Jump to content
SAU Community

Recommended Posts

should be making over 300 on that boost with that turbo so deffs something wrong there

yeah as i said i have problems with ecu sensors jumping all over the place so it is only a half tune and im not really going for max power

  • 3 weeks later...

need to think/find a new muffler/pipes for the back as the cannon thats on there sucks ass and im thinking twin tip but not sure even another cannon that looks better and sounds better would do please discuss!!!

_MG_6436.jpg

spent saturday down hobart helping frenchie out with his bus at the round 3 drift day was a good day besides small miss hap that ended the day but the day gave me a boost to do a bit of work on mine today as im still waiting for wiring to get down before it can go back to have the tune finished :down: so just done some fiddly things started fixing a dicky power window and after taking the door trim off found the car had the intrusion bar cut out and a large rhs frame welded in to the door like a heavy duty crash bar or something super strange and have no idea why its been done as the doors have had no repairs or new skin welded to it

IMG_5460.jpg

other news brought first pair of wheels vskf in 17x9 +18 and have another pair soon 18x9.5 +18

hks oil cooler and oil filter relocation on the way a stainless twin 3inch pipe being made

IMG_1816.jpg

  • 2 weeks later...

damo come done last of the wiring on saturday air temp sensor in earth for the ecu fixed power steering fixed heap of wires cleaned up and neatened and is going back in to have the tune finalised this week and some actually good power figures will be up soon the kfs and going in tomorrow to have tyres changed over and try to get them back on and ply with camber and what not to make them fit ready for tune

well not the best news.. after having the wiring issues fixed on the ecu what we thought was a bad earth that was making the sensors (tps,water temp) gitter and making the motor run super rich i then took the laurel back to the tuner (boost automotive) car had to stay there for a day or 2 as he had to tune the cold start and finalise everything else got a text the next morning and was told the car is still not right and is still all over the place as you can imagine i wasn't after stuffing around with the car for so long and and this ecu so that night wiring mate (DJRIFT) went back through the wiring trying to find a bad earth or bad anything started to think as the ems runs off the ome ecu some of the sensors may of been doubled up and that was making things gitter and go all over the place fixed a few wires sent it back there the next morning still no go better but still no go so this weekend we went back over everything with a borrowed laptop to see if we could get it to work we really went through everything tested every wire and every ground nothing we could do seemed to fix the gitter :( we pull the ems out to check the ecu its self we found what may be sign of water damage and to the computer its self so in the end we have out it down to that the ems ecu has shit its self pretty much from water damage or just from age or bad luck and have now been set back more with having to buy a new computer and im not going to put a cheap half ass computer in it im looking at a haltech platinum pro unsure just sad on the hole car at the moment waaaaa :down:

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • My theory would revolve around the ~4000rpm point being peak torque territory on an RB, where you're supposed to be looking at max efficiency of the head, etc, and....just not having it because the skinny ports are doing something to f**k it up. I'll admit, it's a loose theory.
    • It could be in the tune but in both cases it couldn't be completely solved or eliminated by some of the best tuners in victoria so I'm DOUBTFUL that it's in the tune or ECU but stranger things have happened of course. I've pondered that theory too but is there any theories that thinner and smaller ports overall would cause a turbo to spike? I would've thought it would just restrict it in general if it was small enough to make a difference. I wouldn't expect it to make a different at what is essentially sub 300kw at 4000rpm anyway. I think the next step is going to have to be the 6psi spring to rule out the idea that the gate is cracking open far too wide initially. At least that is the cheapest (free) thing to check initially.
    • I'm thinking it is skinny NA Neo port sizing and cams. Somehow.
    • -5’s did it. 8474 did it. Not hot side related. ECU related? 🤨🤪
    • Above you mentioned you only need to sand primer if there's an issue with it but with fillers it says the surface needs to be sanded to X grit beforehand. Does that sorta contradict that point as the primer hasn't been sanded yet? At the same time if I sand the primer, there's a good chance I'll expose the bare metal and I'm just chasing my tail at that point. Or I'll just use a sand sponge instead of sandpaper, it seems to be far finer in terms of abrasiveness as opposed to sandpaper. From what I understand, filler is like primer and needs scratches from the sandpaper to help it adhere to the panel. I realised the way I'm doing things is actually a bit counter productive as there's a chance after I put filler I will need to put epoxy primer again as opposed to putting the filler first and potentially no primer if I don't go to bare metal. Will keep this in my mind for the rest of my repairs.
×
×
  • Create New...