well. In terms of fixes, the engine was good and there were no leaks. It needed plugs (I hadn't checked them because the coil pack cover was on a new engine and I couldn't imagine they weren't new.....but turns out the temporary plugs to just keep it sealed up were in there.....new plugs gapped to 0.8 and it was fine from there. Also, there was a little preload on the clutch slave which caused some slip. I haven't had the box off so I don't know what the clutch looks like; my guess it is brand new and the pedal had not been adjusted....backed that off a bit and it held fine. Last thing will have Dose crying....the idle especially when cold is a bit difficult between the cams, forward plenum, atmo blow off valve and an 80s air management system. It is fine when hot but a little uneven when cold, will see if I can sort or at least improve that one cold morning. Other than that, tuning went fine. It made 245 but was pulled back to 227 which 2 opportunities to improve in future. 1. The factory CAS is not great and was jumping around at high RPM, so Mark took 2 degrees out up top (that is why it stops making power and lost 20kw). Very safe this way and the extra power is available but will require a more modern ECU and better cam (or even better crank) sensor 2. The 2871 in factory housings is very big for a low mount, and the internal wastegate is too small, so it was creeping from mid range all the way to redline....the duty cycle on the boost controller is turned down a little for safety. That is much harder to fix, it would need a large external gate and that would require a whole bunch of other changes, so it will go as it is for now. It feels nice and healthy and safe, so should be good for about a billion laps like this.
    • what sort of caliper are they? If they are a slider and you gave everything a good clean, you might need to regrease the pins. My guess though is they will come good after some abuse as suggested above
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