Jump to content
SAU Community

Recommended Posts

It may be your issue if you modified it. Do you have access to a compressor, pressure reg and some airline so you can actuate it with air to test how well it moves?

Might be able to pick up a "notchy"section of movement or perhaps it gets stuck somewhere etc

Worth a shot

I think it definetly couldnt hurt. I had a HKS GT2835KAI on my old engine and boost held perfect even though it used the nissan 6 bolt flange instead of the HKS flange which I believe flows a little better

So I put around 22-23psi through the actuator and it opens and closes no worries and the linkage has roughly 10-15mm of travel out & in....

Everything in this situation has checked out normal and ok.... The only thing left to do is drop the exhaust completely and test boost again and then remove the turbo and have it inspected

  • 3 months later...

I did another boost leak test last weekend as my usual preventative maintenance... I normally put my "tap" tool into the start of the cooler hot pipe directly after the compressor outlet... But for a change I pressurised the compressor as well this time.. I put the "tap" at the statue of my air intake where the air flow meter normally goes and then put the usual 30-35psi through the system with my compressor and controlled via twin regulators and than spray soapy water on everything and look/listen for the bubble..
I found that the screws that hold the comp housing to the backing plate are leaking through their threads as the threaded holes go all the way through to the inside of the comp housing. I removed each bolt one at a time and liberally put some loctite 567 heigh pressure thread sealant on each one drove them back home... Retested and Problem solved. No leaks anywhere else. Then I checked and Re-tightened my four t3 flange bolts just to be sure (one was a little loose for my liking), hosed all the soap off and started the car to dry out the engine bay.

This is when I noticed a strange reverberating, tinny, rattling sort of a noise at the dump/front pipe area... I had always heard a similar noise from that area since the HKS 2835 pro S went on the motor and always just assumed it was engine reverberation noise caused by the stainless HKS dump and Hpi stainless front pipe that went on at the same time as the turbo swap...my previous exhaust on the previous turbo was mild steel from turbo back..
I used a large screwdriver and long piece of aluminium angle as a stethoscope and located the exact location of the noise and turns out its coming directly from the internal waste gate mechanism...
I'm guessing the gate poppet isn't fully seating and rattling around in there hahaha..
As seen earlier in this thread, I replaced the actuator with a bew turbosmart unit and put 21psi Springs in it and pre-loaded the f**k out of it to get it to maintain some sort of boost and get a tune happening... Now I finally think nice located the issue!!
Dump is coming off hopefully this weekend and I might get to the bottom of this once and for all!!

SO.......,

It turns out the actuator bracket wasn't fixed stable and had movement when the actuator was loading and unloading boost...

The noise it was making in my last post above was the internal gate flapper rattling around in the breeze at idle [emoji17]

Because the actuator itself was moving around, the gate preload was changing or being lost altogether.

I ended up welding the actuator brackets together to eliminate any movement and then I cut the linkage down and loaded a bit more preload and back to the dyno today.

 

It now makes boost earlier than it ever has, made 20ish more peak HP and picked up 100hp at 3700rpm

 

For a turbo of this size, it's quite a stout result and I now feel it's performing like it always should have... Remembering it's the .87 ar rear as opposed to all other 2835 pro S results on rb25's are .68 ar

 

The car feels much faster on the road now and even my 315/30 nt01's can't cope anymore with this small but decent gain hahah [emoji4]

 

IMG_8360.thumb.jpg.0123f659dc8a8813379d66979ce694ad.jpg

 

 

  • Like 3
That all makes sense, very nice result - always good to see threads like this updated after resolution, too [emoji4]



Thanks Lith [emoji4]
Would be interesting to see this setup with an external gate set up now [emoji848]
But that won't be happening haha

Now I'm just hoping my new hta3076 twin scroll setup can give same sort of response and a father mid/top end power band
Great news! I just saw your post in the RB dyno results page and quickly came over here to check what the fix was. Response still looks great too. 



Thanks man (:
It's very responsive having 240kw at 4krpm makes for a very fun street car indeed.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Cheers. Skyline is back on the menu, can’t get rid of it. It’s like a child you don’t want, or herpes 
    • I got back to Japan in January and was keen to get back on track as quickly as possible. Europe is god-awful for track accessibility (by comparison), so I picked up a first-gen GT86 in December just to have something I could jump into right away. The Skyline came over in a container this time and landed in early January. It was a bit battered after Europe, though—I refused to do anything beyond essential upkeep while it was over there. The clutch master cylinder gave out, and so did the power steering. I didn’t even bother changing the oil; it was the same stuff that went in just before I left Japan the first time. Naughty. Power steering parts would’ve cost double with shipping and taxes, so knowing I’d be heading back to Japan, I just postponed it and powered through the arm workout. It took a solid three months to get the car back on the road. Registration was a nightmare this time around. There were a bunch of BS fees to navigate, and sourcing parts was a headache. I needed stock seats for shaken, mistakenly blew 34k JPY on some ENR34 seats—which, of course, didn’t fit—then ended up having the car’s technical sheet amended to register it as a two-seater with the Brides. Then there’s the GT86. Amazing car. Does everything I want it to do. Parts are cheap, easy to find, and I don’t care what anyone says—it’s super rewarding to drive. I’ve done a few basic mods: diff ratio, coilovers, discs, pads, seat, etc. It already had a new exhaust manifold and the 180kph limiter removed, so I assume it’s running some kind of map. I’ve just been thrashing it at the track non-stop—mostly Fuji Speedway now, since I need something with higher speed after all that autobahn time. The wheels on the R34 always pissed me off—too big, and it was a nightmare getting tires to fit properly under the arches. So I threw in the towel and bought something that fits better. Looks way cleaner too (at least to me)—less hotboy, less attention-seeking. Still an R34, though. Now for future plans. There are a few things still outstanding with the car. First up, the rear subframe needs an overhaul—that’s priority one. Next, I need to figure out an engine rebuild plan. No timeline yet, but I want to keep it economical—not cutting corners, just not throwing tens of thousands at a mechanic I can barely communicate with. And finally, paint. Plus a bit of tidying up here and there.  
    • Nope, needed to clearance under the bar a little with a heat gun, a 1/2" extension as the "clearancer", and big hammer, I was aware of this from the onset, they fit a 2.0 with this intake no problems, but, the 2.5 is around 15mm taller than a 2.0, so "clearancing" was required  It "just" touched when test fitting, now, I have about 10mm of clearance  You cannot see where it was done, and so far, there's no contact when giving it the beans Happy days
    • It's been a while since I've updated this thread. The last year (and some) has been very hectic. In the second-half of 2024 I took the R34 on a trip through Germany, Italy, France and Switzerland - it was f*cking great. I got a little annoyed with the attention the car was getting around Europe and really didn't drive it that much. I could barely work on the car since I was living in an inner-city apartment (with underground parking). During the trip, the car lost power steering in France - split hose - and I ended up driving around 4,000kms with no power steering.  There were a few Nurburgring trips here and there, but in total the R34 amassed just shy of 7,000kms on European roads. Long story short, I broke up with the reason I was transferred to Europe for and requested to be moved back to Japan. The E90, loved it. It was a sunk cost of around EUR 10,000 and I sold it to a friend for EUR 1,500 just to get rid of it quickly. Trust me, moving countries f*cking sucks and I could not be bothered to be as methodical as I was the first time around.
×
×
  • Create New...