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CRSKmD

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Everything posted by CRSKmD

  1. Fun Fact the diff did ~ 3,984,053 revolutions in my ownership before the bolt worked itself out and caused real problems
  2. I acquired another stock R200 and have pulled the broken diff out the car. I am going to take them both to 1110 this week and go from there. Hopefully the centre is salvageable but if not a new 2-way centre, probably KAAZ or OS-Giken, will be needed. I am open to recommendations for good 2-ways (any recommendations of jUsT WelD iT/ JUSt sHiM iT will be ignored). Here are some extra photos of the carnage
  3. unsure but the diff has been in the car since ~2017. I bought it used but had alleged been checked over. Either way that's 30-40 track days + street driving. Shocked and impressed i did ~30mins drifting + 120km ont he freeway with it likely in this state
  4. Further investigation found that a ring gear bold had come loose and punched a hole in the housing before presumably being grabbed by the magnet.
  5. Went up to The Bend for DSA Winterfest the other weekend. Primary as a volunteer to help out but with an opportunity to do some driving later in the day. Had a bit of time on both the skidpan and my first proper sessions on the main track. Between sessions we thought there was the smell of gear oil but couldn't see any drips and assumed the freshly installed gearbox may have been slightly over full and was coming out the breather. Called it a day and drove home. Half way home there was a very loud whining sound which came and went based on load. The weather was very windy with the threat of a storm rolling in so I kept on my way. I was fearing that the freshly rebuilt gearbox was the cause of the noise. After making it home I had a good look under the car and... . Left it in the carport overnight and got some sleep
  6. Other box was pulled down and inspected. This was the selector fork. The remains of the box can be salvaged into a good one with the help of some new synchro's, bearings, sleeves etc along with of course a new selector fork. So the plan is to get that done and keep it on the shelf
  7. Unfortunately the follow event I found an extra two neutrals where 3rd and 4th were when heading down the main straight at The Bend. So for only the 2nd time in 10 years I was unable to drive home from a track day. A full pull down of the bad box has yet to happen but I did fish these out of the oil. Which I can only assume are off the 3rd/4th gear selector fork. Luckily I had a spare box with crunchy syncros I'd left neglected in the corner after changing it it for the now broken box. So it went off to 1110 Engineering for a refresh, New syncros, bearings and seals as required as well as upgrading the selector fork to a fancy steel version to prevent any issues with finding extra neutrals in the future. When compared to the stock selector which only contacts on the brass tabs the steel ones gives a much more direct shift with less chance of snapping. This design also includes provisions for oil to collect/cool/lubricate. I was told by Richie that the stock selector forks tend to wear in three stages; Brass pads worn, ribbing worn, snapped The initial drives of the refurbished/upgraded box went okay. It was a little stiff to get in and out of gear for the first 10kms or so but loosened up to be nice while still being very crisp. The broken box will be off for an inspection and hopefully refurbish soon where it can sit in the shed for when I inevitably need another box haha
  8. Couple of drift and grip days to try out the new setup. Overall an improvement but the front does seem to suffer a little due to reduced travel caused by the stiff bump stops along with the Stanceparts air cups. Next time I hope to get some 20mm longer front struts to compensate. The current setup allows from 35/35mm bump/droop travel up front + additional bump stop compression. Rear wise its at 45/45mm bump/droop travel. The ride heights are set relatively high in order to ensure full travel usage without scrubbing and maintaining good suspension geometry. Please enjoy this POV clip of me in the RB25DET NEO R32 sedan chasing Justin Miller in the Golden Sloth Racing - Time Attack SA80 3SGTE Supra at SA Supra’s Mallala Motorsport Park track day.
  9. Update time. After cracking the shits at the oil temps in my car i decided to relocate the Oil cooler from behind the grill to inside the drivers side front bar duct. Hoping the increased airflow would help with the performance of the cooler. Previously it would take almost a full lap of the track or multiple car park loops to bring the temps down but after relocating the cooler it takes.... about the the time to cool down. I had it ducted the core when behind the grill but have yet to add ducting for the bumper mount so this gives me hope that there is more cooling to be gained. While faffing it was also time to pull out the Shockworks coilovers and send them off for a refurbishment and updated valving along with new spring rates. I had been speaking with Chris and Brett about some of the handling quirks my car had and what i wanted from it considering it had been 3 years since them going in. They even sent me a new revised design coilover C-spanner as park of the service which was very neat. I put the coilovers back in completely re setting up the bump/droop and strut lengths while doing so. Covered previously for anyone interested.
  10. CR-S Update While they are allegedly better in wet conditions than the AR-1 my experience was not great. But i guess 1 better than 0/100 is still only 1/100. I will go through the footage i have, but aquaplaning appeared to me much more of an issue than with the AR1's i suspect this was due to the lack of full thread width grooves for the water to escape/be displaced through.
  11. The Nanknag CR-S is a very different tyre than the AR-1. they were pretty much as robbo_rb180 said. but here are my thoughts and comparisons to the AR-1 in the same Size The Good Road noise greatly reduce (at least while tyre is new) Faster to heat up. just the outlap and basically up to temp by the time you came back around. vs 2-3 laps to warm up the AR-1 Faster to cool down if you don't completely cook them could realistically get them to go 1 warm up, 1 hot, 1 cool, 1 hot, 1 cool etc by comparison the AR-1 needed 2-3 warm up, 2-3 hot, 2 cool down despite the 200TW rating (Tread Wear =/= tyre compound softness i guess) they were gripper than the AR-1. On AR-1 my brakes could easily over come the tyre when at ideal temps where as now its better matched. My suspension almost felt too soft and there was noticeably more roll leading me to believe that the tyres were sticking more leading to more suspension lean where as the AR-1 in the same spots would slide The not so good Only good for ~1-1.5 laps at a 2.6km circuit before they need to cool off The 255/40R17 CRS seems to be taller and slightly wider sidewall to sidewall than the 255/40R17 AR-1 Could just be my car but they didn't seem to "talk" as much as the AR-1 when approaching the edge and would appear to suddenly "let go" Post to follow with track day wrap up thoughts, video and pics
  12. extremely good info thank you. As for being faster we'll see what 2 years of basically only drifting and associated car changes does to my PB from when I did 6 track days at the same track in a row
  13. Oh nice did you have your car there too? my only good comparison will be against the AR1's in the same size. I found on a 2.6Km track it would take 1-3 laps to get them up to temp, then I would get 1.5-2 laps before they got too hot, followed by 1 cool down lap. went out at 21psi cold and if I came back in directly after I overheated them it would be 36-46psi. or coming in after a good lap ~29-31psi
  14. After ~6month break from Motorsport events I signed up for a grip day at Mallala. I decided to try out some new tyres in the form of the Nankang CR-S in a 255/40R17 which I fitted up to my street wheels (the Gram lights) as they were the roundest lol before there was time for an alignment it was All Japan Day 2023 even found this at one of the stalls After the day was done and dusted a mate that was also doing the same grip day came over for us to install some parts and adjust anything that was required. The RA65 ended up with a fully adjustable front end and for the R32 its was raising the height back up to where it was when the shockworks coilovers were first installed as they had settled ~5-10mm over the years and replacing the eccentric bolts that were left with some lock out ones to reduce the chance of the alignment shifting on any off-track adventures. Unfortunately, this meant that my trusty subframe brace/low jack point had to go as the eccentric lockout bolts were not long enough to accommodate both the brace and the washers. Then it was off to the alignment and I went with the below fairly conventional specs Front Toe: -1.5mm toe out each side Camber: - 3.8° degrees Caster +7.4° Rear Toe: 1.75mm in each side Camber: -1.4 ° fun note the last grip day I did on my ad-hoc drift alignment was done with -12.5mm toe out each side for a whopping 25mm total toe out!
  15. after talking to some other drivers i tried to down size my front tyre but up-rate the compound grip So i went from a 235/45R17 street tyre to a tiny 215/50R17 semi. certainly was an obvious visual change But thankfully also an improvement as can be seen in the mash of clips filmed by me and some friends during the day. Enjoy! also safe to say the rear end alignment and arm setup is working well
  16. Next event was a drift day out at Mallala. After some struggles early in the day I was told to try and wind in some more toe out. Good improvement at turn in and mid corner for the higher speed bigger corners. All was going well until about lunch time when after looping it out (again). The car stalled and wouldn't start. Bump start got me going and home where I tore down the starter motor down to find... I sourced a new RD30(?) start motor which was much larger than the old unit was and definitely started up much easier. Despite the larger size it dropped straight in. While under the car replacing the starter motor I noticed a few problems in the form of a missing steering rack bushing alloy spacer and some more than usual oil leaks which I traced to the rubber section of the oil drain hose.
  17. I would suggest taking a look at Shockworks over MCA's but same idea much better suspension can give you a nice comfy ride AND a firm track setup. Instead of just being lower and stiff like BC,HSD, ISC etc
  18. Soon to be super fresh with all the new little touches parts you’re making!
  19. the AAC/IACV had issues on the dyno resutling in a 3000-4000rpm idle hunt which i had previously experienced and resoled with a big stab of the throttle. We gave it an ultrasonic bath which revealed that the vax pellet in the cooland controlled side had vanished. found and cleaned up another one and now for the first time ever my car has a stable 750rpm idle which is kinda of weird. A mate of mine was fed up with my flogged radiator upper mount bushings, which had been an issue for many years, and got me a set from JL Design and Fab / Fitmint auto. Before. After.
  20. Back at home I got stuck into the investigation for the cause of my fuel system woes. Opening the tank up expecting to see debris or a blocked filter sock but it was clean inside. I decided that the Denso Lift pump and the Bosch 044 could simply be too old and had started to fail after years of running in E85 considering neither were technically compatible with Bosch themselves only saying the 044 was good for 500hrs in E85. The 044 at least was more than 5 years old running on E85 the whole time. I purchased a Raceworks EFP-501 low pressure high volume E85 compatible pump for the lift pump and the new Bosch 200 E85 compatible Main pump to replace the 044. Interestingly the terminal sizes are swapped from: small OD (-) and big OD (+) on the 044 nicely colour labeled to Big OD (-) and Small OD (+) on the new 200 with no colour coding During the install I found that the hose from the in-tank lift pump to the surge was prone to kinking which may ahve been the real source of my problem I replaced the effect hoses and in order to help prevent this I added some conduit to avoid future kinking (yes i am kink shaming my hoses) All installed and hoses routed. The positive battery cable needs to be rerouted with a new isolation switch all running well with nice stable fuel pressure I booked it in for a dyno health check in case the new pumps were dramatically different to the old ones.
  21. Shakey cam video of the fuel pressure woes
  22. Bit of a gap between updates but I can confirm the injector seals worked. I entered Winterfest2022 with the hope of getting bulk track time as it was a 9am-9pm day with multiple sessions per group. However, my fuel system had other plans after. Almost immediately after driving out on track I could hear cavitation and watching the fuel pressure live reading it was jumping between 40-60psi with quick succession on cruise. I gave it a quick go and sure enough the LINK said no drifting for you and cut power to protect the motor. With no spare fuel tank o-ring seal on hand i was hesitant to remove the lift pump and look inside the tank due to the known swelling issue they have once removed. So with a few friends we checked over the whole rest of the system jiggling hoses and checking voltages. With nothing found there we were thinking perhaps a blocked fuel filter was the culprit. So we went off to Murray Bridge to grab one. After installing it the fuel pressure looked stable around 60psi on idle...for about 10 minutes when it was fluctuating again. I decided to go back on on track but after the first corner it was pretty obvious that there was no significant improvements. Anyway enjoy the surprising amount of pictures i have from the day
  23. Considering the stock neo injector uses ORings top and bottom and the injector is the same length as my current ones it should not be an issue as is. Just feels off.
  24. Gave the engine bay a good look over before a two day back to back event coming up. Noticed some slight discolouration around the injector lower seals but of course the combination of injectors and rail meant it was near impossible to remove without splitting the plenum and removing the throttle body. after going back through my own thread to realised I had installed it with the plenum apart when i was refreshing the motor. Once I pulled them out to inspect the seals and this is how most of them came out Got a whole new set of the same lower insulator seals I had on there and no mater how evenly I did up the fuel rail or how much silicon spray was used they ended up sitting like this. It just did not feel right. After some solid googling i realised that the RB25DET NEO ran an O-Ring top and bottom as seen on this stock injector. Luckily l was able to grab a set of O-Rings from Garage 7 The fitment seemed much better. Though I am yet to drive the car under boost which is a little concerning if they are not the seals I should be using. As i had to remove the TB during the process I ended up destroying the gasket and was not able to get another one easily/quickly. Luckily I happen to own a Vinyl cutter and with ~$1 of gasket paper I made one. While I had better access than usual I investigated my other phantom oil leak which seemed to be coming from the black -10 AN swivel fitting. Initially I tried to tighten it as it felt a little loose. Still leaked. My next thought is the hose was dud as the fitting seemed to tighten nicely. So I made a new hose and reused the fittings. I degreased the car and sat and watched it with a variety of torches. 5, 10 and 15mins of it idling at ~55C oil and ~77PSI oil pressure went by with not a drop. Great, switched it off and went about cleaning up the work area. When I heard it dripping like a tap. Not a drop when running under pressure but once the car was off away it went. Odd Took the hose out, cleaned it then did the ol' under water leak test... Grabbed a new fitting, Made yet another new line (we all know how much a PITA making braided lines is) and put it in. No leaks when running. Left it while I had dinner and came back and still nice and dry. Success! Now to hope the injectors still seal under boost. surely if the wrong seal swollen and smooshed was fine these will be?
  25. Gave the new suspension and alignment a good test out on the Drifting SA Skidpan at the Bend MotorSport Park. My thoughts: The extra grip and stiffness in the rear end made for a much more consistent and predictable car. There seemed to be reduced slop when going over centre up front which helped the steering on transition. Previously it would hesitate on centre and require some encouragement in the form of a quick steering stab. The extra rear end grip, even with pressures up a little than normal, required a more commitment to get it sliding. Or maybe its all in my head ¯\_(ツ)_/¯ I also tried some scando entries for the first time as well as using the handbrake to trim some angle off. Big thanks to the guidance from the instructors on the day, especially Daniel Prior. Enjoy a lap on board below and some great pics taken by a good friend. I have noticed that the outside edge of my front tyres have taken some serious wear. See the comparison with the rears which were not used for drifting. More front camber might be needed to prevent this and you can see in the pictures above that the leading wheels is positive cambered
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