Jump to content
SAU Community

Recommended Posts

  • 3 weeks later...
  • Replies 214
  • Created
  • Last Reply

Top Posters In This Topic

Top Posters In This Topic

Posted Images

  • 1 month later...

Well it has been way way too long between posts but i have got a little more progress.

The new sump and pick up is modified and fitted, the new balancer is fitted and the fitting is in the back of the head and i have made and fitted the head to sump breather line. All that is left to do is tap out the rear of the coolant rail on the drivers side to take a 1/4 BSPT fitting so i can change the hose fitting to a dash 6 AN one, then is it ready to fit.

The engine bay has had a little clean up and all three harnesses are fitted, the fuse box has been re fitted and also the power steer lines and bottle. So there is not much more to do then the engine can be re fitted.

So fingers crossed next weekend all the engine and drive train will be back in the car.

I have laid out the last two remaining harnesses tried to part out the bits that i will remove, I want to remove all the wires for the Hicas including the control module and the sensor in the steering wheel. I have also purchased a Stack dash so the majority of its wires will be removed also. Does anyone know if i will get heavy steering if i remove the whole system? I have heard that this happens if you remove the module on its own. If so can i put a resistor inline to trick the car into thinking that the Hicas control module is still active?

Cheers,

Ryan

Well it has been way way too long between posts but i have got a little more progress.

The new sump and pick up is modified and fitted, the new balancer is fitted and the fitting is in the back of the head and i have made and fitted the head to sump breather line. All that is left to do is tap out the rear of the coolant rail on the drivers side to take a 1/4 BSPT fitting so i can change the hose fitting to a dash 6 AN one, then is it ready to fit.

The engine bay has had a little clean up and all three harnesses are fitted, the fuse box has been re fitted and also the power steer lines and bottle. So there is not much more to do then the engine can be re fitted.

So fingers crossed next weekend all the engine and drive train will be back in the car.

I have laid out the last two remaining harnesses tried to part out the bits that i will remove, I want to remove all the wires for the Hicas including the control module and the sensor in the steering wheel. I have also purchased a Stack dash so the majority of its wires will be removed also. Does anyone know if i will get heavy steering if i remove the whole system? I have heard that this happens if you remove the module on its own. If so can i put a resistor inline to trick the car into thinking that the Hicas control module is still active?

Cheers,

Ryan

Sweet thanks Duncan i am just going to pull the whole system out and see what happens.

Also my new Stack Dash showed up today woohoo.

I've run a few times on the track without the powersteering pump connected.

It's heavy, not too heavy. Quite nice for track work, until you get into a position where you might need to be flicking left to right trying to catch it... :blink:

Moving around pits though... That's a bastard of a job... :P

I put the belt back on for this reason and texikhana reasons.

excellent choice, I would definately go a logging dash if I was starting over again.

it might seem more expensive at first but it will be so much cheaper, more reliable and more useable over the years

Well a small up date the engine and gearbox are back in with the new clutch and one of JP's clutch lines all on new nismo mounts.

I had the engine in and out three fing times till i got the sump to clear the LH mount and the fitting on the back of the head to clear the fire wall, but it is all good now. Most of the engine is wired up just need to sort out he exh side and re fit the intake piping ect.

I also powered up the dash the other day, so so cool.

Not long now. :unsure:

Another small update, the engine is all wired up and oil lines, boost, fuel, w/gate is all plumbed up.

I hand to modify the oil supply hose to the steer rack as it fouled on the sump. It is all good now with new brackets, all i need to do now is make a new oil return hose as the std one has no chance of fitting. I think i am going to run a cheap oil cooler on the return side any ways so it wont be too big a deal.

Also fitted some new bushes to the front of the diff and fitted the tail shaft.

It is getting there slowly.

Nar Noddy, i was thinking about it but i would have been such a pain at this stage cause i would have had to run no booster and change the master cyls, pedals etc. But i did get the dash bar made out of 44 mm tube so i can hang a pedal box off it later and run fwd supports at a later stage.

I have been meaning to Pm you about you car for a while now but have never got around to it, so expect a little PM soon bud.

Thanks for the kind words.

Ryan

We got it to fit and still work in mine.

Starts off the leg in here

interior.jpg

And pop'sut here with a plate on the tower

cage_in_ebay.jpg

Hope to come down some time in the near future for a track day at Wakefield. You guys will have to let me know when some thing is on.

Edited by Noddy

Nice work Noddy, Next time my engine comes out i will attack the engine bay more i think but yours looks nice and access able. There is a SAU day a Wakie coming up soon check out the NSW section for more info closer to the date but i will let you know either way.

Thanks Michael i hope to have it running in 3-4 weeks, i am sick of looking at it not going.

  • 2 weeks later...

Small update,

I ordered a new Radiator off the SAU group buy Group buy link it should show up next week woohoo. I also ordered some new genuine nissan radiator hoses and a Greddy coolant temp adapter do dar. So i might finish off the engine next weekend, all i need now for the engine bay is a cheap oil cooler for the power steering.

I also ordered a set of the Adj lower control arms for the front so that should finish off the handling side for now also.

I made a new steering wheel boss as the HKB one didn't suit me, so if any one wants a new genuine HKB boss for a Hicas, airbag R33 GTST i have one that i am willing to part with.

So fingers crossed i finish welding the drivers seat in and paint the inside next weekend.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • I had 3 counts over the last couple of weeks once where i got stranded at a jdm paint yard booking in some work. 2nd time was moving the car into the drive way for the inspection and the 3rd was during the inspection for the co2 leak test. Fix: 1st, car off for a hour and half disconnected battery 10mins 4th try car started 2nd, 5th try started 3rd, countless time starting disconnected battery dude was under the hood listening to the starting sequence fuel pump ect.   
    • This. As for your options - I suggest remote mounting the Nissan sensor further away on a length of steel tube. That tube to have a loop in it to handle vibration, etc etc. You will need to either put a tee and a bleed fitting near the sensor, or crack the fitting at the sensor to bleed it full of oil when you first set it up, otherwise you won't get the line filled. But this is a small problem. Just needs enough access to get it done.
    • The time is always correct. Only the date is wrong. It currently thinks it is January 19. Tomorrow it will say it is January 20. The date and time are ( should be ! ) retrieved from the GPS navigation system.
    • Buy yourself a set of easy outs. See if they will get a good bite in and unthread it.   Very very lucky the whole sender didn't let go while on the track and cost you a motor!
    • Well GTSBoy, prepare yourself further. I did a track day with 1/2 a day prep on Friday, inpromptu. The good news is that I got home, and didn't drive the car into a wall. Everything seemed mostly okay. The car was even a little faster than it was last time. I also got to get some good datalog data too. I also noticed a tiny bit of knock which was (luckily?) recorded. All I know is the knock sensors got recalibrated.... and are notorious for false knock. So I don't know if they are too sensitive, not sensitive enough... or some other third option. But I reduced timing anyway. It wasn't every pull through the session either. Think along the lines of -1 degree of timing for say, three instances while at the top of 4th in a 20 minute all-hot-lap session. Unfortunately at the end of session 2... I noticed a little oil. I borrowed some jack stands and a jack and took a look under there, but as is often the case, messing around with it kinda half cleaned it up, it was not conclusive where it was coming from. I decided to give it another go and see how it was. The amount of oil was maybe one/two small drops. I did another 20 minute session and car went well, and I was just starting to get into it and not be terrified of driving on track. I pulled over and checked in the pits and saw this: This is where I called it, packed up and went home as I live ~20 min from the track with a VERY VERY CLOSE EYE on Oil Pressure on the way home. The volume wasn't much but you never know. I checked it today when I had my own space/tools/time to find out what was going on, wanted to clean it up, run the car and see if any of the fittings from around the oil filter were causing it. I have like.. 5 fittings there, so I suspected one was (hopefully?) the culprit. It became immediately apparent as soon as I looked around more closely. 795d266d-a034-4b8c-89c9-d83860f5d00a.mp4       This is the R34 GTT oil sender connected via an adapter to an oil cooler block I have installed which runs AN lines to my cooler (and back). There's also an oil temp sensor on top.  Just after that video, I attempted to unthread the sensor to see if it's loose/worn and it disintegrated in my hand. So yes. I am glad I noticed that oil because it would appear that complete and utter catastrophic engine failure was about 1 second of engine runtime away. I did try to drill the fitting out, and only succeeded in drilling the middle hole much larger and now there's a... smooth hole in there with what looks like a damn sleeve still incredibly tight in there. Not really sure how to proceed from here. My options: 1) Find someone who can remove the stuck fitting, and use a steel adapter so it won't fatigue? (Female BSPT for the R34 sender to 1/8NPT male - HARD to find). IF it isn't possible to remove - Buy a new block ($320) and have someone tap a new 1/8NPT in the top of it ($????) and hope the steel adapter works better. 2) Buy a new block and give up on the OEM pressure sender for the dash entirely, and use the supplied 1/8 NPT for the oil temp sender. Having the oil pressure read 0 in the dash with the warning lamp will give me a lot of anxiety driving around. I do have the actual GM sensor/sender working, but it needs OBD2 as a gauge. If I'm datalogging I don't actually have a readout of what the gauge is currently displaying. 3) Other? Find a new location for the OEM sender? Though I don't know of anywhere that will work. I also don't know if a steel adapter is actually functionally smart here. It's clearly leveraged itself through vibration of the motor and snapped in half. This doesn't seem like a setup a smart person would replicate given the weight of the OEM sender. Still pretty happy being lucky for once and seeing this at the absolute last moment before bye bye motor in a big way, even if an adapter is apparently 6 weeks+ delivery and I have no way to free the current stuck/potentially destroyed threads in the current oil block.
×
×
  • Create New...