Jump to content
SAU Community

Recommended Posts

i think anyone who doesnt own a rs four s should mind their own business as half of this post is a discussion about the diff between a s and a rsfour .

heh real nice.

i fail to see how a boost issue MUST be specific to it being a manual. It could be, but surely we who own (or have owned, as in my case) an s2 RS4(V) can at least offer to help.

The boost solenoid is not complicated at all. Its just bleeding off pressure in order to lift the boost pressure by 2psi after 4500rpm. I'm not sure if this is how it works in the manual versions, but this is definitely what the solenoid does in function.

The vacuum lines just plug into different points on your intake, and also the wastegate actuator. The wastegate actuator then just measures the amount of pressure in the vacuum line. It will open the wastegate when pressure reaches 5psi, and will close it when its below that. Bleeding some pressure off as the solenoid does, will cause the wastegate to see LESS pressure, and thus stay closed a bit longer. If you bleed too much pressure off, by bypassing the solenoid and using too wide a hose, the wastegate actuator may never see 5psi and will stay closed, resulting in "unlimited" boost as mentioned in an earlier post. This is bad.

When the wastegate is closed, the boost pressure keeps building up. When its open, it stops the boost pressure from continuing to build up (ie. because the air is now escaping), and the boost pressure may even fall a little (as it will with a stock engine).

A common problem with these cars is that the wastegate sometimes can get either stuck open, or the spring may weaken and it will creep open rather than staying closed right up to 5psi. In both cases, it will not build boost or may build boost slowly or just slower than it should.

Hope this helps.

  • 1 year later...

After a year of searching this problem still not totally fixed, after fuel pump swap, mechanic changing all relevant sensors from our cars R34 to c34 then adding NISMO fuel pressure reg, running on dyno (mixtures are good), fault is much better. Car is detonating occasionally causing the ECU to put the car into the knock limp mode, this limp mode does not bring up an engine check light. Has anyone else had issues like this? I am still trying to find root cause, not just work around yet. Thanks also to those who posted!

  • 8 years later...
  • 1 month later...

Hey guys,

 

stagea - s2 rb25det

 

just done head gasket and timing kit etc

car has high flow turbo, fmic, bleed valve and exhaust and nistuned

Car back up and running fine but NO BOOST at all - as in it drives n/a fine boost gauge comes up to the 0 but not even 1psi of boost...

ideas?

How fast does it go? Is it boosting but the gauge is dead?

If really no boost you have dead turbo, incorrectly plumbed bleed valve, stuck or maladjusted waste gate or (most likely) massive leak.

If you can't find the leak by following the path around to look for a missing clamp etc the best way is to pull the turbo outlet pipe off and make up a plug with a tyre valve in the middle. If it won't hold say 20 psi you should easily be able to tell where the air is escaping.

Thanks for the reply. Should not be a dead turbocharger. It was perfect prior to me doing the head gasket etc.

i removed the wastegate circlip and operated by hand it opens and closes fine.

removed the intake pipe and spun the compressor wheel by hand - spins freely no issues.

ill make a boost leak tester and check for leaks shortly - a big leak would make the car run rough yes?? Runs perfect doesn’t drop idle etc just no spool.

  • 3 years later...
On 23/11/2010 at 11:23 PM, morm said:

After a year of searching this problem still not totally fixed, after fuel pump swap, mechanic changing all relevant sensors from our cars R34 to c34 then adding NISMO fuel pressure reg, running on dyno (mixtures are good), fault is much better. Car is detonating occasionally causing the ECU to put the car into the knock limp mode, this limp mode does not bring up an engine check light. Has anyone else had issues like this? I am still trying to find root cause, not just work around yet. Thanks also to those who posted!

Hey mate, having similar issues to you.. While in this limp mode you were still able to freely rev it up (past 3-4k) as if it wasnt in a "limp home" mode?

The car ran fine, boost was less. I changed injectors with new OEM injectors and car is fine. I had injectors cleaned and flow tested. There was large differences in flow, both at low flow and high flow which I suspect caused detonation and lower boost 'limp' mode. The car is a factory 2000 RS4s. This is my experience and what worked for me (fixed issue).

On 8/7/2023 at 5:29 PM, Turtle tickler said:

Hey mate, having similar issues to you.. While in this limp mode you were still able to freely rev it up (past 3-4k) as if it wasnt in a "limp home" mode?

Do a proper boost leak check man. That's pretty much exactly what happens when a coupler has popped off. Also solid chance it's crusty old ( or new ) coils

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • When you crank your car, and hit it with a timing light, can you see a steady crank timing?
    • Oh, forgot to add, A few months ago I was getting mixture codes and the car was using crap loads of fuel. You could smell the unburned fuel in the exhaust, it was crazy strong. Economy was over 17.5 l/100 and usually around 19. I smoked the engine and found a leaky CCV hose which I replaced and then I replaced my two pre cat O2 sensors, I also replaced the MAF. This fixed my mixture codes and improved my exonomy but I'm still 14 - 15 l/100 when pottering about town so something is still amiss. Throttle response is much better and it has more pep but I'd like to know why it's still so thirsty (and I'm hoping that whatever it is gives me a bit more poke).    
    • Car is on factory injectors/z32 maf/ q45 throttle body/ z32 ecu with nistune 
    • Hello all, currently finishing up a rb25 swap into my s14. Having issues with starting, car has spark (confirmed by pulling a plug and watching it spark), has fuel(confirmed by checking pulse/voltage at injectors all spark plugs are soaked in fuel). Car cranks over and pops into the exhaust with a heavy fuel smell but no attempt to start or run, I have torn the timing cover off and triple confirmed timing, turned the CAS in multiple spots both directions, attempted to start with coolant temp and maf unplugged, checked my fuel lines and made sure they weren’t backwards, checked voltage at cas/injectors/coilpacks, made sure all the grounds in the harness are connected and added a few grounding straps (1 from chassis to block, 1 from chassis to head, and 1 from chassis to igniter chip) I am getting stumped here. As a last ditch effort I made a full grounding harness tonight that’s going to run from the battery and add an extra ground from the battery onto the coil pack harness/igniter chip/ intake manifold/ Wiring specialties harness ground/ and alternator. I’m hoping maybe the grounding harness will fix it here but posting here to see if anyone has any other ideas on what else I can check. My fuel pressure is unknown right gauge will be here tomorrow.  IMG_3206.mov
    • yeah I was shocked when I checked my spare OEM on and as below that's how they come from Nissan. (side interesting note new NEO gearbox and replacement park lack the brass bush on the tips and its just all alloy) unsure about damage to the box currently back at 1110 to be pulled down/inspected and selector fork replaced as he built it previously and given the never before seen failure on his billet forks he is replacing it under warranty. He said he has used always OEM the keyway tab without issue for years so it could be an unlucky coincidence. I did talk to him about the sharp corners and stress concentration too. Re: hard shifts i got 7+ years out of the OEM one and the fork itself failed not the keyway. so could be bad luck as I said or an age thing + heat cycles in box and during fabrication of billet?
×
×
  • Create New...