Jump to content
SAU Community

Recommended Posts

EDIT** guys please keep this a one post per person thread. anything else u want to say in regards to todays event please keep it to one of the threads in the normal vic forum.

cheers.

my results were...

old power output=110rwkw

new power output= 142.5rwkw

mods since last dyno

-Dr_Drifts ECU Special

-Dr_Drifts Custom Bleed Valve

-Cheapo $80 POD filter and bracket

http://members.optushome.com.au/familypics/dynoday

pics there... (still uploading as of 5.08pm)

Link to comment
https://www.sau.com.au/forums/topic/10882-dyno-day-results-and-pics/
Share on other sites

Me 185rwkw at 12psi! (DOH i should have run more)

Jet u wont need a s-afc as your a/f ratios r ***ing near perfect with that 95 stock ecu!

I get paid $4000 lump sum from work coz i am leaving in 2 weeks, so new turbo looks kinda good!!

I was quite happy with my power curve

attachment.php?s=&postid=178189

Mine was a bit all over over the shop (as you can see!), but it got to 183rkw in the end which i'm fairly happy about. Not sure what all the dipping around is.. Sam said it could just be the humid temp, plug gap a bit too big, Profec being shit or could be anything.

I beat prediator by 1.5rwkw  hehehehe

hehe.. yeah, yeah.. not sure about that though! Ok, I'm sticking to one post here :D If you look at it the one that says "MAX 183" thats the blue one right?? but the run before is actually the higher one (007).. the figures on the back (see other post in VIC section) are for the 007 run which show it reaching 187rwkw. Not sure why they picked the slightly smaller one??

Anyway, its too little to worry about, who cares. You can have your victory if you want inasnt :D

Originally posted by predator666

Mine was a bit all over over the shop (as you can see!), but it got to 183rkw in the end which i'm fairly happy about. Not sure what all the dipping around is.. Sam said it could just be the humid temp, plug gap a bit too big, Profec being shit or could be anything.  

hehe.. yeah, yeah.. not sure about that though! Ok, I'm sticking to one post here :D If you look at it the one that says "MAX 183" thats the blue one right?? but the run before is actually the higher one (007).. the figures on the back (see other post in VIC section) are for the 007 run which show it reaching 187rwkw. Not sure why they picked the slightly smaller one??  

Anyway, its too little to worry about, who cares. You can have your victory if you want inasnt :D

those dips on your r freaky pred!

I though u would get more coz the prof b would hold boost alot better than my turbosmart crap!

How much psi were u running?

Till next time i should have new turbo and some other goodies! :D

i scored a 158.2rwkw @ stock boost (7ish)

i dont hav a scanner so you will just have to use your imagination

fuel was running way too rich after 4000rpm so a lot more in potential there after that is fixed (anyone got a cheap S-afc???)

but still im happy wit the result, i dragged a hyundai when i was on my way home! (well they thought i was dragging them until i decided to go over 3500rpm:p)

mods - 3" exhaust

- "el cheapo" pod filter

- mp3 head unit!

I got 174.6 kW running stock except for:

1. 3" Trust front pipe with 4" Trust cat back exhaust

2. Trust Airnx filter

I am pretty chuffed with this figure, but i haven't made up my cold air partition yet, and i've got a JMS 3" dump pipe that couldn't be fitted before the dyno day...

Look out when they're on and one of Sam's bleed valves is on... I WANT 200 kW!!:D

I seem to be running a bit (oops i meant) RICH too (11.5:1), see the dyno below.

-marcus

I managed to get 188KW...

Sam was gonna up the boost to 15psi but he discovered a problem with my spark plugs.....so we stayed at 12....

All up it was a great day

MODS:

- HKS Cat back

- S-AFC

- Pod Filter

- Boost Controller

My Results.

190 kw @ 9psi --> around the 6000-6500 RPM

MODS:

Turbo (no idea what it is yet... but it's big)

Pod

Chipped R33 ECU

3" Zorst

Massive Front mount (stock one for the R)

Was very happy.

should easily see 250 with just some boost.

Hopeing for 300 as my christmas prezzie to myself :)



  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...