Jump to content
SAU Community

Recommended Posts

To avoid being flamed ypu should just do a bit more searching then come back with any q's ypu will find this sort of info already. And no u would ditch the standard solenoid and just use kinugawa gate.

Although i use a kinugawa gate and greddy profec, but thats a different story to stock.

I just received my Kando adjustable waste gate actuator and it's a piece of shite, lovely machined and built, just poorly designed. Even with a 1 Bar spring, it has less spring pressure than the stock RB20 actuator. The point of difference is the size of the diaphragm, the Kando is 45mm and the RB20 is 60mm.

60mm Ø = 2.36 inches, π r² = 4.37 square inches x 10psi = 43.7 lbs spring

45mm Ø = 1.77 inches, π r² = 2.46 square inches x 14.5psi = 35.7 lbs spring

Clearly, if you are going to use a bleed valve, electronic or manual, you are better off with the RB20 actuator.

Have you tried it out yet though or judt theorizing at this point? For i found the kinugawa to be much stiffer and hold wastegate closed much better, so much i had to get a lower psi spring into it.

I just received my Kando adjustable waste gate actuator and it's a piece of shite, lovely machined and built, just poorly designed. Even with a 1 Bar spring, it has less spring pressure than the stock RB20 actuator. The point of difference is the size of the diaphragm, the Kando is 45mm and the RB20 is 60mm.

60mm Ø = 2.36 inches, π r² = 4.37 square inches x 10psi = 43.7 lbs spring

45mm Ø = 1.77 inches, π r² = 2.46 square inches x 14.5psi = 35.7 lbs spring

Clearly, if you are going to use a bleed valve, electronic or manual, you are better off with the RB20 actuator.

Im using a kinugawa as well, and I have noticed the pressure values of the springs don't actually correspond to what pressure your turbo will produce.

However I don't think that should be a problem, just experiment with the different springs available to get the closest one below your target boost. I have a hypergear standard 21u highflow (which means a larger wastegate flap, therefore more force on the gate) and the kinugawa actuator set with about 3 turns of preload. With the 0.8 bar spring it held around 0.6 bar of turbo pressure. Even at that modest spring pressure it has no problem holding wastegate in conjunction with boost control.

The benefits over a factory actuator is the ability to change spring pressure, adjust preload and greater actuation length (which is helpful if you get some boost creep up high revs due to practice of widening the mounting holes on the bracket and adding preload that way)

A bit of both, theory and practical, just holding the actuator in one hand and pulling on the shaft to compress the spring, you can easily notice the wimpy spring in the Kando, Have test fitted it to my spare turbo, and agree with zooomzoom it did need fettling in order to fit properly.

Also disassembled the actuator to check that Kando put the correct spring in there, and according to his colour scheme (yellow=1Bar) it does have the spring I ordered.

Not even going to bother fitting it to the car, let alone wasting dyno time on it, I have enough confidence in my engineering and maths to know whats what.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...