Jump to content
SAU Community

Recommended Posts

Hi Folks.

Wondering if anyone has heard anything like this before. Head is a RB25DETNeo and this tapping happens just for a minute or two after starting

Hot OR Cold.

There are no unusual sounds otherwise.
It sounds to me that it's similar to a SR20DET VCT rattle, however while this sounds like it is in the same area, it happens if the VCT solenoid is unplugged.
I don't know if this will actually affect things, if the issue is internally mechanical and not solenoid.
There's not a lot of info on VCT rattle on RB25DET's.
I have blocked off one oil feed to the head to combat blowby in the past.
Note: This happens at about ~1500-2000 rpm. It will rattle once, or twice, and the car can rev past it fine. I.e, if you revved to 4k you may hear 1-2 taps while it revs through, but it always appears at that range.
Note: If you rev the car slowly through the rev range after starting, this does not happen. You don't need a ton of throttle, but if you stab it or stand on it it'll happen, it will not happen if you say hold throttle at 10% and slowly rev through the range.


The sound appears to be coming from the intake cam, from what seems to be just under the throttle body.
Again, hot or cold, doesn't matter. Will hear it for about a minute of driving and it'll fade away pretty quick. Leaving the car idling does help if you leave it idle for ~2 minutes etc.
No weird sounds under load at all. Car otherwise drives fine.

From what I can tell, if you leave the car sitting for maybe 5? minutes, the sound will return on re-start. A little less than it would if the car is left overnight, but not much.

Could be related (maybe not) but VCT has only just actually been switched on/wired in recently. Could be piston slap. Could be wrong oil, (5-40, was 10-60 in the past) could be something else entirely. Sound does not appear to be getting any worse since I noticed it (couple of weeks). May have always been there, because the car was previously auto and any throttle will go well over 3k RPM where there's no sound and no load.

Any hints as to what this could actually be given the above info?
Looking to know where to begin, or whether to begin at all if this is actually a common thing people don't talk about.

Could the noise possibly be the iacv or cold start valve doing its thing on start up? Mine makes some pretty weird noises from there until its up to temp.

 

Edit, after re reading your updated post with additional info. Unlikely to be what i suggested.

 

 

 

Possibly, because the stock IACV is broken as it died on the track and gave me 2500RPM idle.
I got around this by actually installing a second IACV which actually controls air flow to the now permanently full open Nissan IACV.

The part that broke, was the part that otherwise moves on heat (i.e the wax pellet). So I can see how heat would no longer affect the operation of that, but I also can't see how it'd change, given it is currently absolutely not functional at all and there's no wiring to the motor right now.

That’s a head scratcher, you might need to just start a process of elimination. The easiest one is to change back to the oil you used to use. Shim bucket clearances would be a good thing to check too.

Update (kind of)

Changed oil, no diff there other than better oil pressure. (10-60 instead of 5-40)
Nothing bearingish in the oil, so I mean that's good. Same amount came out that went in, also good.

Took cam cover off and engine builder had a look, was able to rotate the cam, and have the VCT gear *not* rotate.
Then if rotated the engine enough, it'd get to the end of it's 'play' then lock up and all rotate as one.


After this, it was actually locked up again, moving the cam would move the gear. Until you gave a the cam a little more forceful tug and the cam/vct gear would unlock.


Unsure if this is 'normal' or not. There's also oil (again lol) in the Solenoid plug. Strange. Had one in the past have an oil leak there, and it was able to be moved by hand, the one currently in the car was locked in place (when outside of the car) leading us to surmise the original one was fked as it was unlocked out of the car while the other wasn't.


Changed both the solenoid AND the gear that day. Maybe issue has re-occurred?

Engine builder friend is going to try with people who also own these cars to perform the same test to see if the gear performs the same way.

  • 1 month later...

Nope. Noone has been able to identify this sound whatsoever.  It got *quieter* after an exhaust stud was tightened up. However, the sound is there, so it's entirely possible it was just more audible due to a slight exhaust leak.

It does not appear to be VCT, which is now actually (blissfully) finally wired in and working.

I have a similar issue but only when cold, does your intake cam gear have any play like inward/outward.. 

My head was reconditioned with new springs, 260 cams etc so doesnt make sense to be anything else..

  • 1 month later...

Well, after checking about seventy million things this was actually a badly warped 6boost manifold.


It was 0.5mm out at the front, and 1mm out at the back, and quite twisted. I also had 3 broken studs, but as everything was tight I checked everything else under the sun first.

No more ticky ticky now, and my wallet is much lighter given this also resulted in all the turbo lines being re-engineered as well as a lot of melted wiring from offensively hot exhaust gas going where it wasn't supposed to be.

I only really twigged when I put 98 in the car instead of E85 and could immediately smell the fumes.
Start at the simple stuff, future googlers!

  • Like 1

I hope it’s going back on the dyno now that    all the exhaust gas is making it to the snail and not exiting stage left before it!

The “big turbo” won’t feel as big now. ?

  • Haha 1

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • What an awesome idea to fit the facelift Lamborghini Diablo headlights. They are a perfect fit!
    • An update regarding the registration with the DVLA I sent off the paperwork the day after I collected the car from the port, two weeks later it was all returned with a letter explaining they have rejected the application. This was because the cheque was £20 short for the road tax (I used a price list I found online). Nevermind it is what it is, it was sent back to them the following day with a new cheque. Fast forward another 2 weeks or so, I called them for an update to be told it had been rejected. Yesterday (16th September) I received the documents back along with another letter, this time it was because I didn't put an X in one box on the V750 (personalised number plate certificate), which declared that I had the rights to the personalised number plate. Why this wasn't mentioned in the first rejection letter, I don't know, but it could have saved this headache. The documents were sent back today, so fingers crossed third times a charm and it'll FINALLY be registered on the road just in time for the bad weather (woohoo!) To cheer myself up I lowered the front 25mm, was sick of seeing it sit like a monster truck. No idea how much clearance I'll have getting on and off the driveway, I'll worry about that when I can actually drive it
    • You're going to miss not worrying about rust in the strut towers like the Skyline shitboxes out there
    • A few little updates that weren't filmed due to not taking long to do or not interesting enough for their own video. My new K&N Air Filter arrived, I went with an RU-4180 which matched the dimensions of the universal cone filter the car originally had.  The battery had gone flat, while that was charging I tidied up the spaghetti wiring at the bulk head and down the sides of the engine Next job was to swap the stereo The Kenwood harness had the female ISO plugs cut off and the male ISO plugs cut off the adaptor loom and joined with bullet connectors. I ordered in a repair loom through work and re-did it all. New Kenwood unit installed (Android Auto, DAB, Bluetooth, Reverse Camera) The bonnet/hood gas struts have been poor since collecting the car. I couldn't find any suitable replacements locally so took a chance on a pair from AliExpress.  The originals don't use a retaining clip to secure the cup onto the ball fixture, would explain why I struggled for 10-15mins trying to pry off the cups. The ball fixtures unscrew using a 12mm spanner, new ones are the same size. Sadly no photo of them fitted, you're not missing much lol The dished Momo steering wheel got replaced with my Momo Tuner, turns out I ordered counter sunk bolts for the horn trim ring (like they normally are for the steering wheel) instead of allen cap (flat seat)  A terrible photo of a Quaife style gear shift knob I've had stashed in my tool box for many years after purchasing the incorrect thread size (I can see a pattern emerging with ordering incorrect parts...) Also threw in a cup holder and a (empty) Boss Coffee can, because why not  
    • GT-R clearly the better choice! The 300 is certainly not insaly fast but has a decent amount of poke. Does a nice little drift around the corners with a decent amount of throttle. It's VERY predictable in a slide too.  Feels so progressive! People probably presume there's a 25 year old driving it based on my behaviour this week! 🤣
×
×
  • Create New...