Jump to content
SAU Community

Recommended Posts

  • Replies 61
  • Created
  • Last Reply

Top Posters In This Topic

Yah :down:

Hah!

Good on ya man!

wanted to come but couldnt get my farking wheels off :/

will be there next week if its on with new shoes :D

What wheels you get?

good turn out boys...great night...and jamie nice pics...thanks for taking them again...

No worries man!

Great night, nice turn-out, plenty of fun (with some interesting events) and sweet photos jamie :)

Cool thanks Nath!

How was the cruise?

Some nice skylines at the car wash .

Happened to notice a guy taking shots of my car ,I drove in with the black s14a .

I'm guessing it was Jamie , ? Any pics bro

Ah man!

You had the black S14 with black wheels and red lip around it?

If so, it looked bad ass!

I wanted to take a few pics and tried to but you went a bit far off and could not get a good pic.

Next time :(

Guest
This topic is now closed to further replies.



  • Similar Content

  • Latest Posts

    • The final part arrived today to un-clampify and simplify the intake Who would have though a 1/2" hose stainless bulkhead fitting designed for below waterline bilge pumps would be what I needed Test fit on a 3" offcut I had laying around to see if it would work, and it worked a treat All going well the intake will be on its "final version" tomorrow 
    • Good luck on the weekend mate
    • Must have been an absolute nightmare to drive when the power steer was out, the rack ratio/wheel size/caster is all set up for power assistance
    • Welcome to SAU, what are you looking at buying?
    • I checked the injectors again (1 and 2, since they’re easiest to access) to make sure they weren’t clogged. Even though the entire fuel system had been cleaned, I wanted to be certain. Everything looked clean, so I reinstalled and connected everything. When I started the car to confirm everything was okay, it immediately revved up high, so I shut it off straight away. I checked to see if I’d missed a vacuum hose or something, but everything was connected. On the second attempt, the car ran without the high idle, but I noticed a distinct “compressed air” sound coming from the engine bay. Tracing the sound, I pushed injector #6 forward slightly and the noise stopped — it turned out it wasn’t seated properly, despite the fuel rail being bolted down. While holding it in place, the car idled steadily without stalling and ran for over 5 minutes. At this point, I pulled all six injectors out just in case I hadn’t seated them correctly or dirt had gotten onto the O-rings. Unfortunately, I discovered that I had damaged 3 out of 6 injectors (the OEM 270cc ones) during installation. So yes, this was my fault. Since only the pintle caps were damaged, I’ve ordered a Fuel Injector Service Kit from NZEFI to refurbish them. In the meantime, I reinstalled my new injectors – the car now idles fine for over 15 minutes without stalling. I have not attempted to drive it so far. It’s not perfect yet, as it hesitates when the throttle is pressed, but it’s a big improvement. Unplugging the IACV with the new injectors idles at around 800rpm, even with the IACV screw tightened fully. But this is probably due to tune.
×
×
  • Create New...