Jump to content
SAU Community

Recommended Posts

hey all,

i just installed my hks evc3 :aroused: and gave it a fang and it seems ive got the some problemo's

- can't see boost below 0.74 bar

when in setting mode, im unable to scroll below 0.74 bar for some strange reason. not that i mind but i want to make sure the plumbing and everything is correct because no matter the car goes to about 9psi regardless, even if i set the boost to 0.90 bar its still about 9psi. on the stock solenoid it would run at 5psi then 7psi so it doesn't seem (well i think) that its got a different wastegate spring ?

- turning unit off does nothing

in the sense my boost does get set less or more

i mean by going from green to red mode and also cutting power to the unit

- unit doesnt show current boost level

this is because i haven't plumbed it in the manifold (will fix later)

well at least my understanding of it is, corrections anyone?

If I go boost set, and choose low mode its on 0.74 bar then if I goto high and set it to 0.90 not much happens really. It still seems to the go the same.

Has anyone seen this before? Port 1 goes to intercooler pipe, Port 2 goes to actuator and port 3 goes no where (soon to be fixed). The car feels to pull more and certaintly responds better so the boost feels like its there. I am using the stock guage so its probably out of whack but I should still be able to set the unit below 0.74 bar shouldnt I ?

I've checked manual, google, forum search and wiring plumbing

I still have stock intercooler and exhaust (soon to be changed)

Any ideas would be great thanks

Link to comment
https://www.sau.com.au/forums/topic/58560-hks-evc3-cant-set-below-074-bar/
Share on other sites

fear not, i have indentified one issue. the scan of the hks evc 3 manual i have is blurry and the numbers on the solenoid don't go in order

They go:

2 3 1

I thought it was:

1 2 3

1=intercooler 2=actuator 3=manifold pressure sensor

Will correct tomorrow, this should correct set 0.90 not working :P

Any ideas re: cant see any lower than 0.74 ?

on mine i had it set to .60 bar and .75 bar when i was running the stock turbo

was already set like that when i had the car tho

if i had my manual for it here i could tell u how to do it but my mate has it atm :P

i fixed the incorrect plumbing and the display now shows how much boost

however no matter what i set it wont boost over .045bar no matter how hard i try

ill do a full reset and get it to do its self learning evc mode and see if that helps

okay tried full reset and i cant even start the learning mode

it displays the '3" and its waiting, the manual says take off in 3rd and rev out until it beeps. the unit never beeps and i cant get out. awesome. double checked piping and tried it the other way around, 5psi non stop and just keeps displaying "3"

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...