Visited my girl this arvo but she is not ready to come home yet...
This is where she sits right now.
Power has increased but it's still not right. (up by 11kws) Still pinging but at least the timing is more normal now after the new belt went on.
Apparently it's acting like it has higher than normal compression. Could've had a head gasket replaced at some stage and maybe the head skimmed a little more than usual? Seems to make more power than it should at 10psi and seems to want to be on the leaner side, but Fuel Pressure is good.
Both John and Jake are a little unsure of what's up but they'll sort it.
Perhaps my AFM is a little dodgy.
Will take in my spare tomorrow or else I'll have to buy another one.