Jump to content
SAU Community

Recommended Posts

Hello,

 

During highway around 3000rpm I'm at around 840 in sixth gear.

During a WOT second gear to 4th gear I'm at 960 and I stopped at this point... (MFD starts to warn me)

Engine iddling I'm at about 550

I didn't pay attention in the past to this as I was solving others issues...

The car is fully stock, everything seems to work good

 

It looks like the engine is running too much lean ? Should I make some log data for the AFR ?

I suspected the fuel regulator and the fuel pump to be 22 years old....Is it probably the issue ?

 

THanks for your inputs

Link to comment
https://www.sau.com.au/forums/topic/482685-stock-r34-gtr-high-egt/
Share on other sites

I had this issue and it turned out to be massively wrong timing making the exhaust valves open too soon. The tuner had seen too many rb26s of all kinds and I think they forget what stock is supposed to be like. They just said to me dont worry about it, metal doesnt melt at that temp.

timing probably isnt your problem just saying that you know best that it has changed, so get to the root cause.

  • 2 weeks later...

So I try to set the ignition to 15,20 or 25 doesn't make any difference..

I have 2.6 bar at iddling on the fuel pressure line (taken after the fuel filter)

I have 3.0 bar when removing the vacum hose or during the next 5secs I put the ignition on

The fuel pressure is between 3.0 and 3.5 bars under WOT

The fuel pressure is droping slowly continuously a bit after I switch off the car

According to the service manual, these values are ok meaning pressure regulator and fuel pumps are ok

I don't know what to do/test...

The car is fully stock, seems to be in good health (no suspect sounds or lack of power )

Any suggestions ?

On 8/11/2021 at 10:28 PM, bigboss59400 said:

So I try to set the ignition to 15,20 or 25 doesn't make any difference..

Man, adding a Heap of timing is a brave move. I hope there was no WOT action while doing that test

  • 3 weeks later...

Thanks for all your input guys 

It looks like the exhaust cam timing is wrong ...(1 teeth off )

However when putting the engine at its top dead center 

the admission cam is 0.5 teeth off and so the exhaust cam is 1.5 teeth off 

Does it means that the timing belt pressure is wrong which explains the 0.5 teeth difference?

Thanks for your time 

20210830_231751.jpg

20210830_231730.jpg

20210830_231650.jpg

On 9/5/2021 at 2:26 PM, bigboss59400 said:

So end of the story 

by setting correctly the timing belt everything Line up correctly 

The car is now running much better !!!

I couldn't go above 800 degree on medium/hard road drive 

I'm so happy 

thanks for all 

You should probably verify your base ignition timing and do a compression test before you celebrate. 

  • Like 1
  • 1 month later...

Yeah I

So to conclude compression test is between 100 and 105psi (full throttle, battery charged )

I always noticed that the high rpm didn't felt powerful

So maybe it has been damaged due to the high temp or not

Anyway it's fine for me at the moment I will leave it as it is

Thanks for the help and suggestions !

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Kinda glad I never got to this ..    https://www.facebook.com/groups/1483859159195077
    • @GTSBoy This method was able to get readings of -10 to -2, so it looks like its monitoring.  Now I need to figure out why the vacuum on the line provided isn't alternating with manifold pressure.  I went with 2 lines that an RB25 tuner recommended but I'll get a longer hose and try directly off the back of the manifold.  He may have been used to OEM intake setups while I have a DBW setup that removed the MAF and IACV.  
    • I work at a car detailing and tinting shop called Quark which gets all manner of German cars in usually (mainly due to a contract with Mercedes Benz Kita Osaka, BMW Nishinomiya and others) but every once in a while something special comes in, like a fully restored 1972 HS30 Nissan Fairlady 240ZG... The shop owner had immediately started applying film to the windows as soon as it was in the shop so the interior was completely covered in towels and plastic sheets. But I could get a few photos of the engine bay which was restored like new. Such an amazing car to see in pristine condition in Japan these days.  
    • Was going to say the car pulls up nicely everywhere, especially going into that last long right hander before the main straight. Looks like a lot of fun.
    • Hey Dave, welcome aboard! Good to see another soon-to-be Stagea owner here. The wagons are awesome — plenty of space, still got that Skyline DNA, and loads of potential if you’re into mods. Definitely post up pics when you get it, everyone here loves seeing new builds. What model/year are you looking at?
×
×
  • Create New...