Jump to content
SAU Community

Recommended Posts

  • Replies 41
  • Created
  • Last Reply

Top Posters In This Topic

Top Posters In This Topic

Nah not boydy dude, THE BOSS. The mrs, the minister for war and finances etc etc

Thanks Cal, it is an awesome turbo I'm pretty stoked with it. Having said that though I think the total package with the plazmaman has a lot to do with it too.

.................................Plus the tuner :)

Thanks guys, I just cant get over how smooth and responsive this turbo feels.

It actually gets onto boost better than my HG highflow, btw Hamish we were referencing your graph last night when we first had dramas so thanks man haha

lol no worries

Injectors won't handle it I'm afraid. Hamish' 555's are freakish

yeah, i'm not sure what the go is there...

Removing the cat??????? Dunno what your talking about :) :)

Yeh solved all the dramas, it looked sweet as when we looked through it, but when we had it out Boydy gave it a shake and you could hear it rattling around.

It was the tuners decision to "fix" it.

Told you I'd blame you Jez ;)

Never had a cf coil cover, got a billet vented one from the states that Craved coated. I have a cf radiator air guide thingy but I'm having all kinds of trouble getting a nice fit on it so I'm gonna get the sander out, also have a cf bonnet but it's fouling on the strut brace so it's been swapped for the factory one, probably a blessing in disguise cause it will be my daily for a bit so it's more stealth standard. Looks bloody nice though.

Dave finally gets car tuned.. :banana:

So clarify for me, removing the cat solved everything?

What happened to the CF coil cover..?

Yep. Its a highflow cat now. 1cell.

1st run made 210kw and had a slight ping.

2nd run made 93kw with less timing

3rd run more boost 145kw

Then started the diagnosing. Dropped exh from front of cat and made 195 with low timing but still a little laggy.

So we pulled the dump pipe off and it looked like the wastegate flap wasnt sealing, so abit of emery paper cleaned it up.

Now the boost was nice and responsive and we could start tuning

Yep. Its a highflow cat now. 1cell.

1st run made 210kw and had a slight ping.

2nd run made 93kw with less timing

3rd run more boost 145kw

Then started the diagnosing. Dropped exh from front of cat and made 195 with low timing but still a little laggy.

So we pulled the dump pipe off and it looked like the wastegate flap wasnt sealing, so abit of emery paper cleaned it up.

Now the boost was nice and responsive and we could start tuning

Congratulation to you and more to your tuner. I'm really happy to read this. That's some thing when a experienced tuner with the correct knowledge whom can diagnostic the problem and rectify it on the spot.

Those tuners can get you the result or at least pin point the problem that will make the difference. Some other tuners would tell you to go home with 210rwkws.

At one stage I thought I was going home with 90kw

Wouldve given a hyundia Getz a bloody good run though.....

But in all seriousness I don't think Jez was going to let me leave until it made the numbers.

He is very dedicated to getting the tune right

Got the car cleaned up and I'm ready for the show in the morning, also got the cooling panel on after much sanding and drilling.

If anyone in Sydney is around Liverpool in the morning come by and say gday.

Corner of the Hume and memorial ave.

I'm going to bed.

Congrats on the results! Thats great you guys found the problem and sorted it out there and then and got it tuned! At that time I know alot of people would just give up and leave it for another day!

Top effort!

Thanks Michael,

Jez and Boydy deserve all the credit on this one. I'm good at bolting everything together and basic trouble shooting but Jez is pretty switched on and was suspicious of the cat very early on.

I probably confused him a bit by saying that km wise it was not very old (the car is off teh road more than on lol)

Had a good drive of it today for a car show and man it goes good, I'm very happy with the setup. I can't fault this turbo one bit.

I'm sure the tune is also a big part of it though :)

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Good luck on the weekend mate
    • Must have been an absolute nightmare to drive when the power steer was out, the rack ratio/wheel size/caster is all set up for power assistance
    • Welcome to SAU, what are you looking at buying?
    • I checked the injectors again (1 and 2, since they’re easiest to access) to make sure they weren’t clogged. Even though the entire fuel system had been cleaned, I wanted to be certain. Everything looked clean, so I reinstalled and connected everything. When I started the car to confirm everything was okay, it immediately revved up high, so I shut it off straight away. I checked to see if I’d missed a vacuum hose or something, but everything was connected. On the second attempt, the car ran without the high idle, but I noticed a distinct “compressed air” sound coming from the engine bay. Tracing the sound, I pushed injector #6 forward slightly and the noise stopped — it turned out it wasn’t seated properly, despite the fuel rail being bolted down. While holding it in place, the car idled steadily without stalling and ran for over 5 minutes. At this point, I pulled all six injectors out just in case I hadn’t seated them correctly or dirt had gotten onto the O-rings. Unfortunately, I discovered that I had damaged 3 out of 6 injectors (the OEM 270cc ones) during installation. So yes, this was my fault. Since only the pintle caps were damaged, I’ve ordered a Fuel Injector Service Kit from NZEFI to refurbish them. In the meantime, I reinstalled my new injectors – the car now idles fine for over 15 minutes without stalling. I have not attempted to drive it so far. It’s not perfect yet, as it hesitates when the throttle is pressed, but it’s a big improvement. Unplugging the IACV with the new injectors idles at around 800rpm, even with the IACV screw tightened fully. But this is probably due to tune.
    • I wanted to try and preserve the front bumper as long as possible, they're not cheap and are made to order in Japan. Taking inspiration from my previous K11 Micra build where I made an undertray for the Impul bumper, I did the same for this BN Sports bumper but a little slimmed down.  This time round I only made a 'skid plate' (if that's the correct wording/term) for just the bumper surface area, the Micra version covered the gap like an undertray. Starting off with a sheet of mild steel approx. 0.9mm thick 4ft x 2ft in size. I traced around the bumper, cut it out and cleaned the edges. Luckily I was able to get two halves from one piece of metal In the video I installed it as is, but I've since then I've removed it to spray and add a rubber edging trim. The rubber trim is suitable for 1-2mm and it's a really nice tight fit. The bolts had to be loosened due to the plates being too tight against the bumper, the trim wouldn't push on I used some stainless M6 flat headed bolts for a flusher finish (rather than hex heads poking down), I believe this style fastener is used for furniture too incase you struggle to source some. The corner's are a little wider, but this may be an advantage incase I get close to bumping it  The front grill got some attention, finally getting round to repairing it. Upon removal one fixing pulled itself out of the plastic frame, one side is M8 that fixes inside of the frame, where as the other side is M5. Not knowing I could get replacements, I cut down an M8 bolt, threaded it inside the frame along with a decent amount of JB Weld.  The mesh was replaced to match the bumper. One hole on the bonnet/hood had to be drilled out to 8mm to accommodate the new stud, once the glue had set it could be refitted. I think the reason the grill was double meshed was to hide the horn/bonnet latch (which makes sense) but I much prefer it matching the bumper Bumper refitted and it's looking much better IMO The Youtube video can be seen here: https://www.youtube.com/watch?v=bVZP35io9MA
×
×
  • Create New...