Jump to content
SAU Community

Recommended Posts

  • Replies 1.8k
  • Created
  • Last Reply

Top Posters In This Topic

Top Posters In This Topic

Posted Images

Dezz - which way do you have it plumbed in.. from the sounds of it you've put it in line with the solenoid.. once you hit 4,5000 it shouldn't make any difference if you've got the solenoid T-piece pulled out..

Take a photo of how you've got it plugged in and we'll take a looky.

I'll get a photo of it tomorrow...

its coming off the stock nipple, because my fmic uses the stock piping...so its under the airbox...

stock solenoid has no hoses going into it, and is disconnected at the plug

Hey,

Has anyone heard from mark recently because the last thing i want to do is buy from this jrd guy no offence but i dont beleave in copying then trying to sell your product on a thread that was directed at marks product...

if anyone hear's from mark please post up how they got in contact..

if not i will probly start saving for EBC.

Hey dezz, did you sort out that issue? Very curious to see what's causing it.

I just installed mine tonight, on lowest possible setting for testing. It ran 7psi and slowly creeped up to 8psi by about 5000rpm. Although i dont think it was due to the factory dual stage. I'm thinking maybe the turbotech wasnt meant to hold such low boost.

When i get a chance tomorrow, i'll set it to 10psi and see how it holds.

HI everybody,

i ended up goin on ebay and gettin a turbotech BC. im installing it soon so i took a look under the bonet.

i tryed looking for a 32 install but didnt find. after looking at 30 diff pages.

I already have a hsk bleed valve (came with the car)and would like to replace it.. i numbered the pipes i think are used please help. number 1 is the bleed valve i think.. nice peice of plastc holding my boost.. i feel so safe..

enginbay.jpg

Thank you.

Edited by Fugi

sorry Fugi, not sure about r32 setup.

i set mine to 9psi today, and seemed to hold steady, although daytime traffic etc, and only really tested it in 2nd. so far so good.

i used the standard hoses, and just replaced the T piece with the turbotech, blocked the line that was going to the top of the solenoid, and remove bottom line.

can post pics if anyone needs them (R33).

sorry Fugi, not sure about r32 setup.

i set mine to 9psi today, and seemed to hold steady, although daytime traffic etc, and only really tested it in 2nd. so far so good.

i used the standard hoses, and just replaced the T piece with the turbotech, blocked the line that was going to the top of the solenoid, and remove bottom line.

can post pics if anyone needs them (R33).

Thats ok, i just wanted to see if someone could help me out so i didnt have to use trial and error. i will post up my findings cauz no one seems to have installed it on a r32 and taken picks. i will post soon.

Thanks

hey, on my r33 i had mine wound out so it would only make 6psi or so where the actuator opens. driving around tonight when i came from a bit of acceleration to a stop quickly she'd stall...im guessing this may be the cause as this is the only change ive done other than the new intake...

hey, on my r33 i had mine wound out so it would only make 6psi or so where the actuator opens. driving around tonight when i came from a bit of acceleration to a stop quickly she'd stall...im guessing this may be the cause as this is the only change ive done other than the new intake...

i'd be looking at the new intake. more likely to be that rather than the boost controller, since the boost controller isnt doing anything when your off boost.

new intake as in what? new pod? new intake pipe? new plenum? has your afm been messed around with?

are these still available for SAU members at $22 delivered???

I've tried contacting mark through ebay,email, and through pm on this forum but still no reply, anyone else know how to contact him?

Dont wanna sound cheap but why pay $37.40 on ebay if i can get it for $22...

Hey all as per my post i think like 20 pages ago i managed to get mine working and it has been going strong alot better than my previous turbosmart pos. Anyways i have upped the boost to around what i thought was 11psi. After doing some high load runs i found that it was getting up to a max of 11.6psi at 4500rpm and then worked its way down gradually till 6800rpm when it was down to about 9.8psi. I have checked the lines and they are as straight and short as i can make them. Other than maybe trying to shield the BC from the engine bay heat do people have any other ideas on what i can do.

Summary is below

4500rpm - 11.6psi

5100rpm - 11.1psi

5700rpm - 10.7psi

6300rpm - 10.0psi

6900rpm - 9.8psi

PS i know it's a cheap boost controller and can't expect the world but 1.8psi is a fair drop.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • I had 3 counts over the last couple of weeks once where i got stranded at a jdm paint yard booking in some work. 2nd time was moving the car into the drive way for the inspection and the 3rd was during the inspection for the co2 leak test. Fix: 1st, car off for a hour and half disconnected battery 10mins 4th try car started 2nd, 5th try started 3rd, countless time starting disconnected battery dude was under the hood listening to the starting sequence fuel pump ect.   
    • This. As for your options - I suggest remote mounting the Nissan sensor further away on a length of steel tube. That tube to have a loop in it to handle vibration, etc etc. You will need to either put a tee and a bleed fitting near the sensor, or crack the fitting at the sensor to bleed it full of oil when you first set it up, otherwise you won't get the line filled. But this is a small problem. Just needs enough access to get it done.
    • The time is always correct. Only the date is wrong. It currently thinks it is January 19. Tomorrow it will say it is January 20. The date and time are ( should be ! ) retrieved from the GPS navigation system.
    • Buy yourself a set of easy outs. See if they will get a good bite in and unthread it.   Very very lucky the whole sender didn't let go while on the track and cost you a motor!
    • Well GTSBoy, prepare yourself further. I did a track day with 1/2 a day prep on Friday, inpromptu. The good news is that I got home, and didn't drive the car into a wall. Everything seemed mostly okay. The car was even a little faster than it was last time. I also got to get some good datalog data too. I also noticed a tiny bit of knock which was (luckily?) recorded. All I know is the knock sensors got recalibrated.... and are notorious for false knock. So I don't know if they are too sensitive, not sensitive enough... or some other third option. But I reduced timing anyway. It wasn't every pull through the session either. Think along the lines of -1 degree of timing for say, three instances while at the top of 4th in a 20 minute all-hot-lap session. Unfortunately at the end of session 2... I noticed a little oil. I borrowed some jack stands and a jack and took a look under there, but as is often the case, messing around with it kinda half cleaned it up, it was not conclusive where it was coming from. I decided to give it another go and see how it was. The amount of oil was maybe one/two small drops. I did another 20 minute session and car went well, and I was just starting to get into it and not be terrified of driving on track. I pulled over and checked in the pits and saw this: This is where I called it, packed up and went home as I live ~20 min from the track with a VERY VERY CLOSE EYE on Oil Pressure on the way home. The volume wasn't much but you never know. I checked it today when I had my own space/tools/time to find out what was going on, wanted to clean it up, run the car and see if any of the fittings from around the oil filter were causing it. I have like.. 5 fittings there, so I suspected one was (hopefully?) the culprit. It became immediately apparent as soon as I looked around more closely. 795d266d-a034-4b8c-89c9-d83860f5d00a.mp4       This is the R34 GTT oil sender connected via an adapter to an oil cooler block I have installed which runs AN lines to my cooler (and back). There's also an oil temp sensor on top.  Just after that video, I attempted to unthread the sensor to see if it's loose/worn and it disintegrated in my hand. So yes. I am glad I noticed that oil because it would appear that complete and utter catastrophic engine failure was about 1 second of engine runtime away. I did try to drill the fitting out, and only succeeded in drilling the middle hole much larger and now there's a... smooth hole in there with what looks like a damn sleeve still incredibly tight in there. Not really sure how to proceed from here. My options: 1) Find someone who can remove the stuck fitting, and use a steel adapter so it won't fatigue? (Female BSPT for the R34 sender to 1/8NPT male - HARD to find). IF it isn't possible to remove - Buy a new block ($320) and have someone tap a new 1/8NPT in the top of it ($????) and hope the steel adapter works better. 2) Buy a new block and give up on the OEM pressure sender for the dash entirely, and use the supplied 1/8 NPT for the oil temp sender. Having the oil pressure read 0 in the dash with the warning lamp will give me a lot of anxiety driving around. I do have the actual GM sensor/sender working, but it needs OBD2 as a gauge. If I'm datalogging I don't actually have a readout of what the gauge is currently displaying. 3) Other? Find a new location for the OEM sender? Though I don't know of anywhere that will work. I also don't know if a steel adapter is actually functionally smart here. It's clearly leveraged itself through vibration of the motor and snapped in half. This doesn't seem like a setup a smart person would replicate given the weight of the OEM sender. Still pretty happy being lucky for once and seeing this at the absolute last moment before bye bye motor in a big way, even if an adapter is apparently 6 weeks+ delivery and I have no way to free the current stuck/potentially destroyed threads in the current oil block.
×
×
  • Create New...