Jump to content
SAU Community

Recommended Posts

thanks fellas, the 22psi run didnt get much more power than the 18psi (another 40hp or so) so it looks like its running out of puff on the old t04z, it is a conservative dyno compared to some other ones in perth so it should crack 600 on other dynos if im lucky. looks like its turbo upgrade time to something huge that will make full use of the stroker kit in the near future and keep the Z for road use :huh:

the sound of it at 8500rpm is pure car porn :angry:

  • 4 weeks later...

I said it before, and I'll say it again...

Holy Snapping Ducksh!t Batman!!!!

Gonna hit the strip anytime soon? Let us all know when so we can come down and watch!

new dyno tune, results are 585rwhp on 19psi and 605rwhp on 22psi (didnt rev to rpm limit due to problems so still abit more in it)

ill post graph tommorow

Brad?

Is this for a Stagea or R33 GTST, because your user details list a R33?

Paul im running the 0.81, maybe there is a difference in hks vs garrett versions for power ;)

the dyno i used is very convservative too

lets just say the car is currently engineless and im planning on building a different setup and this engine go into a rwd track car. Not by choice that the motors out soo quick but some problems happened on the dyno and now the motor is stripped with pistons and rods etc all out.

oh i just love cars :(

Edited by overpowered
Paul im running the 0.81, maybe there is a difference in hks vs garrett versions for power :D

the dyno i used is very convservative too

lets just say the car is currently engineless and im planning on building a different setup and this engine go into a rwd track car. Not by choice that the motors out soo quick but some problems happened on the dyno and now the motor is stripped with pistons and rods etc all out.

oh i just love cars :(

Brad, That's a real shame ;) I'd love to do back to back comparison's of HKS versus Garrett, but I'm guessing your on a T3 hourins, not T4 ?

hey thanks guys for the support, that engine will possibly be back in the stagea but not for a while, ill be running another engine combo for the time being.

Paul my turbo is a t4 flange (my manifold is from Trust and suited for a t78/88).

Edited by overpowered

well, $800 later. was going to be a grand but they did me a good deal. can recommend Boostworx for sure.

exhaust manifold was snapped clean in half, replaced with same, busted radiator when I stopped the car in front of the workshop, replaced with slightly thicker GTst unit, new exhaust studs, redid all the intercooler pipes (lol they asked who fitted it hahaha - me ! dodgy home job) for me, all's running well, bar the RESTRICTIVE rear muffler.

Knew I should have changed it back over xmas. Will get an oval 3inch straight thru muffler, have the adjustable exhaust cam wheel fitted, and retune to 16psi.

scan0001.jpg

Dayz special edition Stagea RS V Four,

89000kms, automatic, RB25DET engine, Attessa 4wd

Clarion stereo tape unit with 6-stack cd player

Clarion amp

Clarion 10inch subwoofer

Pioneer 260w 4-way front door speakers

Eclipse 80w 2-way rear door speakers

Black Widow 10000 car alarm

New Oxygen sensor

New 400amp battery

Penrite 5w-60w oil

Davies Craig automatic transmission oil cooler upgrade kit

Whiteline front and rear adjustable swaybars

Whiteline rear subframe alignment kit

Bilstein front and rear suspension shocks, with ‘lowering’ circlips, using standard springs

Bosch 040 fuel pump with direct battery feed at 13.8volts

Nismo adjustable fuel pressure regulator

Nissan Z32 Air Flow Meter

3inch JustJap stainless steel single dump pipe system

3inch Catco high flow catalytic converter

3inch cat-back mild steel exhaust system with restrictive muffler

K&N pod filter

Maxx’s Cold Air Induction box with direct air feed

BassJunky’s Radiator cold air guide

Hybrid dual stage Electronic Boost Controller, set to 14psi

Apexi 'hybrid' front mount intercooler with custom pipe kit

Apexi boost gauge

Apexi SAFC Super Air Fuel Computer

Apexi SITC Super Ignition Timing Computer

R34 GTT 17inch rims

Hankook K104 tyres, 235/45/17

Sliding Performance 360deg journal bearing oil/water cooled highflowed R33 turbocharger, rated at 250rwkw@1bar

Not Yet Fitted:

Volt stabiliser kit

Whiteline front castor kit

Maltech front and rear stainless steel braided brake lines

DBA slotted front rotors

Aerospeed adjustable exhaust cam gear wheel

Need To Buy:

Free-flowing open design 3inch muffler – current muffler is too restrictive

Retune to 16psi with exhaust cam gear wheel installed set to 4deg retarded, with Hiflow muffler, Id guess 220rwkw should be achievable

exhaust manifold was snapped clean in half

You are kidding! Mine did the same, it started to make exhaust leak noises a couple of weeks ago, which gradually got worse. So yesterday I thought I would tighten up the manifold nuts, they are the usual culprit. Been puting it off as the heat shielding is always a bitch to get off. With the heat shielding (finally) off I was amazed to see a cracked exhaust manifold, all the way around the log between #3 primary pipe and the turbine flange. I have never seen that happen before, and now I read the above.

I will post up some pictures tonight.

>_< cheers :)

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Yeah the rule of thumb with an LS is 7psi per 1000rpm. That is decidedly not enough at 6800rpm. I mainly looked for the scenarios where knock started to be picked up and it was later in the session when things were hotter, and oil was thinner, and the pressure was lower than it should be. (i.e very horrible). I am hoping with thicker oil (I was running Penrite ten tenths 10-40, the manual specifies 10-30) that does not leak that it's much improved at that time!!! I am using Project Mu Club Racer CR pads. I'm also using the Project Mu 335C fluid. The symptoms imply that it was fluid that boiled, but no bubbles seemed pretty weird to me when I bled it today. I want to try Castrol SRF as it has a much higher wet temp but, well, I have new Project Mu fluid lol... so I should at least use that. The pedal on track was really noticable. It went from basically normal feeling to instantly near-floor. The car did pull up as before, it was just very much nearly at the floor before the brakes engaged. At that point I pretty much decided the day was very done, it did *kinda* come back during that very slow cooldown lap into the pits. Felt perfectly fine driving home.
    • f**king around with the bro
    • Ludenham   44.2 tops day no issues  
    • Then today, I went to visit a man with an r33 hat Peter and Road and Race sorted the alignment. As it is being set up for general track/hillclimbs etc it has a heap of caster (7o), less camber than I am used to (1o front and 2o rear, as the caster looks after that in turns without the braking downsides), 3mm front toe out and 0 toe rear. Will see how that goes and track tyre wear to see if it does need more camber, but adjsustment is also limited with nismo arms and adjustable bushes at only 1 end. It does have a bent inner tie rod on the driver's side front but as it came up within spec I'll just leave that as is. So, that is getting close to my chapter of this story....could of tidy ups then a shakedown in early October before it finds a new home.
    • So, it went to Unigroup for a run in and tune on Friday, everything went (generally) well. In terms of fixes, the engine was good and there were no leaks. It needed plugs (I hadn't checked them because the coil pack cover was on a new engine and I couldn't imagine they weren't new.....but turns out the temporary plugs to just keep it sealed up were in there.....new plugs gapped to 0.8 and it was fine from there. Also, there was a little preload on the clutch slave which caused some slip. I haven't had the box off so I don't know what the clutch looks like; my guess it is brand new and the pedal had not been adjusted....backed that off a bit and it held fine. Last thing will have Dose crying....the idle especially when cold is a bit difficult between the cams, forward plenum, atmo blow off valve and an 80s air management system. It is fine when hot but a little uneven when cold, will see if I can sort or at least improve that one cold morning. Other than that, tuning went fine. It made 245 but was pulled back to 227 which 2 opportunities to improve in future. 1. The factory CAS is not great and was jumping around at high RPM, so Mark took 2 degrees out up top (that is why it stops making power and lost 20kw). Very safe this way and the extra power is available but will require a more modern ECU and better cam (or even better crank) sensor 2. The 2871 in factory housings is very big for a low mount, and the internal wastegate is too small, so it was creeping from mid range all the way to redline....the duty cycle on the boost controller is turned down a little for safety. That is much harder to fix, it would need a large external gate and that would require a whole bunch of other changes, so it will go as it is for now. It feels nice and healthy and safe, so should be good for about a billion laps like this.
×
×
  • Create New...