Jump to content
SAU Community

Recommended Posts

Just the factory one.. seems accurate enough.. only want to run 1bar so should be fine.

while we are talking boost something i have always wondered about.. with my m35.. if i am sitting on about 70-80kmh and put my foot down about say 1/2 throttle (so a decent amount though not too much).. i will see 14 pound tho the car barely goes anywhere.. this is the first turbo car i have seen where more boost does not neccessarily mean more power to the wheels how the f*k does that happen???

though of course if i put my foot down 3/4 or all the way the boost come on the same way though its all smiles..

real odd..

Edited by Sage222

hmm you could be right.. though seems odd even at that.. 5th gear at 80kmh at 12psi still should haul i would have thought.. tho maybe not.. will knock it back into 4th and try again :)

well yeh pretty much what craig says. theres a mod i could do for it, but your fuel will pretty much go out the window.

just let me know when your back

  • 1 month later...

Ok i had a shot at this on the weekend. seems to have worked (boost is going up when i dial it up!) :)

Just showing you what i did so people can comment on a better way or if i did it wrong..

So i removed the factory boost solenoid completely. and simply plugged in a turbosmart in its place. Mounted it up to the same bracket job done! :)

boost comes on a fair bit quicker.. no more two stage and now sitting at 1bar.

though it seems like the turbo might be running out of puff up top.. boost seems to drop down once i hit a bit over of 5k..

post-78191-0-07466600-1315178339_thumb.jpg

post-78191-0-84075800-1315178358_thumb.jpg

Edited by Sage222

Ok i had a shot at this on the weekend. seems to have worked (boost is going up when i dial it up!) :)

Just showing you what i did so people can comment on a better way or if i did it wrong..

So i removed the factory boost solenoid completely. and simply plugged in a turbosmart in its place. Mounted it up to the same bracket job done! :)

boost comes on a fair bit quicker.. no more two stage and now sitting at 1bar.

though it seems like the turbo might be running out of puff up top.. boost seems to drop down once i hit a bit over of 5k..

and ive just realised you have it plugged in the wrong way.

youre basically on maximum boost and will blow things up pretty soon.

the bleed valve goes between the vacuum line from the intake piping, down to the wastegate actuator.

you have it plumbed into the vacuum waste back into the intake before the turbo.

Those Turbosmart ball and spring style controllers are supposed to be plumbed between the manifold and the wastegate actuator. Follow the hose down to the actuator line, remove the T piece and put the controller in its place with the arrow towards the turbo. The lines will be too large though I think, you may have to run a bit of smaller diameter rubber tubing with some joiners, I used a bit of alloy tube and cable ties.

That said it will work as you have hooked it up, I ran mine like that for a while. Do you have a proper boost gauge? Boost may well drop later in the revs as the turbo runs out of puff up there.

if he has removed the factory actuator, then its not going to work setup like that.

from the picture, it looks like its plumbed between the actuator line and the bleed into the inlet to the turbo (always vacuum) so it will never open the wastegate.

is it supposed to be plumbed between a pressure line (ie after the turbo) and the actuator?

if the stock solenoid was in there, then yeah ok it will work fine.........

thanks for the comments guys. your exactly right scotty its loosing a bit of puff up top.. thought that might be the wastegate though.. i am just using the factory boost gauge currently.. i dont see a reason to change :)

dont think your right zei20l cause if i close the tap completely i run 7psi (approx wastegate pressure).. i turn it up and up it goes.. i run 10.. then 12 then 14.. so its working as it is right now..

if the ECU throws a CEL what will my symptom be? its been unplugged for approx 100kms so far without issue..

appreciate all the info i can get :)

No, should be cool. Im fairly sure you can just bypass the factory solenoid altogether for our usual high boost level as the brass restrictor is still in the line to the T piece.

The stock solenoid usually opens to allow 14psi, bleeding off the excess pressure back to the intake. If it is closed then the boost will remain low as with cold starts. As Iain said you may get an engine light if the solenoid isnt plugged in, and the map sensor may cause one to show anyway if you bump it up too much.

i thought id do a bit of debrief.. well first thing the car is much nicer to drive! heaps more boost downlow and gets on boost much faster.. very happy with it so far.. done 200kms no error yet for not having the factory unit plugged in.. only thing i dont like is that it seems have trouble running anything over 12psi.. occasionally it will run 14 though it seems to have trouble holding it even lower in the rev range.. does this mean i need a scotty special wastegate spring? :)

Edited by Sage222

i thought id do a bit of debrief.. well first thing the car is much nicer to drive! heaps more boost downlow and gets on boost much faster.. very happy with it so far.. done 200kms no error yet for not having the factory unit plugged in.. only thing i dont like is that it seems have trouble running anything over 12psi.. occasionally it will run 14 though it seems to have trouble holding it even lower in the rev range.. does this mean i need a scotty special wastegate spring? :)

more than likely.

The restrictor is inside the hose, replacing the hose will remove it.

That controller should sit inline between the boost source and the actuator, with no bleed setup required. I explained it the other day buddy.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Have a vb in honour of the car comming back
    • It was a great, but typical track day, and some VB was ingested at the night time debrief 🤪
    • And so, to round this out, I couldn't be happier to confirm @MBS206 has decided to buy the car. He drove down from sunny QLD with a trailer last week and it is off to its new home today. I'll let Matt confirm on next steps but I understand broadly that the plan is to leave it pretty much as is, and just get some quality wheel time with a nicely balanced car that is pretty much track ready. There are a few a jobs still to be done first but nothing too major and I think its a very smart buy Dinner last night at the Paragon with a round of VBs (mostly) for Neil
    • Well, 50 pages and the end of a chapter for this car. We took it out for a shakedown at Wakie yesterday, and everything went well. There were a couple of niggles: - Oil cooler fitting leak - tightened, cleaned, stopped leaking - Radiator cap overflow fitting was leaking....Mark called it, the overflow fitting was threaded in and not tight....tightened, tested and held pressure - Small oil leak at the rear of the block, probably the turbo oil feed - too hot to get at it comfortably but probably just needs to be nipped up - leak at the driver's side rear brake line where it meets the hardline. Fitting wasn't loose, so Matt backed it off and back on, no further leaks - there's also a leak somewhere on the top of the fuel tank, maybe that cross over fuel line - that was has been left to fix when its on a hoist Otherwise than those niggles the car went great, turned great and stopped great so it was a very successful day out. I'm always really nervous when a car first hits the track after a long break, especially with a brand new engine as well but it was great. VID-20251011-WA0007.mp4  Big thanks to @The Bogan who dropped by and helped out, @MBS206 and my nephew Lachlan the apprentice.  Neil's wife Mel also surprised the hell out of all of us by dropping by; she's up in Tamworth these days but was travelling to Melbourne so had plausible deniability for turning up at the garage, it was great to see her but also obviously a bit sad all round.
    • Skyline R33 Series 2 sedan tail lights in excellent condition. These are becoming harder to find, especially in this state.    BOTH SETS ARE IN FANTASTIC CONDITION (REFER TO PHOTOS)    ✅ No broken covers or cracks ✅ Lenses are in flawless condition ✅ All rear mounting lugs intact ✅ Comes complete as pictured ✅ Perfect for restoration, replacement, or upgrade   These lights are ready to go, no surprises just quality OEM parts.   These are definitely one of the better sets we have seen in a while. With minimal wear and tear they will come as you see. Bear in mind they are not brand new they are almost 30 years old now. To find them in this condition isn’t easy they can only be obtained on the second hand market.   Australia Wide Postage Available At Buyers Expense. Silver Set:$850 Grey Set:$850 PM Me for purchase or any other questions  IMG_2166.dng IMG_2165.dng IMG_2172.dng IMG_2173.dng IMG_2174.dng IMG_2179.dng IMG_2180.dng IMG_2260.dng IMG_2258.dng IMG_2259.dng IMG_2261.dng IMG_2266.dng IMG_2273.dng IMG_2274.dng IMG_2276.dng
×
×
  • Create New...