Jump to content
SAU Community

Recommended Posts

Hey guys,

I think my 32 seems to have a possible air leak somewhere which is making my torque drop just after my turbo fully spools.

Heres some info of what we've done so far:

(RB25 engine) Forward facing plenum has been machined and so has the manifold

Gaskets replaced

Turbo is a GCG Hi Flowed R33 turbo

Greddy cooler has been tested for leaks

Piping has been flared and silicon hoses have been secured and some replaced

Car was also dyno'd with the exhaust taken off from the dump but results didn't change

Here's the dyno graph, sorry its a bit blurry, was in a rush.dynoz.jpg

Mine is the green one.

If you guys have any ideas or need some more information, please shout out :P

Cheers.

Edited by tkdbboy
Link to comment
https://www.sau.com.au/forums/topic/312388-boost-leak-torque-drop-problem/
Share on other sites

AFRs were on a stable 12. The other graph plotted is of another rb25 r32 with an almost identical setup, main difference is that has a gcg r34 neo turbo high flowed and stock plenum setup (im running a greddy forward facing). So its very unlikely its a tuning problem

I really dont understand why you think it is a boost leak??

The boost pressure looks excellent, very constant.

I would class it as a lack of power and appears to be some sort of restriction.

My initial thoughts are blocked exhaust, maybe a blocked cat or something. Have you tried dropping the cat and doing a dyno run?

Harey, read the first post again. Exhaust was dropped at dump already with no change...

Have to agree with most that its not a boost leak. Strong, steady boost plot!

Out of interest exactly what mods do you have? Have a very similar setup so would just like to know but may also help with diagnosis...

Edited by wlspn

Thanks for the replies guys!

Mods are as follows:

gcg hi flow r33 turbo

3 inch exhaust all the way through

splitfire coilpacks

manual mechanical boost controller

forward facing plenum with 100mm throttle body

greddy FMIC

Power FC

Adjustable cam gear set to stock timing

Bosch 040 fuel pump

Although I am running a stock 33 airbox with a Greddy filter but also with stock piping running to the turbo and also no BOV. So Stao could be onto something :)

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • I know why it happened and I’m embarrassed to say but I was testing the polarity of one of the led bulb to see which side was positive with a 12v battery and that’s when it decided to fry hoping I didn’t damage anything else
    • I came here to note that is a zener diode too base on the info there. Based on that, I'd also be suspicious that replacing it, and it's likely to do the same. A lot of use cases will see it used as either voltage protection, or to create a cheap but relatively stable fixed voltage supply. That would mean it has seen more voltage than it should, and has gone into voltage melt down. If there is something else in the circuit dumping out higher than it should voltages, that needs to be found too. It's quite likely they're trying to use the Zener to limit the voltage that is hitting through to the transistor beside it, so what ever goes to the zener is likely a signal, and they're using the transistor in that circuit to amplify it. Especially as it seems they've also got a capacitor across the zener. Looks like there is meant to be something "noisy" to that zener, and what ever it was, had a melt down. Looking at that picture, it also looks like there's some solder joints that really need redoing, and it might be worth having the whole board properly inspected.  Unfortunately, without being able to stick a multimeter on it, and start tracing it all out, I'm pretty much at a loss now to help. I don't even believe I have a climate control board from an R33 around here to pull apart and see if any of the circuit appears similar to give some ideas.
    • Nah - but you won't find anything on dismantling the seats in any such thing anyway.
    • Could be. Could also be that they sit around broken more. To be fair, you almost never see one driving around. I see more R chassis GTRs than the Renault ones.
    • Yeah. Nah. This is why I said My bold for my double emphasis. We're not talking about cars tuned to the edge of det here. We're talking about normal cars. Flame propagation speed and the amount of energy required to ignite the fuel are not significant factors when running at 1500-4000 rpm, and medium to light loads, like nearly every car on the road (except twin cab utes which are driven at 6k and 100% load all the time). There is no shortage of ignition energy available in any petrol engine. If there was, we'd all be in deep shit. The calorific value, on a volume basis, is significantly different, between 98 and 91, and that turns up immediately in consumption numbers. You can see the signal easily if you control for the other variables well enough, and/or collect enough stats. As to not seeing any benefit - we had a couple of EF and EL Falcons in the company fleet back in the late 90s and early 2000s. The EEC IV ECU in those things was particularly good at adding in timing as soon as knock headroom improved, which typically came from putting in some 95 or 98. The responsiveness and power improved noticeably, and the fuel consumption dropped considerably, just from going to 95. Less delta from there to 98 - almost not noticeable, compared to the big differences seen between 91 and 95. Way back in the day, when supermarkets first started selling fuel from their own stations, I did thousands of km in FNQ in a small Toyota. I can't remember if it was a Starlet or an early Yaris. Anyway - the supermarket servos were bringing in cheap fuel from Indonesia, and the other servos were still using locally refined gear. The fuel consumption was typically at least 5%, often as much as 8% worse on the Indo shit, presumably because they had a lot more oxygenated component in the brew, and were probably barely meeting the octane spec. Around the same time or maybe a bit later (like 25 years ago), I could tell the difference between Shell 98 and BP 98, and typically preferred to only use Shell then because the Skyline ran so much better on it. Years later I found the realtionship between them had swapped, as a consequence of yet more refinery closures. So I've only used BP 98 since. Although, I must say that I could not fault the odd tank of United 98 that I've run. It's probably the same stuff. It is also very important to remember that these findings are often dependent on region. With most of the refineries in Oz now dead, there's less variability in local stuff, and he majority of our fuels are not even refined here any more anyway. It probably depends more on which SE Asian refinery is currently cheapest to operate.
×
×
  • Create New...