Jump to content
SAU Community

Recommended Posts

how a fuel injector ruined my life.

some of you may not know but i couldnt go to the trackday :rant: reasons being my motor crapped itsself finaly. well after 240000km of reliable service.

it started off as a missfire when it was cold in the mornings, just a light one. having a wideband afr meter made this easy to see that it was to lean on cold start up. easy fix, with the autronic i increased the cold start fuel multiplier. fixed :O

after 2 weeks it did it again :S so i re tuned the low rpm fuel sites for more fuel. that fixed it.

then.. the battery went flat, it some how lost its tune after sitting for a week. very strange.. so i retuned. fixed.

and after another two weeks it progressivly got worse and worse till it was missing under boost then just light throttle., so i did the logical thing and put a new set of plugs,and leads into it. that didnt help. ok..

so.. i thought it may may be the cdi unit playing up. i have a spare as one crapped its self earlier due to rain in it lol. it was a fixed one so in ti went. that made no differance. so i put some new coils in.

(the whole time chasing a spark issue.miss under laod while afr is ok)

the new coils made a slight differance. but still not fixed. i checked the wiring from it to the coils. turnes out the wiring was no good. so i made a new harness from the cdi to the coils. no change... f**k!!!

hrmm well i used my old bosses occiloscope to check the outputs on the ecu for the injectors and the cdi unit. they were ok. but being a lcd sreen scope the reponce was not quick enough to garentee a clean signal.

so for the hell of it i changed the crank angle sensor(i had to pull it apart and put a autronic chopper disc in it) that made no differance. gay!!

so out comes the compression testor. yay 5 was down. then 6, then 4, then 3. whoa my motor was dieing quick! ok so i used another comp tester. wtf it was all 140psi hrmmmm.. dodgy comp testor.

still missfirng, comp good. afr good, spark good. mayby its the ecu?? but not an autronic! mayby it was a broken valvespring. i recently put cams in.. so mayby the higher lift fatiged the old springs. oh well after a sold 10 hours changing the head over iin car. (not easy on a gtr) it still missed!!!! grrrrrrrr.

ok must be a broken ring land(s) cos they can give good compression and then not good as the ringland mioves around. oh well il just put my built motor in then.

soo on the weekend i swapped over my engines. pitty our work doesnt have a engine crane jjust a forklift and a big steel tabe. so it was out with the motor/box as one unit onm the crossmember.

anyway i got it done and wtf still missing. but now at idle. f**king hell. cos itr was at idle i could norrow it down to no.4 f**k waht is it.. i swapped my injectors around (there only a year old) and the problem moved. coool spo its a lasy injector.. i pulled the filter out of it and cleaned it. yay no more missfire!! woot and i have a new motor ready for 2 bar eheh

moral of this is never asume something is ok. ie..my new injectors and if its intimitant be prepard for what ive gone thru unless you put it on a dyno. it would of saved me a months stress for the sake a 1 hour on the rollers eek. :rant:

Link to comment
https://www.sau.com.au/forums/topic/175822-my-weekend/
Share on other sites

Bad luck man, like life you live and learn shit happens at least your mechanically minded, as soon as my car seems a miss or not running correctly i get my mechanic or tuner to ckeck it out. Now you have a built motor ready for 2bar boost yeeeeh haaa..

Link to comment
https://www.sau.com.au/forums/topic/175822-my-weekend/#findComment-3219967
Share on other sites

lol great story so many twists and turns....on the bright side you worked in out before you lunched the new motor as well.....

I've put a whole heap of std gtr injectors through flow testing and cleaning - and they all flow horribly....rated at 440cc/min none of them, even r34 freshly cleaned ones pumped more than 400cc/min (except a freak set of 4 from a gtir that did 450, maybe they had been highflowed).

I had a similarly frustrating issue that turned out to be dodgy fuel pump wiring, almost cost me a brand new motor because every time we tried to run it in it ran like crap (missing) causing fuel wash one the bores....very frustrating I swapped bloody everything (wish we had a fuel pressure gauge)

Link to comment
https://www.sau.com.au/forums/topic/175822-my-weekend/#findComment-3220465
Share on other sites

To4GTR,

lol quite an adventure. :S

Duncan,

400cc's was at 100% duty or Pulsed duty (80%)

I had a set of apparent low km R34 GTR injectors flowed and cleaned some time ago.

Before cleaning they were fine; after they were only slightly better.

Averaged 472cc @ 40psi (min 468 max 474)

After cleaning

Averaged 476cc @ 40psi (min 474 max 480

Pulsed duty (80%) they flowed 384cc to 390cc

post-382-1183972337_thumb.jpg

Link to comment
https://www.sau.com.au/forums/topic/175822-my-weekend/#findComment-3220569
Share on other sites

Sorry to hear Dave but the good thing is that your misfortune might lead to me fixing my problem.

At the moment my car is missing under boost.

Dont know too much about cars but i was thinking maybe air flow meter or fuel pump or something in the fuel filter blocking it, sparks, coils... never though to check injectors...

Ill change them and keep ya informed. Thanks again.

Soul.

Link to comment
https://www.sau.com.au/forums/topic/175822-my-weekend/#findComment-3221238
Share on other sites

I had a similarly frustrating issue that turned out to be dodgy fuel pump wiring, almost cost me a brand new motor because every time we tried to run it in it ran like crap (missing) causing fuel wash one the bores....very frustrating I swapped bloody everything (wish we had a fuel pressure gauge)

good story Dave! I wish I was able to sort problems like this my self!

And Duncan I hear you on the wiring issue :rolleyes: its the reason I missed the track day

Link to comment
https://www.sau.com.au/forums/topic/175822-my-weekend/#findComment-3221273
Share on other sites

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • A few small updates since the previous post and lessons. I decided to do a little interior light upgrade on the 110. I quite like the iilumo items, even if they're a bit of a premium over other brands. You'll also note the Stedi Fogs, that will go into the S15 fog lights as I needed to match the bulbs since I got the new ones earlier. I hope they fit as the body is quite a bit longer than your normal bulb.  Annoyingly, I managed to trip the fuse, which normally wouldn't be an issue until I located the fuse. I can't say I've ever come across this. I had lucked out that someone nearby had a spare, but oddly enough Toyota dealerships seem to keep this in stock. I ordered some to keep in my stash and as luck would have it, someone else nearby tripped the same fuse so I passed on the favour.  I also did a little service on the 110 ahead of some additional work coming up. It's been annoying that Goleby's stopped carrying this particular HKS filter for the 110, so now I need to keep them on order from Japan. I also took the opportunity to install a bash plate and number plate riser. The plate riser is such a cheap but nice fix to help really tidy up the car. I'm tempted to now also replace my headlights, on this car. Both items were from Project Aero.    I also needed to replace the rear tyres on the 110, and after trying to get it aligned learnt that I need to replace some bushes in the front end, so that's next.  Closing out this update with a nicer picture as always! 
    • Yeah mate, never miss it.
    • Any going to watch World Time Attack at SMSP this year?
    • Appreciate the correction on the "ground", that will make a huge difference to looking at this. That makes complete sense about AF70/AF71 which is what I had come down to being the issue, one of these. I'll have another look in the ignition wiring when I get a chance next week. I'll also make up a jumper wire for running that AF73 test.  ECU is fine, relay itself is fine, pump harness is fine and the pump itself is fine. I am going to upgrade the Walbro 255 anyway with a DW300 I have since I need to replace the fuel sender and I'm going to upgrade the FPR with my chasebays kit ready for new plenum/injectors/dbw, but I'll get this working first. That's why this is so frustrating. 
×
×
  • Create New...