Jump to content
SAU Community

Recommended Posts

  • 2 weeks later...

Amazing results, credit to you and your research.

If you don't mind me asking, What is your daily job? Do the skills from that job help you at all in the design and build of this motor? Or is this solely an enthusiasts desire to get the best results possible?

I do computer/network management and programming for a living. For the past 10 years I have been primarily supporting engineering firms. From that I have had a lot of exposure to engineering principals, CAD systems and CNC. As well as engineering support from some very clever people.

Add to this that I have been building engines of various kinds since before I could hold a license.

I've decided to get a set of Supertech valve springs for this current engine to sort out the valve float issue, and hopefully punch through that 500kw atw limit. Then maybe also a switch to an EFR 9180 as well.

Truly epic thread here! So thorough and well thought out.

A pleasure to read it from start to finish. If/when you make this a "kit" I can only hope I'll be in a position to get a setup like this for my 33 GTR.

Keep up the great work.

  • 4 weeks later...

Great thread. Have spent the day reading through!

Amazing GTR.

Look forward to updates/ more pics.

Are you running stock gearbox?

Dan

Thanks Dan.

Not much to report other than that I am going through E85 like no tomorrow. I must do a video of what the car drives like. There is a little maintenance to catch up on, needs a wheel alignment and balance, but other than that its still going strong.

Yes its still a stock getrag for the moment. Basically I'll drive it like this until next year some time when it will get an OS88. The drag strip is still being built, so I wont be breaking the getrag anytime soon.

The main focus is on the next two engines now, which will hopefully be finished around November.

  • Like 3

These next two engines are about stress testing the design. Both are being built with a 1000+hp power goal in mind. No expense spared, with a focus on maximum strength for all components.

Once testing has proved the design holds up for the first engine, the second will become available as the first to ever be sold.

  • 3 weeks later...

I am still in the process of getting the final parts made for the next two engines.

One of the two cylinder heads is ready to go. Ported, oversize valves, 280x11.5 cams, dual springs, the works. The second head is still being made, and in comparison it makes the first one look like stock. I am told it will flow past 1kw with ease.

Two crankshafts have been completed and are ready to install. One 87.8mm and one 89.8mm, both with 19mm GTiR journals and clearenced for oil squirters.

Two N1 24U Blocks are now partly composite resin filled, and are about to be sleeved and fitted with girdle plates and main caps. Then onto final bore/hone machining once the pistons arrive.

I am hopeful that I will be assembling engines early to mid December.

Edited by GTRNUR
  • Like 2
  • 1 month later...

I am still waiting on pistons for the next two engines. It took quite some time to get the specifications sorted out for something that will handle extreme punishment for an extended time. In the end I went with a custom JE and Trend DLC coated gudgeons. I'm told they will handle 1800hp+, with a specification normally found in a methanol engine.

I completed the rear R35 GTR brake conversion, and have a functional hand brake thanks to modified Toyota Rav 4 hand brake shoes.

Other than that I have been working on the front suspension lately. I've changed the lower control arms to R33 GTR items, so I can use adjustable tension rods. I've yet to locate or make a set of roll centre correction spacers. Upper arms will be fitted with superpro offset bushes to correct camber.

I've also done the first plug change and compression test since the tune. Dry test and every cylinder is within 3psi, which is amazing. The best leak down and pressure test result I've ever had. Then I re-pressure tested the entire intake side of the engine and found the reason I didn't break 500kw in the last tune session. At some stage between the first and second tune sessions, a weld had developed a small crack in a pipe that links the turbo to the intercooler. So essentially I made 610hp with a serious induction leak. I've had to turn off boost control now too, as it hit boost cut on the first drive once the leaks were fixed.

I believe the leak was in part due to a mostly torn through nismo engine mount, as there has been other signs the engine has moved a little too much. I was blowing off pipes during dyno tuning, but also, the plenum has made contact with the clutch master cylinder at some stage.

I changed my first front inner CV boot too. What a fun task that is.

That's all for now.

  • Like 1
  • 1 month later...

Update time!

Today truely a great day. With the boost issue fixed Trent from Mercury Motorsport was able to get the engine to perform as I had hoped, and we finally got the 500KW ATW goal.

We had a couple of minor issues with blowing off intercooler pipes again, but other than that the car performed flawlessly.

Huge thanks to Trent @ Mercury Motorsports and Daniel Stephensen from LK motors for performing all the tuning and dyno setup.

526kw atw at 28psi (pipe blew off in this run).

495kw atw at 26psi

33 degrees, 82% Humidity! Stinking hot!

I never saw hotter than 86 degrees on the MFD, (Oil and Water)! My cooling sytem rocks!

post-26553-0-77984400-1449994692_thumb.jpg

Edited by GTRNUR
  • Like 2

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Latest Posts

    • Surely somebody has one in VIC. Have you asked at any shops?  Is this the yearly inspection or did you get a canary?
    • This is where I share pain with you, @Duncan. The move to change so many cooling system pieces to plastic is a killer! Plastic end tanks and a few plastic hose flanges on my car's fail after so little time.  Curious about the need for a bigger rad, is that just for long sessions in the summer or because the car generally needs more cooling?
    • So, that is it! It is a pretty expensive process with the ATF costing 50-100 per 5 litres, and a mechanic will probably charge plenty because they don't want to do it. Still, considering how dirty my fluid was at 120,000klm I think it would be worth doing more like every 80,000 to keep the trans happy, they are very expensive to replace. The job is not that hard if you have the specialist tools so you can save a bit of money and do it yourself!
    • OK, onto filling. So I don't really have any pics, but will describe the process as best I can. The USDM workshop manual also covers it from TM-285 onwards. First, make sure the drain plug (17mm) is snug. Not too tight yet because it is coming off again. Note it does have a copper washer that you could replace or anneal (heat up with a blow torch) to seal nicely. Remove the fill plug, which has an inhex (I think it was 6mm but didn't check). Then, screw in the fill fitting, making sure it has a suitable o-ring (mine came without but I think it is meant to be supplied). It is important that you only screw it in hand tight. I didn't get a good pic of it, but the fill plug leads to a tube about 70mm long inside the transmission. This sets the factory level for fluid in the trans (above the join line for the pan!) and will take about 3l to fill. You then need to connect your fluid pump to the fitting via a hose, and pump in whatever amount of fluid you removed (maybe 3 litres, in my case 7 litres). If you put in more than 3l, it will spill out when you remove the fitting, so do quickly and with a drain pan underneath. Once you have pumped in the required amount of clean ATF, you start the engine and run it for 3 minutes to let the fluid circulate. Don't run it longer and if possible check the fluid temp is under 40oC (Ecutek shows Auto Trans Fluid temp now, or you could use an infrared temp gun on the bottom of the pan). The manual stresses the bit about fluid temperature because it expands when hot an might result in an underfil. So from here, the factory manual says to do the "spill and fill" again, and I did. That is, put an oil pan under the drain plug and undo it with a 17mm spanner, then watch your expensive fluid fall back out again, you should get about 3 litres.  Then, put the drain plug back in, pump 3 litres back in through the fill plug with the fitting and pump, disconnect the fill fitting and replace the fill plug, start the car and run for another 3 minutes (making sure the temp is still under 40oC). The manual then asks for a 3rd "spill and fill" just like above. I also did that and so had put 13l in by now.  This time they want you to keep the engine running and run the transmission through R and D (I hope the wheels are still off the ground!) for a while, and allow the trans temp to get to 40oC, then engine off. Finally, back under the car and undo the fill plug to let the overfill drain out; it will stop running when fluid is at the top of the levelling tube. According to the factory, that is job done! Post that, I reconnected the fill fitting and pumped in an extra 0.5l. AMS says 1.5l overfill is safe, but I started with less to see how it goes, I will add another 1.0 litres later if I'm still not happy with the hot shifts.
    • OK, so regardless of whether you did Step 1 - Spill Step 2 - Trans pan removal Step 3 - TCM removal we are on to the clean and refill. First, have a good look at the oil pan. While you might see dirty oil and some carbony build up (I did), what you don't want to see is any metal particles on the magnets, or sparkles in the oil (thankfully not). Give it all a good clean, particularly the magnets, and put the new gasket on if you have one (or, just cross your fingers) Replacement of the Valve body (if you removed it) is the "reverse of assembly". Thread the electrical socket back up through the trans case, hold the valve body up and put in the bolts you removed, with the correct lengths in the correct locations Torque for the bolts in 8Nm only so I hope you have that torque wrench handy (it feels really loose). Plug the output speed sensor back in and clip the wiring into the 2 clips, replace the spring clip on the TCM socket and plug it back into the car loom. For the pan, the workshop manual states the following order: Again, the torque is 8Nm only.
×
×
  • Create New...