Jump to content
SAU Community

Recommended Posts

Ok so, my car is shit, that's a good start.

but seriously

I always road tune my car, just do it myself with the data logit package etc.

Thought, hey why not throw it on the dyno and have a quick look at where i am at.

I'm about to upgrade the exhaust and thought it would be interesting to see what difference is made and was thinking of helping out this site with some real world data etc.

my car ......

R32 GTR

R33 rb26 stock bottom end

JUN 264 9.7mm

700cc sards

z32 AFM's stock airbox, KnN panel

2860-5's

exhaust is...

HKS copy dumps

some no name s/s front pipe 63mm x 2 into 3"

3" decat

HKS super dragger

The dyno i used is a Dyno Dynamics with latest software etc, owned privately.

The owner has tuned a few cars but, he left me to my own to use his dyno etc and just go for it.:teehee:

This is great for me, because i love playing with this sort of stuff etc. Not awsome for when i would like support.

When i went i hadn't slept for 23 hours, because of night shift, yep, shit idea, so i really wasn't on the ball on the day either, :wacko:

any way, results....

Top graph boost and tourqe

bottom kw and AF

dont laugh......

IMG_0478.jpg

IMG_0477.jpg

Edited by blue_vl_t
Link to comment
https://www.sau.com.au/forums/topic/380762-my-laughable-dyno-results/
Share on other sites

  • Replies 48
  • Created
  • Last Reply

Top Posters In This Topic

You think so?

I was thinking i was running 1.5 bar, i have a 1.5 bar gauge and upped the boost until i thought it was at the top of the gauge,

so was quite shocked to see what his dyno had to say, assuming i was running 22 psi max, i assume his sensor is reading ok???

I will fit a better gauge soon anyway to see for sure.

I really think the top of the graph is really flat.

perhaps indicating an exhaust upgrade, which i will be doing regardless.

one other thing i was thinking, with the stock air box, i only run the stock air feed, i will remove the 'chamber' from the botom of the box to see if the extra 3" hole makes much difference.

really looks like a restriction to me, the power just rises and stops dead, then flat lines......

I have my theories, but i'm keen to see what people think if could be

I have some HPI 3" dumps and twin 3" into 4" system to go on, just needs a few more bit modified etc. should be soon

Also i do have some cam gears, but not fitted, mostly because they are ebay ones, and i'm unsure if i should trust them???

true, i only have a cheap ass turbotech valve on it too.

Before a retest i will

remove the chamber from the air box

install a EBC, probably Profec B 2

install the new exhaust.

Triple check the cam timing and base ignition timing.

funny thing is, with any more than 14 degrees of timing the power seemed to drop, unless the heat soak make s a huge difference??

Ahh the joy of learning :laugh:

It also looks a bit lazy onto boost... I know -5s aren't exactly punchy on a 2.6L but surely you should be hitting 20psi a bit earlier than that?

I was thinking this also, "big" (lol) rush of power seems very close to 5000rpm on the street :unsure:

Edited by blue_vl_t

Ill bet with the new exhaust you will be able to run a heap more timing and pick up some response to boot.

lets hope so.

I really wanted to do a before/after test, will be good for me and the forum, if it makes the difference to push power over 350rwkw where it should be i will be quite shocked!!!

true, i only have a cheap ass turbotech valve on it too.

Im just running off actuators and a bleed, on much sooner than you are :)

Fix the exhaust, also check the cams are correctly dialled in, that can often be a problem.

Get 20psi holding rather than falling away to 15psi and you'll be right.

Im just running off actuators and a bleed, on much sooner than you are :)

Fix the exhaust, also check the cams are correctly dialled in, that can often be a problem.

Get 20psi holding rather than falling away to 15psi and you'll be right.

on the top graph, the boost is dropping from 27 to 25 psi, fairly sure thats right.............

Oh yes indeed, looking from my phone again, i should stop doing that :(

The boost graph is even lazier then than i thought now im looking from my PC.

Definately exhaust and get the boost control sorted so it comes on much earlier like it should. It still could indeed be the cams not dialled in correctly too.

on the top graph, the boost is dropping from 27 to 25 psi, fairly sure thats right.............

No thats wrong, thats your torque. Notice it starts way off the charts for what you could consider vacuum? Whereas the other one is accurate for what you expect.

Your boost is hitting 20 and bleeding down to 15.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...