Jump to content
SAU Community

Recommended Posts

Chucked on cooling system pressure tester this morning and found a pin hole leak in the bottom of the radiator on one of the fins.
F*cking shitbox nissan racecar :106_middle_finger: 

Anyone got a 2022 Toyota gr86 they want to swap me






 

2 hours ago, robbo_rb180 said:

Chucked on cooling system pressure tester this morning and found a pin hole leak in the bottom of the radiator on one of the fins.
F*cking shitbox nissan racecar :106_middle_finger: 

Anyone got a 2022 Toyota gr86 they want to swap me






 

Should have bought Reese's from skid control, a quick buff and polish and I'm sure the charring marks would come out :P (I heard it was stolen and lit ablaze :( )

  • Haha 1
Just now, MBS206 said:

Should have bought Reese's from skid control, a quick buff and polish and I'm sure the charring marks would come out :P (I heard it was stolen and lit ablaze :( )

I want the Gr86 not gr yaris 😉

Yeah sucks for him as was a great car, had been in it a few times. 

  • 1 month later...

A few updates in the race car

New radiator is in, required a few small mods to the shroud but all sorted and holds pressure 

20230506_145853.thumb.jpg.1795f5730e82c0edc5c4a1c86625c536.jpg

20230508_162049.thumb.jpg.f8c13f72c6e3d10b5717fcef377dd7ab.jpg

Made up an aluminium foot plate to raise feet up so be more comfortable 

20230509_163637.thumb.jpg.655e48cbf3c12acc7df9f1fae95bc651.jpg

20230509_163742.thumb.jpg.d575b42541dc52ca234afd5ed8412001.jpg

held in by rivnuts and some aluminium angle

also swapped to a lighter battery from the old getz. A few less kg and lower weight.

Just need to check tyre pressures and good to go for a test day Friday before Morgan Park next week.

  • Like 2

Car testing went well Friday, only did a handful of laps but stays cool and brakes work.
Doing some tuning too with boost control and sorting a few areas of fuel map. That confident I haven't even unloaded it,  straight into the shed on the trailer still. Bring on Morgan Park Wednesday 

  • Like 3
21 hours ago, robbo_rb180 said:

Car testing went well Friday, only did a handful of laps but stays cool and brakes work.
Doing some tuning too with boost control and sorting a few areas of fuel map. That confident I haven't even unloaded it,  straight into the shed on the trailer still. Bring on Morgan Park Wednesday 

I was trying to get the bossman to take our work Veloster out to MP on Wednesday. I think he was keen, only if I was already taking a car too, but none of mine to go out there :(

 

I did then try to get him to the Skid control QR AutoCross sprint on Thursday with the whole "No race car? Bring the work car!" I'll remind him I need the company Veloster :P

 

are you doing the Skid Control QR AutoCross on Thursday night too?

  • Like 1
On 5/15/2023 at 2:47 PM, MBS206 said:

I was trying to get the bossman to take our work Veloster out to MP on Wednesday. I think he was keen, only if I was already taking a car too, but none of mine to go out there :(

 

I did then try to get him to the Skid control QR AutoCross sprint on Thursday with the whole "No race car? Bring the work car!" I'll remind him I need the company Veloster :P

 

are you doing the Skid Control QR AutoCross on Thursday night too?

Yeah I am working the rally sprint Thursday. I'll be cruising around the pits and in field area.

 

How good are afternoons at race tracks 

20230516_155710.thumb.jpg.507b7f327c5e8facd3a766755f781c08.jpg

20230516_155744.thumb.jpg.91435655e3ffca449ece92a017bca641.jpg

  • Like 3
  • 3 weeks later...

So..........

Morgan Park was a fail on the brakes. One fast lap and still shudder.
Had another booster from a s14 here so put it on and straight away with a quick blocky was so much better.
Now I have a good work area again I spent the time to go right through the car, bolt check and marking everything. Found a notchy front wheel bearing so replaced it. Full fluid check too. Felt better after doing this as hadn't been done since January. 
Brakeboosterfix.thumb.jpg.80cdf5983e50261d5ceec3041d08927f.jpg
Markbolts1.thumb.jpg.c7a61cdf61558837bfea91e7da70ef77.jpg
Markbolts2.thumb.jpg.324a22f5a97492bd9754cf5a308f60e0.jpg
newwheelbearing.thumb.jpg.c00bd6d51bc4f52ca4432767ab36100f.jpg

With all this done next opportunity I had to drive was at Lakesides All Asian Day with 2 sprint sessions.
Was a bit cautious on the warm up and first fast lap, felt good so sent it. Did a 59.07 then back to back 59.0's second session. Brakes felt great but took an extra lap to come up to temp.
Was fastest car there by a considerable amount and shocked a few by how simple the car is.
My mate with his mazda 2 was doing 68's making some fast cars look silly in the corners.

Mazdaand180sx.thumb.jpg.0d58e6f7b0f619619ca47d7f655a5213.jpg
Towerpic.thumb.jpg.05380f2ef837fb75858bbef7b87296e9.jpg
seagulls.thumb.jpg.13d6a24815cb9d69350343d0b4635a6f.jpg
180sxintoHungryCircleWorkPic.thumb.jpg.5922ac507e54905fb840472deee9409e.jpg

All this was prep for Time Attack round 3 at Queensland Raceway.
Was a cold morning and track took a while to warm up. Used the first session as warmup. The next 2 sessions went and ran 59.0's on clubman layout so was pretty happy as been chasing that for a while, there were mistakes on all laps but got a solid base to work from now. Car was great all day with only a small bit of oil from one of the side diff seals.

Made a video
 

 Thats it for now, give it a wash ready for next event on the 22 June.

  • Like 6
  • 1 month later...

Next Time Attack event just checked fluids, tyre pressures and added a few litres of fuel. 
Nice cool morning and right amount of sun had a heap of people setting PB's. I set a new PB on QR Clubman layout 58.68 which was awesome but had a few issues so normal track day. Had clamps coming loose off intercooler pipes and ended up blowing a decent whole in a silicone.
  20230622_1052591.thumb.jpg.55f461bb06181b25824d67ccc90d4284.jpg

I had a new silicone in the shed but also ordered a heap of constant tension clamps and got it all swapped.
20230628_1138351.thumb.jpg.bf7206d6d03a779ce8f27894f8514f44.jpg

Video from that day, had a weird issue with gopro not recording audio

Built a mezzanine in the shed for all the junk
20230619_1739111.thumb.jpg.ec79fef630f264a35a61ad9b781c3623.jpg
20230628_1135231.thumb.jpg.de3f479c9a7464cc63aeb1e3af8c5641.jpg

Did some more yard stuff with area for water tank, stones around the shed and driveway edge. over 4m3 of road base and stones ,oved by hand 
20230708_1640571.thumb.jpg.fa49c137b5420a47e7446cebbf1bb383.jpg

Got the shed epoxy floor done
20230710_1430391.thumb.jpg.07ba889b7a5918560af6b3eaf6879640.jpg

Next up was King of QR. So car got a good going over with new engine oil and filter, brake bleed, inspect pads, wheel rotation, full bolt check and wheel alignment.
20230721_1034101.thumb.jpg.46f3f70f50eae5bc6920d00796035f82.jpg

King of QR 2023
Great event and did really well, class was stacked with 3 new Supra's with great drivers and a WTAC Hyundai. 
Car performed great and turned it upto around 20psi which definitely made it move.
Ended up finishing 2nd in class around 1.2 seconds behind 1st and 0.052 ahead of 3rd. Which is crazy after all 4 different layouts of QR

National 1:19.442
Clubman 58.932
Sprint 56.229
Sportsman 56.618

IMG_2504.thumb.jpg.31b9d25cafe762f40d3d5169028f08c2.jpgIMG_2514(2).thumb.jpg.674e474c8b27c5152b08621d0ec8ade9.jpg
IMG_1330.thumb.JPG.ad2ac82c83c1198817ae703a61e21022.JPGIMG_1348-CopyK.thumb.JPG.77aee0064fd09cb08b4ec3e35ffe6882.JPGIMG_1356.thumb.JPG.bca985e61c81e7b0d5a672a84402d795.JPGIMG_1405-CopyK.thumb.JPG.c990bfc427708d98b0bee23deb14d9b6.JPG

on board for national layout


Car needs a good going over will change all fluids and potentially need to pull the gearbox to inspect clutch and replace the 5th/reverse selector fork. For a 30 year old car it performed so well against $100+K new cars.

Got Morgan Park time attack mid next month which is an amazing track and should suit the 180sx well.
  

  • Like 6
  • 4 weeks later...

Went out to Morgan Park yesterday for the next round of the Time Attack Super Series.
A bit of a slow start in the morning in first session with traffic and getting everything up to temp.
Second session with no traffic went a bit quicker and set a new pb on e track with a 1:07.91 which placed me third outright. Next session decided to turn boost up but went a little bit slower with carrying a bit of extra speed so stuffed up 2 braking points.
After that noticed a bit of oil from between engine and gearbox and a exhaust nut from the down pipe on the ground. Cleaned the oil up and sprayed a heap of brake clean in bell housing but not much came out, put nut back on and waited for the afternoon e track sessions.
Didn't go any quicker but everyone was .2-.3 slower so cooled it down and missed a K track session to have a go later.
At this point tyres were fair gone and weather had a been a bit patchy with a few drops so took it easy first time out and did a 1:25.9 with traffic so jumped further up the start line next time and  had a 2 back to back 1:24 laps last being a 1:24.57 which placed me 2nd for the that layout. Bloody stoked with that result.

Car all day was down on power and a quick look at gauge was around 12psi at 6000rpm so don't know whats going on there and will definitely investigate and hopefully have time to pull the gearbox before the next round as oil drops are getting bigger.

A quick video on board for K Track layout

 

  • Like 2
  • 2 weeks later...

Found reason down on power....... split silicone off turbo again. Looking back through the data it split at King of qr 3rd session of the day 😅

 

 

Have a cast elbow and billet clamp to fit now. While replacing the gearbox seal and diff seal, inspected tailshaft and all the uni's were stuffed and very worn tailshaft yoke so it's being rebuilt with new uni's, centre bearing and yoke.

Waa going to pull motor and gearbox to try and find where oil was coming from. Took off the exhaust manifold heat shield and found a catch can breather/drain hose pretty much off so that where oil was coming from.

 

  • 2 weeks later...

I had a lot of issues with silicon elbows many years ago and ended up being an engine mount issue causing it to tear! I've never run one off the turbo since as alloy elbow is the way to go!

Good luck with the tailshaft lol... I think mine should be sorted now, won't get to test back at SMSP until later in the year but will do it before Round 6 so I don't have another poor result!

Finally got a chance to go through the build and watch the videos! Awesome stuff... Morgan Park looks like fun, will see if I can get up there later this year but depends on how the rest of the events go for now!

Keep the updates coming!

 

 

 

  • Like 1

Bloody tailshaft curse struck.....

7-8mm too long and new yoke jammed against dust cover. They are fixing it today.

Thanks for watching, Morgan Park is amazing and worth the trip up.


Hoping to have a decent up date either Sat/Sun.

18 hours ago, robbo_rb180 said:

Bloody tailshaft curse struck.....

7-8mm too long and new yoke jammed against dust cover. They are fixing it today.

Thanks for watching, Morgan Park is amazing and worth the trip up.


Hoping to have a decent up date either Sat/Sun.

First time anyone has ever complained about their shaft being too long :P

Hopefully its an easy fix. Did you go to a single or stay 2pc OEM style? I'll be keeping a close eye on how others go with their drivelines after my ordeal. I'm not 100% sure it was the shaft alone that caused my issue, however I feel way better knowing the 2pc is in now and a lot less load on the back of the gearbox especially at high RPM! Just moving around the driveway seems smoother so far.

Will get to Morgan Park over the next 12mths for sure, if we miss the November event I'll make an effort to get some guys together and catch up there at a social day. Jim Berry said he would tag along for the day which would be good!

 

  • Haha 1

Car is all ready for Thursday QR Time Attack round 4

So I had a few little things to sort and thought I'll pull the engine. Start removing bits and found the hose from block to catch can just hanging there, it sits under the heat shield so can't see it. First win.

Pull the tailshaft to replace gearbox rear seal and pull the diff to replace side seal. With that done thought i'll have a good look at the tail shaft. The yoke was very pitted and a decent wear mark, Uni's were all notchy. Tried finding some uni's from a bearing shop but at $400+ and they are staked to need a certain type of uni joint.  I thought a shop should be able to get it sorted for around little bit more so rang around for a price to get uni's but since non replaceble and need to "see it" all were around $1200 and one place wanted to build a one piece, no thank you. Found a shop that was happy to do it, new yoke, centre bearing and the 3 uni's, $900 awesome. Got it back and went to fit it........... yep 7mm to long and was fowling the gearbox dust cover so went back and they sorted it pretty quick with no fuss.
20230906_083922.thumb.jpg.e6b05e614101e509c36c9bdbd0ec00e0.jpg


Next up was the cast elbow. My brother had a sleeve made up as housing was 2.25 and elbow 2.5. Slipped it on and welded it, got the elbow slipped over and welded then the billet clamp. Turbo had to come off ad no studs came out so another win. Fitted turbo back up, measured up the cold pipe and cut what needed to be removed for the other side of the billet clamp. With 3 Tacks done went to do a 4th and blew a hole in the pipe......... Called it quits for the day at that point.
20230909_100756.thumb.jpg.915ab05ab28fffdba67ae5b509d97f94.jpg
20230909_100853.thumb.jpg.6b1095b06e3f8621e751a09b9c2a38f0.jpg
20230909_143647.thumb.jpg.9bbfca6eedb230829a6540ea1ffd044f.jpg

With a day off from it and a hurry up email from event organiser got back into today.

Cleaned up the blowout, cleaned everything, drop down to a 1.6mm tungsten and 6 cup finished up welding the cold pipe, Turned out ok. Its sealed and functional.
20230911_112336.thumb.jpg.cdee7d76f08583bfbb7a6775cee9519e.jpg

started the car up to rebleed coolant and warm up ready for an oil change. Dropped oil and all looks good but the smallest amount of bearing material. I cut filter apart and nothing in it bar a small amount in bottom of housing. Guessing this is normal for what this engine is doing.
Dropped gear box oil and well I found why having trouble shifting. So much syncro material so did the right thing and put in new GL4 oil and ignored that. Only got 3 rounds left for the year so maybe 15-18 proper laps.
20230911_142536.thumb.jpg.a2292a4b557edb95f4065ae42bd84f24.jpg
Diff oil looked good and replaced it with no issues.
also made a drain hose up for the catch can so don't have to take it out to drain. Had plenty of spare fittings so its tucked nicely against the chassis rail.

All that is left to do is a quick wash, top off fuel and load up.

Also started mocking up where I want the hoist to go, need to mod the cross beam to make it work but a mate is coming to install it early October so no more working on the ground soon.

 

20230911_145953.jpg

  • Like 3

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • I had 3 counts over the last couple of weeks once where i got stranded at a jdm paint yard booking in some work. 2nd time was moving the car into the drive way for the inspection and the 3rd was during the inspection for the co2 leak test. Fix: 1st, car off for a hour and half disconnected battery 10mins 4th try car started 2nd, 5th try started 3rd, countless time starting disconnected battery dude was under the hood listening to the starting sequence fuel pump ect.   
    • This. As for your options - I suggest remote mounting the Nissan sensor further away on a length of steel tube. That tube to have a loop in it to handle vibration, etc etc. You will need to either put a tee and a bleed fitting near the sensor, or crack the fitting at the sensor to bleed it full of oil when you first set it up, otherwise you won't get the line filled. But this is a small problem. Just needs enough access to get it done.
    • The time is always correct. Only the date is wrong. It currently thinks it is January 19. Tomorrow it will say it is January 20. The date and time are ( should be ! ) retrieved from the GPS navigation system.
    • Buy yourself a set of easy outs. See if they will get a good bite in and unthread it.   Very very lucky the whole sender didn't let go while on the track and cost you a motor!
    • Well GTSBoy, prepare yourself further. I did a track day with 1/2 a day prep on Friday, inpromptu. The good news is that I got home, and didn't drive the car into a wall. Everything seemed mostly okay. The car was even a little faster than it was last time. I also got to get some good datalog data too. I also noticed a tiny bit of knock which was (luckily?) recorded. All I know is the knock sensors got recalibrated.... and are notorious for false knock. So I don't know if they are too sensitive, not sensitive enough... or some other third option. But I reduced timing anyway. It wasn't every pull through the session either. Think along the lines of -1 degree of timing for say, three instances while at the top of 4th in a 20 minute all-hot-lap session. Unfortunately at the end of session 2... I noticed a little oil. I borrowed some jack stands and a jack and took a look under there, but as is often the case, messing around with it kinda half cleaned it up, it was not conclusive where it was coming from. I decided to give it another go and see how it was. The amount of oil was maybe one/two small drops. I did another 20 minute session and car went well, and I was just starting to get into it and not be terrified of driving on track. I pulled over and checked in the pits and saw this: This is where I called it, packed up and went home as I live ~20 min from the track with a VERY VERY CLOSE EYE on Oil Pressure on the way home. The volume wasn't much but you never know. I checked it today when I had my own space/tools/time to find out what was going on, wanted to clean it up, run the car and see if any of the fittings from around the oil filter were causing it. I have like.. 5 fittings there, so I suspected one was (hopefully?) the culprit. It became immediately apparent as soon as I looked around more closely. 795d266d-a034-4b8c-89c9-d83860f5d00a.mp4       This is the R34 GTT oil sender connected via an adapter to an oil cooler block I have installed which runs AN lines to my cooler (and back). There's also an oil temp sensor on top.  Just after that video, I attempted to unthread the sensor to see if it's loose/worn and it disintegrated in my hand. So yes. I am glad I noticed that oil because it would appear that complete and utter catastrophic engine failure was about 1 second of engine runtime away. I did try to drill the fitting out, and only succeeded in drilling the middle hole much larger and now there's a... smooth hole in there with what looks like a damn sleeve still incredibly tight in there. Not really sure how to proceed from here. My options: 1) Find someone who can remove the stuck fitting, and use a steel adapter so it won't fatigue? (Female BSPT for the R34 sender to 1/8NPT male - HARD to find). IF it isn't possible to remove - Buy a new block ($320) and have someone tap a new 1/8NPT in the top of it ($????) and hope the steel adapter works better. 2) Buy a new block and give up on the OEM pressure sender for the dash entirely, and use the supplied 1/8 NPT for the oil temp sender. Having the oil pressure read 0 in the dash with the warning lamp will give me a lot of anxiety driving around. I do have the actual GM sensor/sender working, but it needs OBD2 as a gauge. If I'm datalogging I don't actually have a readout of what the gauge is currently displaying. 3) Other? Find a new location for the OEM sender? Though I don't know of anywhere that will work. I also don't know if a steel adapter is actually functionally smart here. It's clearly leveraged itself through vibration of the motor and snapped in half. This doesn't seem like a setup a smart person would replicate given the weight of the OEM sender. Still pretty happy being lucky for once and seeing this at the absolute last moment before bye bye motor in a big way, even if an adapter is apparently 6 weeks+ delivery and I have no way to free the current stuck/potentially destroyed threads in the current oil block.
×
×
  • Create New...