Jump to content
SAU Community

Recommended Posts

genuine nissan HICAS tie rods (different to front tie rods!) are about 250$ for both. from nissan. not cheap. but if you go ling long...well...yeah

well if you got a GT-R I wouldn't use ling long, but I own a R33 GTS-t (ling long is acceptable) haha :)

^ maybe he likes HICAS :)

Theoretically it makes sense to have HICAS, and the system was revised in Series III GT-Rs like yours Paul, prior to that HICAS was pretty shit.

I've tossed mine in the bin too, but I own a fridge.

A lock bar doesn't really solve the problem that you probably have anyway. The outer tie rod ends are the spot that wears the most, and a HICAS delete bar leaves those in place. You'd still need to replace them.

Question.....does 5500 rpm relate to a particular road speed at all? HICAS is known to exhibit it's problems at particular speeds because the HICAS computer reaches "panic mode" at those points when given sensors are not working. Steering angle sensor is one that people often accidentally lose when they put a different steering wheel on the car and the hub doesn't have the drive pin for the steering sensor. On my car (last century) it would crank the steering wheel over to the (left? right?) by about 45° when over 80km/h just because no steering sensor. HICAS panic. No steering sensor also meant I couldn't put it into diagnostic mode which made it very hard to work out what was going wrong. The HICAS computer also looks at VSS, and for all I know in the later GTRs it might even be looking at the G sensors. There's lots of things that can make it act flaky.

Try to put it into diagnostics mode (no, I don't know how to do it on your car, only on an R32). Failing that, get a mechanic with a decent scan tool to hook up to the Consult port and see if there are any codes in the HICAS computer. You may have to take it for a drive and trigger the fault to see anything.

Try to put it into diagnostics mode (no, I don't know how to do it on your car, only on an R32). Failing that, get a mechanic with a decent scan tool to hook up to the Consult port and see if there are any codes in the HICAS computer. You may have to take it for a drive and trigger the fault to see anything.

yeah I'm thinking the same

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Yeah the rule of thumb with an LS is 7psi per 1000rpm. That is decidedly not enough at 6800rpm. I mainly looked for the scenarios where knock started to be picked up and it was later in the session when things were hotter, and oil was thinner, and the pressure was lower than it should be. (i.e very horrible). I am hoping with thicker oil (I was running Penrite ten tenths 10-40, the manual specifies 10-30) that does not leak that it's much improved at that time!!! I am using Project Mu Club Racer CR pads. I'm also using the Project Mu 335C fluid. The symptoms imply that it was fluid that boiled, but no bubbles seemed pretty weird to me when I bled it today. I want to try Castrol SRF as it has a much higher wet temp but, well, I have new Project Mu fluid lol... so I should at least use that. The pedal on track was really noticable. It went from basically normal feeling to instantly near-floor. The car did pull up as before, it was just very much nearly at the floor before the brakes engaged. At that point I pretty much decided the day was very done, it did *kinda* come back during that very slow cooldown lap into the pits. Felt perfectly fine driving home.
    • f**king around with the bro
    • Ludenham   44.2 tops day no issues  
    • Then today, I went to visit a man with an r33 hat Peter and Road and Race sorted the alignment. As it is being set up for general track/hillclimbs etc it has a heap of caster (7o), less camber than I am used to (1o front and 2o rear, as the caster looks after that in turns without the braking downsides), 3mm front toe out and 0 toe rear. Will see how that goes and track tyre wear to see if it does need more camber, but adjsustment is also limited with nismo arms and adjustable bushes at only 1 end. It does have a bent inner tie rod on the driver's side front but as it came up within spec I'll just leave that as is. So, that is getting close to my chapter of this story....could of tidy ups then a shakedown in early October before it finds a new home.
    • So, it went to Unigroup for a run in and tune on Friday, everything went (generally) well. In terms of fixes, the engine was good and there were no leaks. It needed plugs (I hadn't checked them because the coil pack cover was on a new engine and I couldn't imagine they weren't new.....but turns out the temporary plugs to just keep it sealed up were in there.....new plugs gapped to 0.8 and it was fine from there. Also, there was a little preload on the clutch slave which caused some slip. I haven't had the box off so I don't know what the clutch looks like; my guess it is brand new and the pedal had not been adjusted....backed that off a bit and it held fine. Last thing will have Dose crying....the idle especially when cold is a bit difficult between the cams, forward plenum, atmo blow off valve and an 80s air management system. It is fine when hot but a little uneven when cold, will see if I can sort or at least improve that one cold morning. Other than that, tuning went fine. It made 245 but was pulled back to 227 which 2 opportunities to improve in future. 1. The factory CAS is not great and was jumping around at high RPM, so Mark took 2 degrees out up top (that is why it stops making power and lost 20kw). Very safe this way and the extra power is available but will require a more modern ECU and better cam (or even better crank) sensor 2. The 2871 in factory housings is very big for a low mount, and the internal wastegate is too small, so it was creeping from mid range all the way to redline....the duty cycle on the boost controller is turned down a little for safety. That is much harder to fix, it would need a large external gate and that would require a whole bunch of other changes, so it will go as it is for now. It feels nice and healthy and safe, so should be good for about a billion laps like this.
×
×
  • Create New...