Jump to content
SAU Community

Recommended Posts

DIY:
Hicas ball joint removal & replacement / Gktech lock bar install.
 
Job:
Replace worn out hicas ball joints, without removing hubs.
Fit hicas lock bar.
 
Parts needed:
Gktech lock bar
2x Hicas ball joints

cover1.jpg.20a002e907dda38573d396804fc43bc0.jpg
 
Tools needed:
Jack, Jack stands, WD40, Grease, Impact wrench, Adjustable wrench, Socket set 10-30mm, Circlip pliers, Pliers, Ball joint press kit, 42mm O.D. x 37mm I.D. x 60mm Steel pipe, Pitman arm tool, Angle grinder, Breaker bar, Safety glasses, Hearing protection, Mask.
 
Duration:
3-6hrs.

Difficulty:
Medium - Easy with the right tools.
 
 
Step 1:

Remove rear seat, remove battery earth and remove suspension.

Then carefully jack up the car and use jack stands.
 
46.jpg.c1264be76a2dd92d6433120d3a01c36f.jpg
 
 
Step 2.

Spray wd-40 on the bolts, remove split pin and 17mm nut from ball joint/tie rod end.
 
45.jpg.d1a215e11323e96e06b9c6776cb58cf2.jpg
 
 
Step 3.

Use pitman arm tool or suitable tool to remove tie rod end.
 
44.jpg.146c7967e09de8892e1afce1f51a31c2.jpg
 
 
Step 4.
 
Crack the tie rods from the hicas unit under the rubber boot, unplug the hicas wiring.
 
42.jpg.87217dc8f77e261f4c37dbe310fa7856.jpg
 
 
Step 5.

Remove the 19mm bolts holding the hicas unit to the car and then remove the tie rods.
 
41.jpg.8f12ecf70e1e4961f239117522aa196c.jpg
 
 
Step 6.

Install the tie rods into the gktech lock bar leaving the rubber boots loose. 
 
21.jpg.060ab13cda0d3fe4688be725f4fe931d.jpg
 
 
Set that aside for now. 
 
 
BALL JOINT REMOVAL.
 
cover2.jpg.9f328d717179f063ce6386c651aa76e5.jpg
 
 
Step 7.
 
Remove circlip from back of ball joint.
 
22.jpg.1b1e2a8c3aa19e474f2dd251725d1f07.jpg
 
 
Step 8.

Cut the ball joint stud to allow more space to remove.
 
31.jpg.4da77c9d3ea780a99245f0617b4658ff.jpg
 
 
Step 9.

If you haven't removed suspension do it now.

Use the ball joint press tool to press the joint out.

Most kits don't come with a small enough size pipe to allow for extraction of the joint, so you will have to find a steel pipe of 42mm O.D. x 37mm I.D. x 60mm. Very common pipe size fits perfectly.
 
33.jpg.c80b4ef37a4b6d48e9fe3c741ac03697.jpg

Carefully align your press tool with the pipe on the hub. I used 5mm steel plate as a backing plate and then used the correct size socket to sit flush on the back of the ball joint. This will allow you to push the ball joint through the hub towards the rear. 

32.jpg.4453cb004c6e5202c1404e9ddfb48ca0.jpg
 
 
Step 10.
 
With the ball joint removed, clean the ball joint housing with wd40 and a rag.

30.jpg.145ab309f2456b91493ad44196d67555.jpg

 

Step 11.

Apply grease to the joint and housing.

6.jpg.7e1c01ebeee3c18f195db0d57390b8c9.jpg

 

Step 12.

Use a 30mm socket or similar sized pipe that fits over the rubber boot and sits on the metal rim of the joint to press the new joint in.

8.jpg.3e20d60c0035fa37a7cd8809ffca3912.jpg

Align the press tool with the socket and ball joints rim and start to turn the press tool to insert the joint into the hub.

27.jpg.36e87d900ad9d15d78cbfb6cca0d5e2e.jpg

4.jpg.d374f661c313aa5183176ff341c8ae6a.jpg

3.jpg.2d1eae626d6565bc66af6c4d297626ae.jpg

Joint installed.

23.jpg.b3d8281b8863d529745aeec374f1360d.jpg

 

Step 13.

Reinstall the circlip to the back of the ball joint.

22.jpg.1b1e2a8c3aa19e474f2dd251725d1f07.jpg

 

Step 14.

Cable tie the hicas wiring out of the way.

20.jpg.54159fc3969083e63a3d7e157a95d9fc.jpg

Install the gktech lock bar.

14.jpg.baf0038ee483d1d5c1d842fbc83a1434.jpg

Tighten the 19mm bolts. Check the tie rods are tight, then secure the rubber boots.

19.jpg.44e322758b6658db5bbfa8c01331ef15.jpg

 

Step 15.

Install the tie rod ends and replace the 17mm nut and split pin.

1.jpg.f36faaaf78b6537d1c25b06ecd39fd6f.jpg

 

Step 16.

Reinstall suspension, rear seat and wheels.

Remove hicas bulb on the cluster, or cut hicas warning light wire on hicas cu in boot.

Get wheel alignment.


All Done.

Edited by dyl33

Mental notes;

  1. The above is valid for electric HICAS, like 33 & 34. Not same same for hydraulic 32 HICAS.
  2. I shudder when I see chassis stands under the rear end of the chassis rails. It's too far forward for a stable support and it puts a lot of leverage from the mass of the rear of the car on the contact points and drives dents into the chassis rails. I prefer to locate them carefully under the subframe.
  3. ...
  4. Otherwise. Good.
  • Like 2
6 minutes ago, GTSBoy said:

Mental notes;

  1. The above is valid for electric HICAS, like 33 & 34. Not same same for hydraulic 32 HICAS.
  2. I shudder when I see chassis stands under the rear end of the chassis rails. It's too far forward for a stable support and it puts a lot of leverage from the mass of the rear of the car on the contact points and drives dents into the chassis rails. I prefer to locate them carefully under the subframe.
  3. ...
  4. Otherwise. Good.

1. Correct.

2. I'll take note. There is 4 stands under it, the blue 2 are on the subframe. 

3. ...

4 .?

  • 2 weeks later...

I wasted so much money on the Frenchy's Performance Garage tool. I'm sure it's great if your balljoints are in good condition, but I ended up stripping the coupler nut, and bending the threads on the balljoint trying to use their removal tool. 

I basically ended up doing the exact same thing as this guide to remove mine, and they came out like butter.

I used a torch to heat the knuckle up for around 60 seconds, and I used my 36mm axle nut socket as the retainer. I then used a thick washer on the back first, before putting a 14mm socket on the back to push it the rest of the way. This process took about 15-20 minutes per side, compared to the hours I spent trying different methods. Using the 36mm socket it has the dpeth that you don't need to grind the end of the balljoint off either. 

3e6b37ef690ce0179ebb33414a7e01bb.jpg

Edited by Jarsky
  • Like 1
  • 7 months later...
1 hour ago, Bart Japan said:

Does anyone know how to do a 32? Do you get a fitting that recirculates the HICAS?

If you don't want to remove the lines, I'm selling this spare kit.

134044532_10159572282190400_5239933425189596540_n.jpg.a37065c2d7f4799d69fc20317d281bf5.jpg

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • f**king around with the bro
    • Ludenham   44.2 tops day no issues  
    • Then today, I went to visit a man with an r33 hat Peter and Road and Race sorted the alignment. As it is being set up for general track/hillclimbs etc it has a heap of caster (7o), less camber than I am used to (1o front and 2o rear, as the caster looks after that in turns without the braking downsides), 3mm front toe out and 0 toe rear. Will see how that goes and track tyre wear to see if it does need more camber, but adjsustment is also limited with nismo arms and adjustable bushes at only 1 end. It does have a bent inner tie rod on the driver's side front but as it came up within spec I'll just leave that as is. So, that is getting close to my chapter of this story....could of tidy ups then a shakedown in early October before it finds a new home.
    • So, it went to Unigroup for a run in and tune on Friday, everything went (generally) well. In terms of fixes, the engine was good and there were no leaks. It needed plugs (I hadn't checked them because the coil pack cover was on a new engine and I couldn't imagine they weren't new.....but turns out the temporary plugs to just keep it sealed up were in there.....new plugs gapped to 0.8 and it was fine from there. Also, there was a little preload on the clutch slave which caused some slip. I haven't had the box off so I don't know what the clutch looks like; my guess it is brand new and the pedal had not been adjusted....backed that off a bit and it held fine. Last thing will have Dose crying....the idle especially when cold is a bit difficult between the cams, forward plenum, atmo blow off valve and an 80s air management system. It is fine when hot but a little uneven when cold, will see if I can sort or at least improve that one cold morning. Other than that, tuning went fine. It made 245 but was pulled back to 227 which 2 opportunities to improve in future. 1. The factory CAS is not great and was jumping around at high RPM, so Mark took 2 degrees out up top (that is why it stops making power and lost 20kw). Very safe this way and the extra power is available but will require a more modern ECU and better cam (or even better crank) sensor 2. The 2871 in factory housings is very big for a low mount, and the internal wastegate is too small, so it was creeping from mid range all the way to redline....the duty cycle on the boost controller is turned down a little for safety. That is much harder to fix, it would need a large external gate and that would require a whole bunch of other changes, so it will go as it is for now. It feels nice and healthy and safe, so should be good for about a billion laps like this.
    • what sort of caliper are they? If they are a slider and you gave everything a good clean, you might need to regrease the pins. My guess though is they will come good after some abuse as suggested above
×
×
  • Create New...