Engine and gearbox ready to be taken off the subframe and dropped off at Race Pace.
Was originally going to suck it and see if the engine was ok, but thought better and ended up getting it all pulled apart. Was the right choice because there was an 8 thou bend in the middle of the crank, a spark plug tip had come off and damaged the bore a little, and the turbo bearing cages were not in the best shape.
New R34 crank, machining, 87mm pistons up from 86.5mm, new bearings and consumables, reco of the turbos and a good check over everything else.