Jump to content
SAU Community

Recommended Posts

Thanks SK. Running standard boost on the dyno (about 7psi) the AFR were going as low as 10:1 - does this mean it was starting R&R?

I had 1.1mm gap plugs before, replaced with 0.8mm NGK - no difference. I checked timing yesterday and looks to be about 18deg BTDC. Wondering whether I should gap down to 0.6mm?

Just envious of other R33 owners who can get up to 12psi without trouble. I wonder why mine is different..

  • Replies 119
  • Created
  • Last Reply

Top Posters In This Topic

Top Posters In This Topic

Posted Images

Thanks SK.   Running standard boost on the dyno (about 7psi) the AFR were going as low as 10:1  - does this mean it was starting R&R?    

I had 1.1mm gap plugs before, replaced with 0.8mm NGK - no difference.  I checked timing yesterday and looks to be about 18deg BTDC.  Wondering whether I should gap down to 0.6mm?

Just envious of other R33 owners who can get up to 12psi without trouble. I wonder why mine is different..

I am surpised just like you, there must be an answer, or maybe several answers, a few little things that add up to a problem.

I have never had to go down to 0.6 mm, the lowest I ever tried was 0.7 mm and it was no difference to 0.8 mm.

I would try advancing the ignition up to 20 degrees, maybe even 25 degrees and see what happens. Listen for pre-ignition very closely, around 3,500 to 4,000 rpm when you load it up, in say 3rd or 4th, going up a long hill is best. If you can hear the pinging then retard it and try again, same hill, same rpm, same gear. Keep retarding until it doesn't ping. Then check it with the timing light and see where it ends up. That rules out ignition timing as an issue.

An A/F ratio of 10 is low, but I have seen 9's before they start running rough.

I assume the air filter and fuel filter are clean and the AFM has been cleaned recently. Yes?

Injector clean and flow test would be on the list, after I had checked that the fuel pressure was OK (36-38 psi at zero boost or vacuum).

Do you know anyone with a Consult screen you can borrow? That will tell you if you have a crook sensor, water temp, TPS, knock etc.

Have you had a leak down test done, ever?

;)

Thanks SK for the ideas.

I think I am at the limit of advance as I have heard slight pinging before so I retarded the timing 1-2 deg and haven't heard it since

1. Fuel filter looks new. Last owner had it done (about 1 year ago) and have the reciept. Maybe I should get a new air filter.

2. I'll clean the AFM - with contact cleaner? Or anything else just as good. - I have carby cleaner at home...

3. Well on the dyno at stock boost it was at 10:1. The car runs perfectly at stock boost - but increase it a little and it kind of hesitates a little as you rev it out. The more boost you run the worse it gets.

4. Havent had a leak down test but it uses no oil and oil is only a little dirty at 5k kms.

5. Don't know whether I should still be looking at coils as there is a little light around them still, maybe this is normal. Although going from 1.1mm to 0.8mm made no difference - if coils were the problem this should have helped??

One night had the boost controller set to about 10psi. I went up a steep hill in 4th - as boost came up to 9psi (at around 3000rpm) the engine almost died. Quite viscous as if I just put on the brakes or lost all forward momentum. If it were coils this probably wouldn't be the case??

The engine doesn't blow smoke or use coolant etc. It feels more as if it is ECU or some thing sensor related that causes it..

I might take the car to UAS as they know skylines.

I can hear a little hissing around the PCV valve hose cannot really see a leak or anything though. I'm wondering whether I could have an intake leak somewhere but not sure how to tell. As this would mean that more air has to travel through the AFM to maintain the same boost level...however when they dyno ran it they didnt find a leak. You would think under boost you would hear one..

Bit annoying...

Hey Sk - could you read the above, hope it's not too long.

Also, you mention about asvancing base timing. Could it be possible that I should be retarding rather than advancing. I'm just thinking that maybe the ecu isR&R due to it knock sensing. What do you think? I can't hear any pinging at the moment..

Thanks SK for the ideas.  

I think I am at the limit of advance as I have heard slight pinging before so I retarded the timing 1-2 deg and haven't heard it since

1. Fuel filter looks new.  Last owner had it done (about 1 year ago) and have the reciept.  Maybe I should get a new air filter.

2. I'll clean the AFM - with contact cleaner?  Or anything else just as good. - I have carby cleaner at home...

3. Well on the dyno at stock boost it was at 10:1.  The car runs perfectly at stock boost - but increase it a little and it kind of hesitates a little as you rev it out.  The more boost you run the worse it gets.  

4. Havent had a leak down test but it uses no oil and oil is only a little dirty at 5k kms.  

5. Don't know whether I should still be looking at coils as there is a little light around them still, maybe this is normal.  Although going from 1.1mm to  0.8mm made no difference - if coils were the problem this should have helped??

6. One night had the boost controller set to about 10psi.  I went up a steep hill in 4th - as boost came up to 9psi (at around 3000rpm) the engine almost died.  Quite viscous as if I just put on the brakes or lost all forward momentum.  If it were coils this probably wouldn't be the case??

7. The engine doesn't blow smoke or use coolant etc.  It feels more as if it is ECU or some thing sensor related that causes it..  

8. I might take the car to UAS as they know skylines.

9. I can hear a little hissing around the PCV valve hose cannot really see a leak or anything though.    

10. I'm wondering whether I could have an intake leak somewhere but not sure how to tell.  As this would mean that more air has to travel through the AFM to maintain the same boost level...however when they dyno ran it they didnt find a leak.  You would think under boost you would hear one..

Bit annoying...

Suggestions follow;

1. Fuel filters are cheap, change it. What air filter are you using? If standard, they are cheap too, buy a new one. Or a Pipercros for $50 for better flow.

2. We use brake cleaner, carby cleaner leaves residue.

3. That's standard ECU R&R, nothing unusual there.

4. Sounds OK, but if you have leaking valves (for example) the oil tests are irrleleant and won't show up anything. Leak down test takes about 1 hour, well worth it.

5. Coils, coils, coils everything gets blaimed on coils. I have never replaced a coil on a RB, maybe I am just lucky. Or maybe its becuase I dry the coils out after I wash the engine, some people don't and drive it with a river of water in the plug valley. Stuffs coils real fast.

Gapping down helps lazy coils and does nothing for stuffed ones. But what you are describing is not a miss (as in 1, 2 or 3 failed coils). All 6 would have to have failed, I don't think so Tim.

6. Nope that's ECU R&R, when it happens on the dyno the car lurches around madly, particularly the 4wd's (GTR's and Stagea).

7. Refer 4 above.

8. Worth a try, please post up what they find

9. Is that with the engine running? Or Off? Leaking around there is a sign of blocked PCV valve, take it out and give it a good clean in some kero. Check the rubber seal while it is out, they wear due to heat. Silicone sealer can help.

10. I would check the AFM voltage, connect a multimeter while driving and look at the voltage. That will tell you where it is on the 0 to 5.1 volt scale.

As a few others have already said, it sounds like it's time for an SAFC, DFA or Power FC. The Stagea was real bad on ECU R&R at 8 psi and 10 to 1 AFR, now it runs perfectly using the DFA.

Hope that helps some more :P

Thanks again SK!! You're really helpful.

Should I connect the multimeter into the ECU or just run some wire through to the AFM. I don't really want to have to cut the wires unless I have to. Do you know at what approx voltage the cars ususally go R&R - is it about 4.8v (I guess it depends on a few factors)?

I can hear a leak around the PCV when car is running. not very loud though but you've given me a few thing to try before I go to UAS. But I think it might be powerfc time.

My coils look ok..the fact that is doing a huge big cut in the power delivery means that I must be bordering on the ecu R&R (unless something else), but it isnt really a miss like you say. I think if I had a leaky valve I would notice it on 7psi right? It's very smooth at stock boost.

Ive got it set on about 9psi now and it ran ok this morning (reset ecu last night), but it feels a bit dead at certain rpm and the at the power isnt as smooth as it could be - maybe just a bit of R&R as you say.

Powerfc time I think - that is after I check all the things you've mentioned

Thankyou!!

PS. I can definately see a little light around the coils - even with my friends set that work at 14psi. Maybe you could see light on all cars if really dark and have the middle cover off. On the side slightly, not a shooting arc just some faint light. There is no burn marks oon either set of coils!! Or cracks..

Thanks  again SK!!  You're really helpful.  

Should I connect the multimeter into the ECU or just run some wire through to the AFM.  I don't really want to have to cut the wires unless I have to.  Do you know at what approx voltage the cars ususally go R&R - is it about 4.8v (I guess it depends on a few factors)?

Either way will work, I do it at the ECU because it is closer and I don't have to run wires though under the bonnet. All you need to know is the pin outs to locate the AFM signal. You are measuring voltage so you don't have to cut any wires, just stick the multimeter probe into the rear (exposed) of the ECU plug.

There is no absolute AFM voltage, it's more a change in voltage. Run it at the highest boost you can get without R&R and note the voltages. Then increase the boost to the amount where you have a problem and note those voltages when it is R&R'ing. That should tell you what the limit is at various rpm's.

What I have seen on the R32GST Commander (when I jack up the boost) is a big jump in AFM voltage at an RPM range (usually around max VE, 4,500 tpo 5,000 rpm). It goes 3.0, 3.0, 3.1, 3.2, 3.2, 3.9 ....that's the problem (not the 3.9 itself) but the 0.8V jump. The Standard ECUs' don't seem to like this and they go R&R (the PFC doesn't care of course).

On the Stagea I used the DFA to smooth out these sort of jumps by correcting the A/F ratios. That accomplished 2 things, stopped the A/F ratios creeping too rich and removed that jump in the AFM voltages. I also used the IEBC to smooth out the boost curve, as the standard turbo gets onto boost very rapidly when the wastegate is held closed by the IEBC solenoid.

Since I retarded the exhaust camshaft timing by 4 degrees, I have noticed a little bit of the R&R has crept back. It feels flat occasionally (not all the time) at 3,000 to 3,500 rpm, so I probably need to do a bit more smoothing. Obviously the change in exhaust camshaft timing has increased the airflow to just over the standard ECU comfort zone. I guess that's a good thing because I know I haven't wasted my time fitting the adjustable exhaust camshaft pulley.

:)

  • 3 months later...
sk i think u should write a book on modifying skyline engines, u would sell a bloody heap and make cash  :)

your a great help to everyone on the forum :D

That sounds like a fantastic idea StageZilla - it would be very helpful for all :D Plus Gary....*cough*....My Dad is a publisher :D

That sounds like a fantastic idea StageZilla - it would be very helpful for all :) Plus Gary....*cough*....My Dad is a publisher  ;)

If I only had time (that's a song isn't it?) :lol:

Maybe I should just put all my posts together in one document and sell that.

Sort of like a collection of short stories.

Shakespear did it with sonnets, so Sydneykid can do it with posts :)

Now all I need is a catchy title B)

:) Cheers :)

  • 2 weeks later...
  • 9 months later...
  • 2 months later...

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Have a look at that (shitty) pic I posted. You can see AN -4 braided line coming to a -4 to 1/8 BSPT adapter, into a 1/8 BSPT T piece. The Haltech pressure sender is screwed into the long arm of the sender and factory sender (pre your pic) into the T side. You can also see the cable tie holding the whole contraption in place. Is it better than mounting the sender direct to your engine fitting......yes because it removes that vibration as the engine revs out 50 times every lap and that factory sender is pretty big. Is it necessary for you......well I've got no idea, I just don't like something important failing twice so over-engineer it to the moon!
    • Yup. You can get creative and make a sort of "bracket" with cable ties. Put 2 around the sender with a third passing underneath them strapped down against the sender. Then that third one is able to be passed through some hole at right angles to the orientation of the sender. Or some variation on the theme. Yes.... ummm, with caveats? I mean, the sender is BSP and you would likely have AN stuff on the hose, so yes, there would be the adapter you mention. But the block end will either be 1/8 NPT if that thread is still OK in there, or you can drill and tap it out to 1/4 BSP or NPT and use appropriate adapter there. As it stands, your mention of 1/8 BSPT male seems... wrong for the 1/8 NPT female it has to go into. The hose will be better, because even with the bush, the mass of the sender will be "hanging" off a hard threaded connection and will add some stress/strain to that. It might fail in the future. The hose eliminates almost all such risk - but adds in several more threaded connections to leak from! It really should be tapered, but it looks very long in that photo with no taper visible. If you have it in hand you should be able to see if it tapered or not. There technically is no possibility of a mechanical seal with a parallel male in a parallel female, so it is hard to believe that it is parallel male, but weirder things have happened. Maybe it's meant to seat on some surface when screwed in on the original installation? Anyway, at that thread size, parallel in parallel, with tape and goop, will seal just fine.
    • How do you propose I cable tie this: To something securely? Is it really just a case of finding a couple of holes and ziptying it there so it never goes flying or starts dangling around, more or less? Then run a 1/8 BSP Female to [hose adapter of choice?/AN?] and then the opposing fitting at the bush-into-oil-block end? being the hose-into-realistically likely a 1/8 BSPT male) Is this going to provide any real benefit over using a stainless/steel 1/4 to 1/8 BSPT reducing bush? I am making the assumption the OEM sender is BSPT not BSPP/BSP
    • I fashioned a ramp out of a couple of pieces of 140x35 lumber, to get the bumper up slightly, and then one of these is what I use
    • I wouldn't worry about dissimilar metal corrosion, should you just buy/make a steel replacement. There will be thread tape and sealant compound between the metals. The few little spots where they touch each other will be deep inside the joint, unable to get wet. And the alloy block is much much larger than a small steel fitting, so there is plenty of "sacrificial" capacity there. Any bush you put in there will be dissimilar anyway. Either steel or brass. Maybe stainless. All of them are different to the other parts in the chain. But what I said above still applies.
×
×
  • Create New...