Jump to content
SAU Community

Recommended Posts

I have recently been experiencing idle issues and also hard starting after sitting when hot. Today it blew a stack of steam out the exhaust so I pressurised the radiator and pulled the plugs. Number six was full of green coolant....to the extent that when I turned the motor over to clear, it shot a stream out so hard it made a neat hole in my bonnet underlay.

What confuses me is how a trust metal head gasket could let go?? would it be more likely a crack in the head or block? I did notice some small cracks around the head stud and water jacket holes in the block after getting it bored out. Advan told me this wasn't an issue and the N1 blocks are the only ones that don't do it.

Has anyone had a similar problem with a metal head gasket??

I'll let you know what it was when I remove the head, but that might not be for a couple of weeks.

cheers

Matt

Hard to tell without removing the head as it could be either of the things to stated!

Maybe the gasket was faulty, unlikely but possible.

Then the same for a crack in the gallery/jackets etc.

Interesting one Matt, be sure to post back up about it

I blew a tomei metal head gasket, but it was the center two pots that did it and the gasket cracked both on the same side, i used to be fairly unkind to it when cold though and my motor has been bored another 3mm so the coolant to cylinder gap is much smaller, but more than likely blew it by boosting it before everything had warmed up and expanded.

learn from my experiance! be nice to your motor... :domokun:

Just make sure you get everything machined nice and smooth as with metal gaskets everything needs to be spot on, pay attention around the head bolt holes if your just going to clean up the block as they can tend to pull up if they've been overtorqued.

Edited by kwazza11

get hold of a borescope.

orr... carfully drain the coolant out of the head. by taking the top hose block of the head. then presurise it and see if it still leaks.

cracks in blocks dont go away either, im suprised they actually went ahead with the build after seeing that

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Good luck on the weekend mate
    • Must have been an absolute nightmare to drive when the power steer was out, the rack ratio/wheel size/caster is all set up for power assistance
    • Welcome to SAU, what are you looking at buying?
    • I checked the injectors again (1 and 2, since they’re easiest to access) to make sure they weren’t clogged. Even though the entire fuel system had been cleaned, I wanted to be certain. Everything looked clean, so I reinstalled and connected everything. When I started the car to confirm everything was okay, it immediately revved up high, so I shut it off straight away. I checked to see if I’d missed a vacuum hose or something, but everything was connected. On the second attempt, the car ran without the high idle, but I noticed a distinct “compressed air” sound coming from the engine bay. Tracing the sound, I pushed injector #6 forward slightly and the noise stopped — it turned out it wasn’t seated properly, despite the fuel rail being bolted down. While holding it in place, the car idled steadily without stalling and ran for over 5 minutes. At this point, I pulled all six injectors out just in case I hadn’t seated them correctly or dirt had gotten onto the O-rings. Unfortunately, I discovered that I had damaged 3 out of 6 injectors (the OEM 270cc ones) during installation. So yes, this was my fault. Since only the pintle caps were damaged, I’ve ordered a Fuel Injector Service Kit from NZEFI to refurbish them. In the meantime, I reinstalled my new injectors – the car now idles fine for over 15 minutes without stalling. I have not attempted to drive it so far. It’s not perfect yet, as it hesitates when the throttle is pressed, but it’s a big improvement. Unplugging the IACV with the new injectors idles at around 800rpm, even with the IACV screw tightened fully. But this is probably due to tune.
    • I wanted to try and preserve the front bumper as long as possible, they're not cheap and are made to order in Japan. Taking inspiration from my previous K11 Micra build where I made an undertray for the Impul bumper, I did the same for this BN Sports bumper but a little slimmed down.  This time round I only made a 'skid plate' (if that's the correct wording/term) for just the bumper surface area, the Micra version covered the gap like an undertray. Starting off with a sheet of mild steel approx. 0.9mm thick 4ft x 2ft in size. I traced around the bumper, cut it out and cleaned the edges. Luckily I was able to get two halves from one piece of metal In the video I installed it as is, but I've since then I've removed it to spray and add a rubber edging trim. The rubber trim is suitable for 1-2mm and it's a really nice tight fit. The bolts had to be loosened due to the plates being too tight against the bumper, the trim wouldn't push on I used some stainless M6 flat headed bolts for a flusher finish (rather than hex heads poking down), I believe this style fastener is used for furniture too incase you struggle to source some. The corner's are a little wider, but this may be an advantage incase I get close to bumping it  The front grill got some attention, finally getting round to repairing it. Upon removal one fixing pulled itself out of the plastic frame, one side is M8 that fixes inside of the frame, where as the other side is M5. Not knowing I could get replacements, I cut down an M8 bolt, threaded it inside the frame along with a decent amount of JB Weld.  The mesh was replaced to match the bumper. One hole on the bonnet/hood had to be drilled out to 8mm to accommodate the new stud, once the glue had set it could be refitted. I think the reason the grill was double meshed was to hide the horn/bonnet latch (which makes sense) but I much prefer it matching the bumper Bumper refitted and it's looking much better IMO The Youtube video can be seen here: https://www.youtube.com/watch?v=bVZP35io9MA
×
×
  • Create New...