Jump to content
SAU Community

Recommended Posts

So i recently purchased an m35, knowing it had an overheating issue. I knew it would 99% be headgasket blown! Only 70km on the clock.

Thankfully the motor looks on great nic on the inside! I was also happy to note that the coolant didnt blow through into the oil galleries - which has made the repair job much easier!!!

These things are built tough, ive played with vq35's a hell of a lot previously and RB's. I am falling in love with the design of these motors. Thick sleeves, large coolant volumes around the sleeves which the 3.5 block doesn't have. Good pistons.

That centre blanking cap in the middle of the valley I think is used for a coolant control valve in the US market? Inside mine looks to have boiled under there and acted as a small air lock. I'm going to link from here and the factory bleeder valve to a bubble tank - hopefully alleviating air lock issues in the future!

post-137370-0-13526200-1414895316_thumb.jpg

post-137370-0-77462300-1414895338_thumb.jpg

post-137370-0-31803800-1414895362_thumb.jpg

post-137370-0-78595100-1414895385_thumb.jpg

Link to comment
https://www.sau.com.au/forums/topic/450283-dreaded-vq25det-headgasket/
Share on other sites

Scotty_m35 makes a bolt up coolant mod that works similar to the us version and also has a nice bleed valve added in. We'll wprth the investment

Any pics or links to the system he uses? I am just about to order an fittings and weld ons.....

Any pics or links to the system he uses? I am just about to order an fittings and weld ons.....

Search the forum for scotty's m35 coolant mod.

Pretty reasonably priced for the product and the quality of his workmanship.

Also Google scotty's customs. He has a website and produces a lot of bolt on m35 parts that are proven to produce the goods.

Also look at his dump pipe, it's the best there is

Oh, to answer the question on the extra coolant gallery, it was a feature on some of the other motors in some of the other motors inthe VQ range, that part of the "towing package" would feature an additional coolant passage with separate thermostat.

Here are the parts :)

http://www.z1motorsports.com/350_g35/product_info.php?products_id=3011

Good job opening it up, and sorting out the issue btw.

Except those parts won't fit the M35. ;)

Overheating doesn't mean the head gasket is gone in these, so anyone reading this later, check you have properly bled the cooling system, or fit my coolant mod kit before ripping the engine out. Please. It will save you a lot of headaches.

  • Like 1

Definitely not, plus the outlet pipe to the radiator is completely different.

No idea why you would need another two thermostats either, just another part to fail.

My kit uses the heater line to bypass coolant from the block, rather than relying on the one small pipe at the back of the engine. It also replaces the plastic bleed assembly with alloy which is another common failure point.

Except those parts won't fit the M35. ;)

Overheating doesn't mean the head gasket is gone in these, so anyone reading this later, check you have properly bled the cooling system, or fit my coolant mod kit before ripping the engine out. Please. It will save you a lot of headaches.

Correct! However - these being open deck - often will warp the heads. The whole VQ range from my experience does not suffer to well under heat - ive seen them where they even warp through the cam tunnels!!!

Of course i didnt just take a punt - i knew it was head gasket before ripping it out.....

Often? I've had mine at 150C at the track on many occasions, it never lifted or warped the heads, even at 40psi up the straight... Being alloy block changes things, as the expansion rates are similar, unlike iron block/alloy heads.

If the heads are warping that bad there is an airlock causing no coolant to flow, which is the common VQ fault I tried to alleviate with my coolant mod design. As the bore and heads overheat they cause flash boiling which exacerbates the problem.

Often? I've had mine at 150C at the track on many occasions, it never lifted or warped the heads, even at 40psi up the straight... Being alloy block changes things, as the expansion rates are similar, unlike iron block/alloy heads.

If the heads are warping that bad there is an airlock causing no coolant to flow, which is the common VQ fault I tried to alleviate with my coolant mod design. As the bore and heads overheat they cause flash boiling which exacerbates the problem.

Well when you are running ARP head studs i would hope you don't have issues!!! FYI i've gone back to OEM studs - ditched the angular torque and run my own torque values (105NM final value). Angular torque on a used block is a waste of time and generally ends in uneven torque values.

The issues with OEM bolts and open deck comes down to contact surface area. Nothing to do with iron alloy mixes....that wasn't even on the pallet for discussion haha. Like you say - flash boils - but the residual heat in the open deck decreases the dynamic torque of the studs and allows warping and reduced pressure between bolt spreads. When the pressure between the cylinders lifts obviously they blow through. I have never actually seen a VQ blow through on the outside of the open deck and lift to an adjoining oil passage - always happens middle of block between coolant chambers.

I've blanked off my radiator cap. Fitted my own bubble tank with the pressure cap, teed off from turbo water feed (base of turbo), centre of valley, teed off top of thermostat and bridged and removed OEM plastic bleeder.

I must say however I do prefer the VQ25 block over the same era VQ35 blocks. These blocks are much more boost friendly with a thicker sleeve and larger volume coolant chambers surrounding the sleeves. Also the OEm metal gaskets are very good - however I don't like they fact they pre coat them with the teflon/graphite mix. I threw mine in the light costic wash for a few hours to get rid of the coating :)

Edited by DMM

Could you give the reasoning behind not wanting to use angle torque on a used block?

It is my understanding that angle is used to remove the error caused by varying amounts of friction acting on the thread, interfering with the actual clamp load and stretch of the bolt.

How does the block being used negatively affect that?

I only fitted the ARP's after running unlimited boost, lifting a head. I also ran the car hard for a year before the head gasket finally let go in a big way on the dyno. Like you say the extra meat of the bore is what helps us VQ25 guys, comparing it to the VQ35 is silly, they are very different as you have found.

OEM gaskets here, with extra Hylomar spray. 105nm sounds like a lot on stock bolts...they will have twisted nicely. Did you lube the threads at least, and clean the threads in the block?

Could you give the reasoning behind not wanting to use angle torque on a used block?

It is my understanding that angle is used to remove the error caused by varying amounts of friction acting on the thread, interfering with the actual clamp load and stretch of the bolt.

How does the block being used negatively affect that?

Ive found in the past angular torque stretches the block threads heavily. There have been some situations where a customer has requested a certain bolt with angular torque and it pulls the thread. The only way i've found against this is using helicoils to increase thread depth contact area. Mathematically when you use stretched alloy the thread bolt only touches around 60% of possible mating thread in the block.

If it was all brand new then nothing wrong with angular as yes you are right - helps eliminate error.

I only fitted the ARP's after running unlimited boost, lifting a head. I also ran the car hard for a year before the head gasket finally let go in a big way on the dyno. Like you say the extra meat of the bore is what helps us VQ25 guys, comparing it to the VQ35 is silly, they are very different as you have found.

OEM gaskets here, with extra Hylomar spray. 105nm sounds like a lot on stock bolts...they will have twisted nicely. Did you lube the threads at least, and clean the threads in the block?

No twist - prepared in layers. Cleaned and oiled of course. Process as follows:

1)Spun bolts in and out 3 times to distribute oil evenly and wipe off excess after each spin.

2)Check block temp - anything over 25degree at 0.15% NM for every 1 degree over 25.

3) Torque all bolts to 65NM. Let gasket squish and settle.

4) Torque to 90NM - let set over night

5) Release bolts, remove and check oil coverage. You will see ghost marks on bolts if oil coverage is poor, otherwise will have nice even moist look.

6) Nip to 90NM again - just touch 90, no need for high tension load.

7)Torque to 105NM and finished.

No bolt groan, no binding, no twisting process! Used this many time over the years on RB, SR and VQ engines. A lot have seen the loads of bathurst etc without engine failure.

It won't matter how tight the bolts are done if you don't fix the coolant issue. Surely you would have known about that with your VQ racing expertise?

I chose to do my bolt tensions that way to reduce twist or shift. Not to stop a head gasket from lifting. Gaskets are designed by nature to be the weak point.

Coolant issue is as you have said - failure to flow out the back of the block/heads. The two passages out of the rear of the heads are tiny and restricted from flow heavily. This is why is I'm adopting the centre relief in the valley to help with flow.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • And finally, the front lower mount. It was doubly weird. Firstly, the lower mount is held in with a bracket that has 3 bolts (it also acts as the steering lock stop), and then a nut on the shock lower mount itself. So, remove the 3x 14mm head bolts , then the 17mm nut that holds the shock in. From there, you can't actually remove the shock from the lower mount bolt (took me a while to work that out....) Sadly I don't have a pic of the other side, but the swaybar mounts to the same bolt that holds the shock in. You need to push that swaybar mount/bolt back so the shock can be pulled out past the lower control arm.  In this pic you can see the bolt partly pushed back, but it had to go further than that to release the shock. Once the shock is out, putting the new one in is "reverse of disassembly". Put the top of the shock through at least one hole and put a nut on loosely to hold it in place. Put the lower end in place and push the swaybar mount / shock bolt back in place, then loosely attach the other 2 top nuts. Bolt the bracket back in place with the 14mm head bolts and finally put the nut onto the lower bolt. Done....you have new suspension on your v37!
    • And now to the front.  No pics of the 3 nuts holding the front struts on, they are easy to spot. Undo 2 and leave the closest one on loosely. Underneath we have to deal with the wiring again, but this time its worse because the plug is behind the guard liner. You'll have to decide how much of the guard liner to remove, I undid the lower liner's top, inside and lower clips, but didn't pull it full off the guard. Same issue undoing the plug as at the rear, you need to firmly push the release clip from below while equally firmly gripping the plug body and pulling it out of  the socket. I used my fancy electrical disconnect pliers to get in there There is also one clip for the wiring, unlike at the rear I could not get behind it so just had to lever it up and out.....not in great condition to re-use in future.
    • Onto the rear lower shock mount. It's worth starting with a decent degrease to remove 10+ years of road grime, and perhaps also spray a penetrating oil on the shock lower nut. Don't forget to include the shock wiring and plug in the clean.... Deal with the wiring first; you need to release 2 clips where the wiring goes into the bracket (use long nose pliers behind the bracket to compress the clip so you can reuse it), and the rubber mount slides out, then release the plug.  I found it very hard to unplug, from underneath you can compress the tab with a screwdriver or similar, and gently but firmly pull the plug out of the socket (regular pliers may help but don't put too much pressure on the plastic. The lower mount is straightforward, 17mm nut and you can pull the shock out. As I wasn't putting a standard shock back in, I gave the car side wiring socket a generous gob of dialectric grease to keep crap out in the future. Putting the new shock in is straightforward, feed it into at least 1 of the bolt holes at the top and reach around to put a nut on it to hold it up. Then put on the other 2 top nuts loosely and put the shock onto the lower mounting bolt (you may need to lift the hub a little if the new shock is shorter). Tighten the lower nut and 3 upper nuts and you are done. In my case the BC Racing shocks came assembled for the fronts, but the rears needed to re-use the factory strut tops. For that you need spring compressors to take the pressure off the top nut (they are compressed enough when the spring can move between the top and bottom spring seats. Then a 17mm ring spanner to undo the nut while using an 8mm open spanner to stop the shaft turning (or, if you are really lucky you might get it off with a rattle gun).
    • You will now be able to lift the parcel shelf trim enough to get to the shock cover bolts; if you need to full remove the parcel shelf trim for some reason you also remove the escutcheons around the rear seat release and you will have to unplug the high stop light wiring from the boot. Next up is removal of the bracket; 6 nuts and a bolt Good news, you've finally got to the strut top! Remove the dust cover and the 3 shock mount nuts (perhaps leave 1 on lightly for now....) Same on the other side, but easier now you've done it all before
    • OK, so a bunch of trim needs to come off to get to the rear shock top mounts. Once the seat is out of the way, the plastic trim needs to come off. Remove 2 clips at the top then slide the trim towards the centre of the car to clear the lower clip Next you need to be able to lift the parcel shelf, which means you need to remove the mid dark trim around the door, and then the upper light trim above the parcel shelf. The mid trim has a clip in the middle to remove first, then lift the lowest trim off the top of the mid trim (unclips). At the top there is a hidden clip on the inner side to release first by pulling inwards, then the main clip releases by pulling the top towards the front of the car. The door seal comes off with the trim, just put them aside. The the lighter upper trim, this is easy to break to top clips so take it carefully. There is a hidden clip towards the bottom and another in the middle to release first by pulling inwards. Once they are out, there are 3 clips along the rear windscreen side of the panel that are hard to get under. This is what the rear of the panel looks like to assist:
×
×
  • Create New...