Jump to content
SAU Community

Recommended Posts

Hey guys,

I think my 32 seems to have a possible air leak somewhere which is making my torque drop just after my turbo fully spools.

Heres some info of what we've done so far:

(RB25 engine) Forward facing plenum has been machined and so has the manifold

Gaskets replaced

Turbo is a GCG Hi Flowed R33 turbo

Greddy cooler has been tested for leaks

Piping has been flared and silicon hoses have been secured and some replaced

Car was also dyno'd with the exhaust taken off from the dump but results didn't change

Here's the dyno graph, sorry its a bit blurry, was in a rush.dynoz.jpg

Mine is the green one.

If you guys have any ideas or need some more information, please shout out :P

Cheers.

Edited by tkdbboy
Link to comment
https://www.sau.com.au/forums/topic/312388-boost-leak-torque-drop-problem/
Share on other sites

AFRs were on a stable 12. The other graph plotted is of another rb25 r32 with an almost identical setup, main difference is that has a gcg r34 neo turbo high flowed and stock plenum setup (im running a greddy forward facing). So its very unlikely its a tuning problem

I really dont understand why you think it is a boost leak??

The boost pressure looks excellent, very constant.

I would class it as a lack of power and appears to be some sort of restriction.

My initial thoughts are blocked exhaust, maybe a blocked cat or something. Have you tried dropping the cat and doing a dyno run?

Harey, read the first post again. Exhaust was dropped at dump already with no change...

Have to agree with most that its not a boost leak. Strong, steady boost plot!

Out of interest exactly what mods do you have? Have a very similar setup so would just like to know but may also help with diagnosis...

Edited by wlspn

Thanks for the replies guys!

Mods are as follows:

gcg hi flow r33 turbo

3 inch exhaust all the way through

splitfire coilpacks

manual mechanical boost controller

forward facing plenum with 100mm throttle body

greddy FMIC

Power FC

Adjustable cam gear set to stock timing

Bosch 040 fuel pump

Although I am running a stock 33 airbox with a Greddy filter but also with stock piping running to the turbo and also no BOV. So Stao could be onto something :)

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Bit of a pity we don't have good images of the back/front of the PCB ~ that said, I found a YT vid of a teardown to replace dicky clock switches, and got enough of a glimpse to realize this PCB is the front-end to a connected to what I'll call PCBA, and as such this is all digital on this PCB..ergo, battery voltage probably doesn't make an appearance here ; that is, I'd expect them to do something on PCBA wrt power conditioning for the adjustment/display/switch PCB.... ....given what's transpired..ie; some permutation of 12vdc on a 5vdc with or without correct polarity...would explain why the zener said "no" and exploded. The transistor Q5 (M33) is likely to be a digital switching transistor...that is, package has builtin bias resistors to ensure it saturates as soon as base threshold voltage is reached (minimal rise/fall time)....and wrt the question 'what else could've fried?' ....well, I know there's an MCU on this board (display, I/O at a guess), and you hope they isolated it from this scenario...I got my crayons out, it looks a bit like this...   ...not a lot to see, or rather, everything you'd like to see disappears down a via to the other side...base drive for the transistor comes from somewhere else, what this transistor is switching is somewhere else...but the zener circuit is exclusive to all this ~ it's providing a set voltage (current limited by the 1K3 resistor R19)...and disappears somewhere else down the via I marked V out ; if the errant voltage 'jumped' the diode in the millisecond before it exploded, whatever that V out via feeds may have seen a spike... ....I'll just imagine that Q5 was switched off at the time, thus no damage should've been done....but whatever that zener feeds has to be checked... HTH
    • I think Fitmit had some, have a look on there (theyre Australian as well)
    • Hah, fair enough! But if you learn with this one you can drive any other OEM manual. No modern luxury features like auto rev-matching or hillstart assist to give you a false sense of confidence. And a heavy car with not that much torque so it stalls easily. 
    • Actually, I'd say all three are the automatic option. Just the different trim levels. The manual would be RSFS, no? 
×
×
  • Create New...