Jump to content
SAU Community

Recommended Posts

ok so mods as follows.

standard 25 neo

bosch 044

725 injectors

Z32 AFM

return flow FIMC

turbo back exhaust

GT3076

Nistune.

265 rwkw, 11.8 AFR, 16 PS

...................................................

so last week added splitfires, and changed my spark plugs from bcpr6es to bcpr7es.

Got a retune a few days later.

went on a cruise last night in the pouring rain, and after some mild driving for a few hours , my car started to violently miss fire across the rev range under boost and so i went home.

Next day i pull the plugs to find all fine, a little rich looking, but number six earth point is melted...

Put the old plugs back in, go for a run, still missfiring.

Check plugs again and there all fine.

Check AFM ( which is in the cooler pipes), to find a large amount of moisture inside the pipes.

After investigating, considering the down poor last night, im fairly confident the water was sucked in my intake.

Im letting the cooler and pipes dry out over night so i havent driven the car.

Im not to worried about the water, but the single melted plug as me scared shitless....

Im stumped as to what it could be...

HELP!!!

post-65812-0-11276400-1324210184_thumb.jpg

post-65812-0-97072500-1324210227_thumb.jpg

Link to comment
https://www.sau.com.au/forums/topic/386055-one-spark-plug-melted-rest-are-fine/
Share on other sites

Injectors for sure.

We flow test every single injector from new. A lot have to be at least cleaned, some returned to the supplier.

These are brand new straight out of the box injectors. Its the most logical place to start looking.

sounds like a plan then.

pretty shit considering i was planing on driving home to Sydney from Adelaide on Wednesday...

there goes that plan lol.

ill pull the injectors and have them cleaned...

What about your store bought injector cleaner?

ive got some liqui moly injector cleaner laying around...

worth a shot or not?

do a comp test on it and get your injectors clean. should aleays try and fill up at a quater if you ever get to see the bottom of a fuel tank you would never drop it low again. you need to get them cleaned properly your motor is worth it

Edited by Bsa

Very odd that it was running fine before the tune, 6 cylinder tends to run alot warmer then the rest of the cylinders so generally the tuner will/should add a little more fuel to it to keep it cool... If this hasn't happened then the cylinder runs lean and can cause detonation/ even pre ignition in extreme cases.. Also a melted spark plug may occur.

Clean the injectors, though I wouldn't be putting my eggs in that basket.. Defiantly compression test, you may have mashed ring lands or even a hole burnt in the top of the piston..

Let's hope not anyway...

Ps don't buy that injector clean stuff, pull them out and get it done properly

Edited by GTR_JOEY

What about your store bought injector cleaner?

ive got some liqui moly injector cleaner laying around...

Ps don't buy that injector clean stuff, pull them out and get it done properly

this, dont use the snake oil, get them properly cleaned if you pull them out.

the only way i can think of the water contributing, is if , by pure chance, water got into that cylinder, hydraulic locked it slightly, bent the electrode to touch, and it melted from there.

would be a 1 in a 1,000,000,000,000,000,000 type of thing.

owuld be checking advice above, and progress from there.

good luck.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Good luck on the weekend mate
    • Must have been an absolute nightmare to drive when the power steer was out, the rack ratio/wheel size/caster is all set up for power assistance
    • Welcome to SAU, what are you looking at buying?
    • I checked the injectors again (1 and 2, since they’re easiest to access) to make sure they weren’t clogged. Even though the entire fuel system had been cleaned, I wanted to be certain. Everything looked clean, so I reinstalled and connected everything. When I started the car to confirm everything was okay, it immediately revved up high, so I shut it off straight away. I checked to see if I’d missed a vacuum hose or something, but everything was connected. On the second attempt, the car ran without the high idle, but I noticed a distinct “compressed air” sound coming from the engine bay. Tracing the sound, I pushed injector #6 forward slightly and the noise stopped — it turned out it wasn’t seated properly, despite the fuel rail being bolted down. While holding it in place, the car idled steadily without stalling and ran for over 5 minutes. At this point, I pulled all six injectors out just in case I hadn’t seated them correctly or dirt had gotten onto the O-rings. Unfortunately, I discovered that I had damaged 3 out of 6 injectors (the OEM 270cc ones) during installation. So yes, this was my fault. Since only the pintle caps were damaged, I’ve ordered a Fuel Injector Service Kit from NZEFI to refurbish them. In the meantime, I reinstalled my new injectors – the car now idles fine for over 15 minutes without stalling. I have not attempted to drive it so far. It’s not perfect yet, as it hesitates when the throttle is pressed, but it’s a big improvement. Unplugging the IACV with the new injectors idles at around 800rpm, even with the IACV screw tightened fully. But this is probably due to tune.
    • I wanted to try and preserve the front bumper as long as possible, they're not cheap and are made to order in Japan. Taking inspiration from my previous K11 Micra build where I made an undertray for the Impul bumper, I did the same for this BN Sports bumper but a little slimmed down.  This time round I only made a 'skid plate' (if that's the correct wording/term) for just the bumper surface area, the Micra version covered the gap like an undertray. Starting off with a sheet of mild steel approx. 0.9mm thick 4ft x 2ft in size. I traced around the bumper, cut it out and cleaned the edges. Luckily I was able to get two halves from one piece of metal In the video I installed it as is, but I've since then I've removed it to spray and add a rubber edging trim. The rubber trim is suitable for 1-2mm and it's a really nice tight fit. The bolts had to be loosened due to the plates being too tight against the bumper, the trim wouldn't push on I used some stainless M6 flat headed bolts for a flusher finish (rather than hex heads poking down), I believe this style fastener is used for furniture too incase you struggle to source some. The corner's are a little wider, but this may be an advantage incase I get close to bumping it  The front grill got some attention, finally getting round to repairing it. Upon removal one fixing pulled itself out of the plastic frame, one side is M8 that fixes inside of the frame, where as the other side is M5. Not knowing I could get replacements, I cut down an M8 bolt, threaded it inside the frame along with a decent amount of JB Weld.  The mesh was replaced to match the bumper. One hole on the bonnet/hood had to be drilled out to 8mm to accommodate the new stud, once the glue had set it could be refitted. I think the reason the grill was double meshed was to hide the horn/bonnet latch (which makes sense) but I much prefer it matching the bumper Bumper refitted and it's looking much better IMO The Youtube video can be seen here: https://www.youtube.com/watch?v=bVZP35io9MA
×
×
  • Create New...