Jump to content
SAU Community

Official SAU Dyno Day V.2 Review Thread ***PICS*** v.56kdie


Recommended Posts

Well today saw the running of the second official dyno day at Unique Autosports dyno room in Castle Hill.

Though the day started slow with many people enjoying a Saturday sleep in, the carpark began to pack rapidly with a huge assortment of skylines and other high performance cars.

Congratulations must go to the individual class winners who were up against some stiff competition.

Results are listed below:

Award winners

Top RB20DET standard turbo - Silver GTS-T (R32 GTS-T) 150.6 Kw

Runnerup RB20DET standard turbo - Kinks (R31 w/ RB20DET) 144.5 Kw

Note: There were no modified turbo RB20DET's in attendance so a runnerup category for standard turbo was put in its place.

Top RB25DET standard turbo - R33vit (R33 GTS-T) 197.6 Kw

Top RB25DET modified turbo - B-Man (R33 GTS-T) 327.9 Kw

Top RB26DETT/RB30 standard turbos - Dave (R32 GTR) 249.5 Kw

Top RB26DETT/RB30 modified turbos - Antonio (RB30 Powered R33 GTS-T) 319.5 Kw

Zoom Magazine Encouragement award - Wilch (R33 GTS-T Series 2)

Overall competitor summary:

R33 GTS-T

B-Man - 327.9 Kw

Antonio - 319.6 Kw

Jimbo - 215.1 Kw

Sparki_D - 215 Kw

R33vit - 197.6 Kw

Goldrays - 181.6 Kw

Scott - 180.2 Kw

Ash - 173.0 Kw

Wilch - 166.9 Kw

Neil - 159.8 Kw

Eden - 158.3 Kw

R32 GTS-T

Silver GTS-T - 150.6 Kw

Cereal_Killer - 137.8 Kw

GTR

CNG - 301.3 Kw

Dave - 283 Kw

GTR032 - 188.6 Kw

Misc Entries

Grant - Soarer - 263.2 Kw

Andrew - Supra Twin Turbo - 246.2 Kw

Stewart - E46 M3 - 183.9 Kw

Haroon - S13 Silvia - 158.6 Kw

Kel - 350z - 156.9 Kw

Kinks - R31/RB20DET - 144.5 Kw

Sean - Supra Non-Turbo - 111.4 Kw

Carlo - Supercharged MR2 - 87.2 Kw

Chris - Datsun 240z - 67 Kw

Duncan - Datsun 200B - 49.7 Kw

Thankyou to all of you who attended today for making it a truely great day for all!

dsc01335.jpg

dsc01330.jpg

dsc01352.jpg

dsc01349.jpg

dsc01353.jpg

dsc01371.jpg

dsc01378.jpg

  • Replies 74
  • Created
  • Last Reply

Top Posters In This Topic

good day

did 321 GO have a turn?

and whos posting up photos???????????????????????????????????????????

sure did. Andrew made 178rwkw if memory serves me correctly.

I'm really disappointed with my dismal dyno effort. I have no idea why it was so low. I made 131.7rwkw previous with just a 3" dump / front pipe. Now with a full 3" including high flow cat, front mount and pod filter I managed a shocking 137.8. Very confused. :(

congrats to BMan for the highest figure of the day.

Yep Andrew's 321GO RB20 R32 GTS-T made 178rwkw with E Boost set at 15psi standard RB25 turbo, FMIC and full 3 inch exh. Also Dave's GTR who won RB26 stock turbo went back on dyno last and sorted out boost controller and made 280 somethingrwkw. Yes it was a big day and thanks to SAU gang for the biggest ever Dyno Day we have had. Thanks Uncle Nick and Carlo. Lots of good pics including that immaculate purple GTR.

PS. I had my third V drink in my life. Hope I can sleep tonight. I think I might be dreamin Skylines.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • This is where I share pain with you, @Duncan. The move to change so many cooling system pieces to plastic is a killer! Plastic end tanks and a few plastic hose flanges on my car's fail after so little time.  Curious about the need for a bigger rad, is that just for long sessions in the summer or because the car generally needs more cooling?
    • So, that is it! It is a pretty expensive process with the ATF costing 50-100 per 5 litres, and a mechanic will probably charge plenty because they don't want to do it. Still, considering how dirty my fluid was at 120,000klm I think it would be worth doing more like every 80,000 to keep the trans happy, they are very expensive to replace. The job is not that hard if you have the specialist tools so you can save a bit of money and do it yourself!
    • OK, onto filling. So I don't really have any pics, but will describe the process as best I can. The USDM workshop manual also covers it from TM-285 onwards. First, make sure the drain plug (17mm) is snug. Not too tight yet because it is coming off again. Note it does have a copper washer that you could replace or anneal (heat up with a blow torch) to seal nicely. Remove the fill plug, which has an inhex (I think it was 6mm but didn't check). Then, screw in the fill fitting, making sure it has a suitable o-ring (mine came without but I think it is meant to be supplied). It is important that you only screw it in hand tight. I didn't get a good pic of it, but the fill plug leads to a tube about 70mm long inside the transmission. This sets the factory level for fluid in the trans (above the join line for the pan!) and will take about 3l to fill. You then need to connect your fluid pump to the fitting via a hose, and pump in whatever amount of fluid you removed (maybe 3 litres, in my case 7 litres). If you put in more than 3l, it will spill out when you remove the fitting, so do quickly and with a drain pan underneath. Once you have pumped in the required amount of clean ATF, you start the engine and run it for 3 minutes to let the fluid circulate. Don't run it longer and if possible check the fluid temp is under 40oC (Ecutek shows Auto Trans Fluid temp now, or you could use an infrared temp gun on the bottom of the pan). The manual stresses the bit about fluid temperature because it expands when hot an might result in an underfil. So from here, the factory manual says to do the "spill and fill" again, and I did. That is, put an oil pan under the drain plug and undo it with a 17mm spanner, then watch your expensive fluid fall back out again, you should get about 3 litres.  Then, put the drain plug back in, pump 3 litres back in through the fill plug with the fitting and pump, disconnect the fill fitting and replace the fill plug, start the car and run for another 3 minutes (making sure the temp is still under 40oC). The manual then asks for a 3rd "spill and fill" just like above. I also did that and so had put 13l in by now.  This time they want you to keep the engine running and run the transmission through R and D (I hope the wheels are still off the ground!) for a while, and allow the trans temp to get to 40oC, then engine off. Finally, back under the car and undo the fill plug to let the overfill drain out; it will stop running when fluid is at the top of the levelling tube. According to the factory, that is job done! Post that, I reconnected the fill fitting and pumped in an extra 0.5l. AMS says 1.5l overfill is safe, but I started with less to see how it goes, I will add another 1.0 litres later if I'm still not happy with the hot shifts.
    • OK, so regardless of whether you did Step 1 - Spill Step 2 - Trans pan removal Step 3 - TCM removal we are on to the clean and refill. First, have a good look at the oil pan. While you might see dirty oil and some carbony build up (I did), what you don't want to see is any metal particles on the magnets, or sparkles in the oil (thankfully not). Give it all a good clean, particularly the magnets, and put the new gasket on if you have one (or, just cross your fingers) Replacement of the Valve body (if you removed it) is the "reverse of assembly". Thread the electrical socket back up through the trans case, hold the valve body up and put in the bolts you removed, with the correct lengths in the correct locations Torque for the bolts in 8Nm only so I hope you have that torque wrench handy (it feels really loose). Plug the output speed sensor back in and clip the wiring into the 2 clips, replace the spring clip on the TCM socket and plug it back into the car loom. For the pan, the workshop manual states the following order: Again, the torque is 8Nm only.
    • One other thing to mention from my car before we reassemble and refill. Per that earlier diagram,   There should be 2x B length (40mm) and 6x C length (54mm). So I had incorrectly removed one extra bolt, which I assume was 40mm, but even so I have 4x B and 5x C.  Either, the factory made an assembly error (very unlikely), or someone had been in there before me. I vote for the latter because the TCM part number doesn't match my build date, I suspect the TCM was changed under warranty. This indeed led to much unbolting, rebolting, checking, measuring and swearing under the car.... In the end I left out 1x B bolt and put in a 54mm M6 bolt I already had to make sure it was all correct
×
×
  • Create New...