Jump to content
SAU Community

Recommended Posts

If your able to make it your self it will cost 1/4 of that cost. :)

~$40-50 for welding the 2 bungs in for the bov and breather then a little for the pipe (~$20) + 2 bits of silicon.

If the pipe is in 4" stainless then for a 90degree bend its around $40.

when i did mine i didn't have the catch can and i had the bov hooked up, would've been so much easier for me to make if i'd had the catch can on and the bov d/c like i do now. haha, heinsight's a wonderful thing!

Hey Ash,

Once all tuned up does yours fart and carry on with the bov blocked off?

At the moment untuned mine randomly when coming off the throttle to change gears pops and farts; drivability is fine; very little afm reversion and no stalls. I'm thinking off hooking mine up just to get rid of the popping and farting incase a mr police man is sitting behind at the time. :S

Cubes, I got my turbo 2 afm pipe on with my stocker blocked for the moment with no atmo BOV and it has a catch can installed.

I get backfiring, etc, but its a combination of my 02 sensor dead (reads like 0.02v at idle and randomly goes to 0.30 and then back to 0v while driving) and I have all those mods on stock ecu.

Kind of off topic but while on the topic of catch cans. :thumbsup:

I'm running twin catch cans temporarily to see how much it breathes. If its all good I'll be plumbing it back in. :) lol Reason for twin catch cans is its not as obvious.

So far its all super clean; not a single drop or smear of oil in the can or in the pipe its self. The single 1.5mm restrictor is definitely working well. :(

Pics...

Drivers side u can see how I've T'd in to the cam cover to PCV valve. Its just for looks; the PCV is blocked off.

Passenger side u can only just see the coke bottle with the hose going in to it. Both coke bottles have a modified top so they can breathe and filled with s/steel scourer. Hopefully I can't plumb it all back up as I really don't like catch cans due to being a big hit on the defect list.

---

If your O2 sensor is reading lean constantly unplug it.

Its telling the ecu the mixture is lean so the ecu dumps in more fuel. Your better off with it disconnected. From memory with it disconnected cruise afr's are around the 13:1 mark which isn't so bad.

post-382-1186640517_thumb.jpg

post-382-1186640523_thumb.jpg

Apart from the usual sponge and spray over at car lovers/BP no. :)

It looks clean as I just put it back together; I had the head off to be sorted as well as head oil restrictors and new turbo bolted on.

Give it a month and it will look normal again. :thumbsup:

If your O2 sensor is reading lean constantly unplug it.

Its telling the ecu the mixture is lean so the ecu dumps in more fuel. Your better off with it disconnected. From memory with it disconnected cruise afr's are around the 13:1 mark which isn't so bad.

Speaking of O2 sensors, I filled up last week and got a solid 350km out of her, I think mine could be on its way out....lol I could've sworn i replaced it about 2 years ago. How often have people been changing thier 02 sensors??

Hey Ash,

Once all tuned up does yours fart and carry on with the bov blocked off?

At the moment untuned mine randomly when coming off the throttle to change gears pops and farts; drivability is fine; very little afm reversion and no stalls. I'm thinking off hooking mine up just to get rid of the popping and farting incase a mr police man is sitting behind at the time. :S

nah mine's fine apart from stalling after a while of driving and it defintiely runs richer but once tuned she'll be all sweet, i'd probably run the bov in your instance, u dont need any more response, hehe!

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • What does it look like with highway driving? And yes, I had a similar thought as Duncan. It looks quite similar in my Stagea and I have made myself accept it as normal. Might have to look into it some day  
    • While I was waiting for the new parts to come in for the charge pipe and radiator I decided to do some turbo modification. The drive pressure (exhaust backpressure) was a lot higher that I thought it should be. For 32lbs of boost drive was 55lbs. The turbine housing is a 1.10AR and my turbo builder has suggested to go to a 1.25AR. To test if a larger AR would do anything to reduce drive pressure AND not spend any money I decided to hog out the divider in my current housing. I removed it from the inlet and the whole way through the housing.  After reassembly and testing it doesn't look like this modification did anything for reducing drive pressure or requiring more fuel (making more power). Oh well, it was worth a shot. We'll get some data at the track if it makes it past the 60ft. I also machined a $7 shift knob off Amazon to fit my Stillway shifter since I didn't like the Stillway shift knob. Next on the list was the radiator replacement and fabrication of a new intercooler tube that had no silicon coupler. No pictures of this - I was short on time each night after work to get this done and didn't stop to take pictures.  Next was to get the clutch disks out and replaced. Previously when installing the dogbox I had ordered a set of the same sintered iron disks I had been running because I switched to the 26-spline input shaft. I thought it was odd that they didn't have any markings or brand name on them like all my old disks had but installed them anyway. At the track I could not get the clutch to lock up using my normal strategies. After two track nights I reached out to the clutch manufacturer and ask their thoughts. They said they had to switch the material out because they were having trouble getting the original material and that this new material would not take to being slipped very well.  So out with the first set of 26-spline disks and in with the correct material 26-spline disks. While I had the trans out I added an inspection/service hole. I've wanted one of these for a while. Now I can have a look at things and change the front cover shimming when needed (clutch wear). I hustled and got the clutch change done in a few hours on a Saturday. Hopped in the car and drove home. On the way home I did a 1-3 pull. When shifting from 2nd to 3rd the core plug in the back of the cylinder head popped out and dumped all the coolant. Thankfully I was only 30 seconds from home and coasted it there. Datalog showed nothing unusual and 2.5psi of coolant pressure. That plug has been in there since 1992 but I guess it worked its way out. Pulled the trans AGAIN and replaced the plug, JB welded it in, and made a brace. Also deleted the head drain I had added in during the bearing issue fiasco.  I am currently changing my boost control plumbing to make it cleaner. After that is done I'll make another attempt at getting past the 60.
    • Are you 100% sure this isn't tune related?
    • 140-150 across the board. At this point hoping the grounding harness fixes it. My grounds are all tied to the chassis and none to the battery. For SR and KA that’s never been a problem for me but had a few other guys here and Reddit who told me RB really like a very solid ground setup tied to the battery so going to try that next, I’m stumped if that doesn’t do it. Never had a car have spark and fuel and not fire off before. Only thing I can think is the spark is intermittent/weak because of grounds nothing else really makes sense at this point 
    • I am having close to the same issue. Can you help me with what wire you grounded to get your pump to trigger?
×
×
  • Create New...