Jump to content
SAU Community

Recommended Posts

New wheels for the GTR..

Volk GTC, 19x10.5, +11. 275/30/19 Hankook K107

n630730284_6147360_736772.jpg

n630730284_6147357_1419089.jpg

n630730284_6130672_3567831.jpg

Very happy. :blink:

You certainly got THE CAR that you patiently forecast and got Huy.

More pics of R34s will certainly emerge after 26/4/09 when the 10th ANNIV R34 GT-R CELEBRATION gets under way.

Autumn colours at Mt Wilson will certainly help set them off as well as what will be displayed on HPI via their photographer.

n630730284_6158887_3012704.jpg

Rear has some camber, which is why is looks like it's sitting inside the guard, but the front is sticking out a few mm.

Size is perfect imo!

I prefer the silver for sure.

Edit - All four rims are exactly the same size.

Edited by Huy
Hers a photo of my 34, shes a dirty dirty girl in this photo...

p1802090755.jpg

heres a few more of my car

p160309124301.jpg

w640.png

p160309124101.jpg

going to have the car resprayed eventually... lesson learnt, dont drive behind trucks in the country

w640.png

Edited by Sammy34
hey guys some pics of the 34s

hey GTR32X is FLYT34 urs? saw what seemed to be that exact car being chased by a police car lol. sorry to say, but i was relieved that he wasnt pulling me over :verymad:. but anyway was just wondering if u ended up getting away?

have any r34 owners done a battery relocation to the boot of their cars?? doing one on the weekend and just wanting any tips from ppl who have done it before

I've got one done... not out of choice but out of necessity (new catch can system took up the battery spot).

Not much to it, just need some proper wiring, battery box, good fuse, and some handy work at the terminals / fuse box.

PS; get your grounding right.

I've got one done... not out of choice but out of necessity (new catch can system took up the battery spot).

Not much to it, just need some proper wiring, battery box, good fuse, and some handy work at the terminals / fuse box.

PS; get your grounding right.

what about all this i hear about having batteries in a concealed area bad due to smell or smoe other thing? what about acid leaks?

Do 34s/gts-t/gtts have their batteries in front?

I never took notice, i know the gtr's well my ones have it in the rear.

THE BIGGEST PAIN to remove when they die..

i think 34s were the only ones to have batts in the front. quite annoying for engine mods =[

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Yeah the rule of thumb with an LS is 7psi per 1000rpm. That is decidedly not enough at 6800rpm. I mainly looked for the scenarios where knock started to be picked up and it was later in the session when things were hotter, and oil was thinner, and the pressure was lower than it should be. (i.e very horrible). I am hoping with thicker oil (I was running Penrite ten tenths 10-40, the manual specifies 10-30) that does not leak that it's much improved at that time!!! I am using Project Mu Club Racer CR pads. I'm also using the Project Mu 335C fluid. The symptoms imply that it was fluid that boiled, but no bubbles seemed pretty weird to me when I bled it today. I want to try Castrol SRF as it has a much higher wet temp but, well, I have new Project Mu fluid lol... so I should at least use that. The pedal on track was really noticable. It went from basically normal feeling to instantly near-floor. The car did pull up as before, it was just very much nearly at the floor before the brakes engaged. At that point I pretty much decided the day was very done, it did *kinda* come back during that very slow cooldown lap into the pits. Felt perfectly fine driving home.
    • f**king around with the bro
    • Ludenham   44.2 tops day no issues  
    • Then today, I went to visit a man with an r33 hat Peter and Road and Race sorted the alignment. As it is being set up for general track/hillclimbs etc it has a heap of caster (7o), less camber than I am used to (1o front and 2o rear, as the caster looks after that in turns without the braking downsides), 3mm front toe out and 0 toe rear. Will see how that goes and track tyre wear to see if it does need more camber, but adjsustment is also limited with nismo arms and adjustable bushes at only 1 end. It does have a bent inner tie rod on the driver's side front but as it came up within spec I'll just leave that as is. So, that is getting close to my chapter of this story....could of tidy ups then a shakedown in early October before it finds a new home.
    • So, it went to Unigroup for a run in and tune on Friday, everything went (generally) well. In terms of fixes, the engine was good and there were no leaks. It needed plugs (I hadn't checked them because the coil pack cover was on a new engine and I couldn't imagine they weren't new.....but turns out the temporary plugs to just keep it sealed up were in there.....new plugs gapped to 0.8 and it was fine from there. Also, there was a little preload on the clutch slave which caused some slip. I haven't had the box off so I don't know what the clutch looks like; my guess it is brand new and the pedal had not been adjusted....backed that off a bit and it held fine. Last thing will have Dose crying....the idle especially when cold is a bit difficult between the cams, forward plenum, atmo blow off valve and an 80s air management system. It is fine when hot but a little uneven when cold, will see if I can sort or at least improve that one cold morning. Other than that, tuning went fine. It made 245 but was pulled back to 227 which 2 opportunities to improve in future. 1. The factory CAS is not great and was jumping around at high RPM, so Mark took 2 degrees out up top (that is why it stops making power and lost 20kw). Very safe this way and the extra power is available but will require a more modern ECU and better cam (or even better crank) sensor 2. The 2871 in factory housings is very big for a low mount, and the internal wastegate is too small, so it was creeping from mid range all the way to redline....the duty cycle on the boost controller is turned down a little for safety. That is much harder to fix, it would need a large external gate and that would require a whole bunch of other changes, so it will go as it is for now. It feels nice and healthy and safe, so should be good for about a billion laps like this.
×
×
  • Create New...