Jump to content
SAU Community

Recommended Posts

i think anyone who doesnt own a rs four s should mind their own business as half of this post is a discussion about the diff between a s and a rsfour .

heh real nice.

i fail to see how a boost issue MUST be specific to it being a manual. It could be, but surely we who own (or have owned, as in my case) an s2 RS4(V) can at least offer to help.

The boost solenoid is not complicated at all. Its just bleeding off pressure in order to lift the boost pressure by 2psi after 4500rpm. I'm not sure if this is how it works in the manual versions, but this is definitely what the solenoid does in function.

The vacuum lines just plug into different points on your intake, and also the wastegate actuator. The wastegate actuator then just measures the amount of pressure in the vacuum line. It will open the wastegate when pressure reaches 5psi, and will close it when its below that. Bleeding some pressure off as the solenoid does, will cause the wastegate to see LESS pressure, and thus stay closed a bit longer. If you bleed too much pressure off, by bypassing the solenoid and using too wide a hose, the wastegate actuator may never see 5psi and will stay closed, resulting in "unlimited" boost as mentioned in an earlier post. This is bad.

When the wastegate is closed, the boost pressure keeps building up. When its open, it stops the boost pressure from continuing to build up (ie. because the air is now escaping), and the boost pressure may even fall a little (as it will with a stock engine).

A common problem with these cars is that the wastegate sometimes can get either stuck open, or the spring may weaken and it will creep open rather than staying closed right up to 5psi. In both cases, it will not build boost or may build boost slowly or just slower than it should.

Hope this helps.

  • 1 year later...

After a year of searching this problem still not totally fixed, after fuel pump swap, mechanic changing all relevant sensors from our cars R34 to c34 then adding NISMO fuel pressure reg, running on dyno (mixtures are good), fault is much better. Car is detonating occasionally causing the ECU to put the car into the knock limp mode, this limp mode does not bring up an engine check light. Has anyone else had issues like this? I am still trying to find root cause, not just work around yet. Thanks also to those who posted!

  • 8 years later...
  • 1 month later...

Hey guys,

 

stagea - s2 rb25det

 

just done head gasket and timing kit etc

car has high flow turbo, fmic, bleed valve and exhaust and nistuned

Car back up and running fine but NO BOOST at all - as in it drives n/a fine boost gauge comes up to the 0 but not even 1psi of boost...

ideas?

How fast does it go? Is it boosting but the gauge is dead?

If really no boost you have dead turbo, incorrectly plumbed bleed valve, stuck or maladjusted waste gate or (most likely) massive leak.

If you can't find the leak by following the path around to look for a missing clamp etc the best way is to pull the turbo outlet pipe off and make up a plug with a tyre valve in the middle. If it won't hold say 20 psi you should easily be able to tell where the air is escaping.

Thanks for the reply. Should not be a dead turbocharger. It was perfect prior to me doing the head gasket etc.

i removed the wastegate circlip and operated by hand it opens and closes fine.

removed the intake pipe and spun the compressor wheel by hand - spins freely no issues.

ill make a boost leak tester and check for leaks shortly - a big leak would make the car run rough yes?? Runs perfect doesn’t drop idle etc just no spool.

  • 3 years later...
On 23/11/2010 at 11:23 PM, morm said:

After a year of searching this problem still not totally fixed, after fuel pump swap, mechanic changing all relevant sensors from our cars R34 to c34 then adding NISMO fuel pressure reg, running on dyno (mixtures are good), fault is much better. Car is detonating occasionally causing the ECU to put the car into the knock limp mode, this limp mode does not bring up an engine check light. Has anyone else had issues like this? I am still trying to find root cause, not just work around yet. Thanks also to those who posted!

Hey mate, having similar issues to you.. While in this limp mode you were still able to freely rev it up (past 3-4k) as if it wasnt in a "limp home" mode?

The car ran fine, boost was less. I changed injectors with new OEM injectors and car is fine. I had injectors cleaned and flow tested. There was large differences in flow, both at low flow and high flow which I suspect caused detonation and lower boost 'limp' mode. The car is a factory 2000 RS4s. This is my experience and what worked for me (fixed issue).

On 8/7/2023 at 5:29 PM, Turtle tickler said:

Hey mate, having similar issues to you.. While in this limp mode you were still able to freely rev it up (past 3-4k) as if it wasnt in a "limp home" mode?

Do a proper boost leak check man. That's pretty much exactly what happens when a coupler has popped off. Also solid chance it's crusty old ( or new ) coils

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Apologies for the long post, but needed somewhere to lay out the entire timeline of events and actions taken:   I've got an 89 GTR with a R34 RB in it. It's been running great all year, driven probably 500KM in the last month. It's not my daily driver, just a weekend fun car.    Build info: R34 RB26 - HKS 2.7 stroker kit, HKS adjustable cam gears, HKS turbo upgrades, Trust intercooler, R34 factory DENSO 440cc injectors, JUN chipped/tuned R32 ECU. All of this work was performed in Japan back in 2019.    Thursday 10/2/25 - It's a nice day and decided I'll drive it to work, I start it up in the garage and I notice it took a few extra cranks and sounded a bit funny. I figure maybe it was just because it was a pretty chilly morning. I pull it out into the driveway to warm up a bit before leaving. As I leave the driveway, it feels very off and sounds like a misfire. I pull it back in the garage to deal with after work and take the daily to work. I was able to diagnose it as a cylinder 5 misfire with the old spark plug test (unplugging each plug until a sound change with the engine running). I take off the whole ignition system, ignitor, plugs, spark. *Important note, it is still on the R32 ignition system with the separate ignitor system. I test each system with a multi-meter and nothing presents as a smoking gun. I put it all back together and it starts up no issue. I go ahead and order the PRP R35 ignition conversion kit. It should arrive today (10/13/25)   Friday 10/3/25 - Another nice day, car starts up great and drives great all day. Very pleased that everything seems to be OK   Sunday 10/5/25 - Decided I'll take it to play some golf, load up and drive to the course about 25 minutes away. Drives wonderful the whole way there, I pull in the parking lot and the engine completely comes to a stop. I do not recall if it sputtered at all, but just remember all of the sudden the engine was off. I roll it into a parking spot, try to crank it back on and nothing.  It'll crank and crank and not even try to start. End up getting it towed back to my house and push it up into the garage.    Items I have checked: Fuel in the tank Fuel Pump relay Fuel pump fuse  Spark Plugs & gap Coil packs Ignitor    I know the cylinders are getting fuel as the plugs smell like fuel after a start attempt. I tried spraying starter fluid into the manifold and cranking and not even a sputter.    I decided to do the live CAS test (removing the the CAS, ignition on and spinning the CAS stalk to see if the injectors pulse and spark is active). All of the injectors were pulsing and I have spark at the plug. The half-moon end of the CAS did seem very loose, I'm not sure how much play is supposed to be there, but it was more than I expected. There was no in/out play of the shaft, just the tip end that is pinned on had quite a bit of play.    CAS Play video   When I put the CAS back in, I stupidly did not re-time the engine. I know I need to do that tonight, however, I do not think it will start given it seemingly was not the issue. My plan is to do the PRP R35 coil kit and retime the engine at the same time.    I plan on ordering the Haltech Nexus Plug-in ECU once they are available again, but ideally would like to get this sorted before firing the parts cannon at it and potentially adding more variables.    Anything glaring that I am missing here, I'm a bit at a loss?          
    • Get it on a dyno. Get something logging Consult. Run it up and find out what is causing it.
    • Looking for a plenum for rb25 de+t neo  Not looking to push much power maybe 300kw at the wheels, is there much difference in flow for Freddy “Greddy style” compared to original Greddy or options like Proflow or Otaku garage?    I won’t be porting the de Neo head for now as I think it’ll be fine 280-300rwkw but appreciate the help and any experiences anyone has between them and any advice. Thanks  Looking at this plenum for now below 
    • engine wise almost no mods: stock ecu Greddy front mount intercooler Greddy forward facing intake w R33 TB stock fuel system, stock injectors, rail etc. Kakimoto racing hyper 3 inch exhaust system Apexi intake filter New NGK –R BCPRES (.8 gap) plugs  
    • Nice one @Pac - looks like a fair few 1600's there! 
×
×
  • Create New...