Jump to content
SAU Community

Recommended Posts

  • Replies 96
  • Created
  • Last Reply

Top Posters In This Topic

the world also has another donut shaped radiator now... from memory he wanted to go again, but the hole in the radiator stopped him right?

RedR32... your car rocked ass... *drools over the signal R32* ... oh and yes, I'll get around to changing your nick to PurpleR32 in a sec.

RedR32... your car rocked ass... *drools over the signal R32* ... oh and yes, I'll get around to changing your nick to PurpleR32 in a sec.

I remember seeing it on Prestiges Mailing List, am I correct?

That my freinds sounds like a nitrous backfire.

 

Does leewah's car run nitrous oxide at all.??

Yes, DeSiReD is correct. My car does run NOS in shows and when drag racing.

the piping from the cooler to the manifold blow off and bent the pipe and some one said it shattered his radiator as well

This is mostly correct. It didn't shatter the radiator, it put a small hole in it when the piping shot off the plenum.

if it was "only intercooler hosing blowing off and cracking the aluminium pipiing.. then WTF was the flash of spark? and then oil .. me things number 5 rod and piston thru block.

Hmmm, bit technical and imaginative but incorrect.

sound like its pretty much the same as what happened to him at heathcote...

Unfortunately Nark, it was nothing like what happened at Heathcote. This one happened coz the piping travelled at a great speed into it....The Heathcote radiator blew due to too excessive pressure.

I bet the nos has backfired.

 

If you watch the video you can hear they slow it up and then give it the boot and if the nos was engaged when they did that then it would have filled the plenum and cylinders with gas.

 

Nitrous is a very funny thing and if you stuff up with it it can go very bad very quickly.

Give this man a trophy. Correct. The NOS backfired due to a stuck switch engaging the NOS when it shouldn't have. Ie. Too early.

The oil leaking probly comes down to metal maybe piercing the engine oil cooler or maybe if he has a remote oil filter that may have been pierced.

Actually....take that trophy back. No oil cooler to pierce nor a remote oil filter :P

Oh and also did it crack his front bar or anything? because i realised it started swaying :D

No it didn't touch the front bar. Total falacy.

its that the GTR from ICE Performance?

Yes it is. RacePace Motorsport also had a lot to do with the inital development of the car.

Found this in another thread before MAS

 

Quote:

Leewah[/b]]

Originally Posted by Leewah

 

I'm not gonna break the car for a trophy.  

But you broke the car and didnt get a trophy

Obviously you didn't stay for the trophie ceremony where I won "Tough As Nails" for the 3rd time running. That's OK though, not many people do ;)

Man, am I buggered. I have slept a total of 9 hours since Friday night, so I'm stuffed and short in paitence. I'm wearing total black today to mourn the dispair of not taking back the 4WD record at MAS.

Anway, you guys wanted an account of what happened, here goes....

On Friday night the car was prepped and ready. We made final adjustments and dynoed the car at Ice Performance making a comfortable 591rwkw with gas. This was better than the 556rwkw we made back in April.

The car sat happily on the FangArtists stand all weekend without a problem and without any bits being stolen which was a good thing.

When the car got on the dyno, nothing was changed and the car began ramping up. When the NOS switch was turned on, a huge bang occured with a rather large flame coming out the top. I was standing pretty close to the front of the car but unfortunately I wasn't facing the engine bay at the time. Anyway, the huge flame and bang made everyone duck for cover as if we were under attack but as soon as I heard it, I suspected the NOS has done something very very naughty.

My suspicion was true. The NOS switch had locked itself into the armed position which cause the NOS to be fired into the piping leading to the plenum too early causing a backfire. The pressure from the explosion caused the cooler piping to essentially spilt and come off the silicon connectors. The piping came off with such force that it swung forwards and hit the radiator, rupturing it and leaving a small hole. There was no oil leaking from the car either.

The car was driven off the dyno, back onto the tow truck at the end of the night and into the factory.

A check of the engine has come up with nothing. Because the explosion happened in the piping and then blew off the plenum, the engine was saved and is still in perfectly good working order.

The only parts that need to be replaced after this thing is the cooler piping and a radiator. It could have been much worse but thankfully the safety measures were in place and did their job to a tea.

Working for Cabin over the weekend was another great experience. James, Ash, myself and a couple other people over the weekend lent a hand to Cabin and helped move over 120 cars on and off the dynos to and from their displays. Cars like the widebody Accord were absolute hell. With rims the size of manhole covers, the width and turing circle of a 747, it was no easy task moving it to the dyno to find that it was too low. Going back was even worse as the driver couldn't reverse park very well. I think working for Cabin allowed us to move cars more efficiently and flowing nicely. We hope you all enjoyed the show as I can assure you all that we worked like absolute dogs. It was defiantely the hardest I've worked in a long time.

Thanks to the FAs for putting up another great stand. Although the position wasn't as good as last time round, we did the best with what we had. We still walked away with 6 trophies and a nominee for King of AutoSalon with the Ice Supra. Great work Nige.

My thanks go to Damian, Andrew, Charles, Gareth and all the other Cabin staff who made Melbourne AutoSalon Semi-final another great show.

Thanks for Sam and Nick from XTC for operating the dyno all weekend and getting through the 120+ cars we ended up completing. Also a massive thanks to Sam and Nick for understanding our needs in having our own dyno operator. Without your understanding and efforts the 2 most powerful cars and my POS wouldn't have made the dyno.

A check of the engine has come up with nothing.  Because the explosion happened in the piping and then blew off the plenum, the engine was saved and is still in perfectly good working order.

Good to hear, hope its back up and running soon :D

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • LOL, when one "money pit" is never enough Noice, and excellent work mate
    • I have more than enough digging, laying blocks, moving gravel, airrating, feeding and top soiling the grass, and setting up the veggie gardens growing some seedlings,  and then removing all the unused rock to keep me busy for the next few months at least,  hopefully the rain stops soon so I can get a few hours in this arvo, but, before that Sunday is washing day, is every body happy, you bet your life we are Nice country road day drives are a day off whenever I'm muscle sore from all the landscaping at the moment, but, more epic multiple day drives will start once the majority of the big jobs outside are completed
    • I hear that would involve some nice country road drives into the hills for Mark...
    • I thought I'd come back and add something I JUST learned. A Toyota LandCruiser with a 1HZ, mates perfectly with a bottle of Nulon brake fluid. As in, it perfectly screws in. Great make shift funnel when you cut the bottom of it off. This may work for your Corolla.   Unfortunately, tipping a 10L drum is much harder than a 4 to 6L bottle, and they no longer include the easy pour tap which was just perfection to use previously.  
    • Guys since i bought r33 gts25t coupe 1994 automatic a/t(manual swap 350z gearbox)  all i got is problems, always problems. Lets start with that when i turn key into ignition(ON) fuel pump doesnt always works. Sometimes i have to turn key twice Off/on/off/on until it primes. Its new, dw300 - 340lph. My gearbox broke so i did gearbox swap, install different intake manifold, injectors and i take pipes. Car was sitting in garage for more than half a year. I did assembly all not that long ago and when i turn ignition cant hear prime. All of sudden it stopped working. Theres many videos on YouTube how to make relay mod on r33 straight from battery so i did and it doesnt work! 😰 30 - battery positive  87 - positive from fuel pump to relay 85, 86 - one of two wires from original fuel pump wires(light blue, grey) and it didn’t work. so I check on ignition and took original BLUE relays wires from trunk, next to fuses. (I believe it’s IGN+ and ECU pin 18. it didn’t work…  tried connecting (IGN+ from og relay) and (ECU 104 from 1of4 FPCM wires) to my new relay 85/86 and it didn’t work.  I unplug FPCM. Didn’t work. im thinking what’s wrong   fuel pump is working, if I leave IGN+ on 85 and 86 straight to ground it works but it’s just nonstop. Since it getting constant 12v after key in ON. light blue wire gives me 6-8v.  so how this should be connected? What causing ECU not giving — on pin? Or I did sth wrong and that’s why it doesn’t work? I need negative signal on ECU that control fuel pump. What this should be?
×
×
  • Create New...