Jump to content
SAU Community

Recommended Posts

Anyone got some tips as to what is going on here.

Cam tech 270- 9.5mm cams no vct

Shimmed to

.010" intake

.012" exhaust

+\- .001"

Pretty confident of the clearances, have checked twice. Cams don't appear to be hitting anything. Can't see any marks on Pistons (checked with bore scope). Listened with stethoscope and it sounds valve train related...

Running performance springs.

Stock cams were quiet. Same springs just changed clearance

Edited by Huzqld
Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/
Share on other sites

I'm no cam expert (and no idea how to diag by the sound of it), but how did you decide on the clearances and are those hot or cold readings?

http://www.sau.com.au/forums/topic/397382-rb25det-neo-r34-gt-t-valve-clearances-solid-lifters/

Workshop manual in the above thread says 0.31mm intake and 0.51mm exhaust when cold.

0.31mm = 0.012" which is close to your figure.

0.51mm = 0.020" so your exhaust side has about half the clearance it should have

Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/#findComment-7538683
Share on other sites

Have asked camtech. They Aren't really sure what's going on. Obviously more investigating to do.

But always Good to see if anyone else has had issues similar

Came up with those clearances as that's what it says on the cam card they are cold readings.

You are right though the factory cams do run with bigger clearance and that is what I had the stock cams set to and the engine was quiet as.

Edited by Huzqld
Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/#findComment-7538777
Share on other sites

Not running vct in mine anymore.

Triple checked the clearances and it is as per cam card.

Retarded the intake and advanced the exhaust just to see if the noise changed (doing this should effectively give more piston to valve clearance?)

No change in noise.

Will keep investigating.

Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/#findComment-7539155
Share on other sites

The VCT assembly will still need some form of lubrication even if you're not using it. I remember reading some issues a while back about someone swapping heads and didn't keep the VCT oil feed and then had cam bearing issues. But if you are using the stock head and have just unplugged the actuator electronics then it will be fine. Didn't realise the cam had to be modified with a gallery too, sounds interesting.

What viscosity of oil are you using?

Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/#findComment-7540445
Share on other sites

Whoever originally done the vct setup on this head has done it a completely different way to what I've seen them done. They drilled down through the cam gallery and into the vct feed and grub screwed the top hole.

I found the thread somewhere but can't find it now.

But it hasn't worked, the vct half kicks in and then the car just idles normally again. (When testing at idle) made no difference to dyno graph either.

Plus it's an auto with a 3k stall and will probably go bigger down the track.

Didn't check the valve springs honestly (we should have) but they should cope with that lift.. They aren't stock springs and plenty of people have used them on bigger cams then this. They are the 'performance valve springs' springs and ti retainers.

Not sure what you mean by weight on nose of cam, but am only running adjustable gears.

I've packed the cams up and sent them back to camtech to check out.

Put the stock cams back in just to make sure and it's back to being very quiet.

Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/#findComment-7540556
Share on other sites

  • 2 weeks later...

Whoever originally done the vct setup on this head has done it a completely different way to what I've seen them done. They drilled down through the cam gallery and into the vct feed and grub screwed the top hole.

I found the thread somewhere but can't find it now.

But it hasn't worked, the vct half kicks in and then the car just idles normally again. (When testing at idle) made no difference to dyno graph either.

Plus it's an auto with a 3k stall and will probably go bigger stall down the track.

^

The solenoid seemed fine, maybe it was the gear, not really sure. Anyway, no more.

Link to comment
https://www.sau.com.au/forums/topic/456825-neo-noisy-cams/#findComment-7547666
Share on other sites

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • The final part arrived today to un-clampify and simplify the intake Who would have though a 1/2" hose stainless bulkhead fitting designed for below waterline bilge pumps would be what I needed Test fit on a 3" offcut I had laying around to see if it would work, and it worked a treat All going well the intake will be on its "final version" tomorrow 
    • Good luck on the weekend mate
    • Must have been an absolute nightmare to drive when the power steer was out, the rack ratio/wheel size/caster is all set up for power assistance
    • Welcome to SAU, what are you looking at buying?
    • I checked the injectors again (1 and 2, since they’re easiest to access) to make sure they weren’t clogged. Even though the entire fuel system had been cleaned, I wanted to be certain. Everything looked clean, so I reinstalled and connected everything. When I started the car to confirm everything was okay, it immediately revved up high, so I shut it off straight away. I checked to see if I’d missed a vacuum hose or something, but everything was connected. On the second attempt, the car ran without the high idle, but I noticed a distinct “compressed air” sound coming from the engine bay. Tracing the sound, I pushed injector #6 forward slightly and the noise stopped — it turned out it wasn’t seated properly, despite the fuel rail being bolted down. While holding it in place, the car idled steadily without stalling and ran for over 5 minutes. At this point, I pulled all six injectors out just in case I hadn’t seated them correctly or dirt had gotten onto the O-rings. Unfortunately, I discovered that I had damaged 3 out of 6 injectors (the OEM 270cc ones) during installation. So yes, this was my fault. Since only the pintle caps were damaged, I’ve ordered a Fuel Injector Service Kit from NZEFI to refurbish them. In the meantime, I reinstalled my new injectors – the car now idles fine for over 15 minutes without stalling. I have not attempted to drive it so far. It’s not perfect yet, as it hesitates when the throttle is pressed, but it’s a big improvement. Unplugging the IACV with the new injectors idles at around 800rpm, even with the IACV screw tightened fully. But this is probably due to tune.
×
×
  • Create New...