Jump to content
SAU Community

Recommended Posts

  • Replies 316
  • Created
  • Last Reply

Top Posters In This Topic

Top Posters In This Topic

Posted Images

Basically the new gen core is rated to flow more, the older core is rated to flow less.

If it's possible to use the new gen core with the internal gate housing i'm not sure, if it works well is another thing, you may experience surge with a small exhaust a/r?

Bullant.

You mentioned the GCG may bring back the 500 hp turbo, but woulld have to address the size of the wastegate in order to make it commercially viable.

Did they offer to enlarge your wastegate?

I once spoke to them about highflowing my turbo and I asked if they could make it bigger, and they said no problems.

Just a thought.

Any further reflections on how the turbo performs?

Have you done the 2nd gear from walking pace test? When does she begin to boost?

BASS OUT (Still searching for a VG30DET Exhaust housing)

Sorry i dont know about a 500hp hi flow.

2nd gear boost starts at about 2200rpm and makes a lot of wheel spin at about 3700rpm.

3rd gear boost starts at about 2200rpm and makes full boost (19psi) at around 3800rpm.

It ramps up very strong and really fast in between these revs.

Sorry i dont know about a 500hp hi flow.

2nd gear boost starts at about 2200rpm and makes a lot of wheel spin at about 3700rpm.

3rd gear boost starts at about 2200rpm and makes full boost (19psi) at around 3800rpm.

It ramps up very strong and really fast in between these revs.

I did the same thing in my car as have a standard turbo for a comparison (mods are in sig). I did it by just idling along in the selected gear than just held it flat.

2nd gear boost starts at 1000rpm and full boost 11psi at 3000rpm.

3rd gear was exacly the same.

So to me it looks as though boost comes on 1000rpm later but spools just as quick or quicker than stock. You have got to be happy with that very impressive. I would like to see people do the same tests with 2535 standard gcg highflow ect for interests sake.

:D

Bullant.

 

You mentioned the GCG may bring back the 500 hp turbo, but woulld have to address the size of the wastegate in order to make it commercially viable.

 

 Did they offer to enlarge your wastegate?

The issue with the old GCG 500hp highflow wasn't boost creep (where boost cannot be kept down, creeps up as revs increase) the issue was with surge.

A larger exhaust a/r was needed to help shift the full spool a little higher in the rev range where the motor can consume the air better.

I'm unsure of the differences between the 500hp and 450hp highflows they offered, I assume it was the compressor size.

It looks as if the GCG Highflow on the rb25 would be very similiar to the XR6 Turbo on the Rb30. Spool wise. :D

I did it in mine today. Stock Rb20DET Turbo running stock boost. :D

Boost and surge under 2000rpm, as soon as 2000rpm hits it kicks and breaks in to a wheel spin at this time it looks like its wheelspinning around 2300rpm or so. :)

Just a pitty the power drops off rapidly after 5000rpm and peak power is made around 4400rpm. lol

Cubes yes , the GT30 housings will fit early and late cartridges as will any housing machined (profiled) to suit .

Garrett often sells cartridges without exhaust housings so the end user can select one of several to suit his/her application . If you look in the old Garrett catalogue PDF the "GT3071R" (700177-23 CHRA No) is sold as a cartridge without compressor or exhaust housings but there are three variations of both turbine and compressor housings available .

The integral gate HKS housings are the go and while expensive not as much as an aftermarket cast manifold and waste gate . GCG can get HKS housings (as I suppose HPIAB could) and if enough people were interested they could possibly market these with late "GT30R" turbochargers that will bolt up and take advantage of all the available technology .

Cheers A .

Got any pics?

No sorry, I only had the VG30 in my possession for about 15 minuites. GCG got it and opperated on it almost immediately...It was complete with dump, 02 sensor and in good condition actually.

Hey on another note, I went back to C&V for a touch up on the tune cause along with the massive power the car is making, some knock was occasionally observed on the Power FC. It appears that the R34 fuel pump is maxed out and A/F is leaning out at high speed (around 180kph). Next week a Bosch 044 and swirl pot is being fitted to keep the A/F line straight on the graph. Con recons the turbo is so efficient that with more fuel he can make a lot more power safely. After he played with the high end fuelling and took out a little timing it actually made 273.9kw@tw. 3kw more than before. So be prepared to think about fuelling cause the GCG Hiflow with the VG30 turbine housing sees the end of the GTR fuel pump upgrade. I'll post up the dyno sheet when i hook up the scanner.

Ian

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...