Jump to content
SAU Community

Recommended Posts

Pretty much as per title. I have to do a timing belt / water pump replacement so I'm trying to figure out the hurdles before I get to them. What are some ways of preventing the crank from turning while loosening or tightening the crank bolt with an auto gearbox? Maybe jamming something into the starter ring gear?

On 4/15/2023 at 9:39 AM, Ben C34 said:

Having said that I have done it with a screw driver on my own but that was on engine stand.in car would be more challenging.

Just double checking how you're locking (and accessing) the flex plate with the engine+trans in the car? Is that using a screwdriver in a vent/breather port directly under the bell housing?

Starter motor out.

On 4/18/2023 at 9:14 AM, zoomzoom said:

Just double checking how you're locking (and accessing) the flex plate with the engine+trans in the car? Is that using a screwdriver in a vent/breather port directly under the bell housing?

 

  • Like 1
  • 2 weeks later...
2 hours ago, zoomzoom said:

I'll probably tackle this over the weekend. The manual says to remove the radiator, do you guys bother with that?

Yes, if not you'll have a hard time trying to remove the balancer.

Not saying it's impossible but you'll be swearing less, and not damaging your radiator in the process.

Also probably good time to inspect the radiator and replace if required.

I do not enjoy removing the Stagea starter motor or any if I can help it. I constructed these locking bars that attach to the front pulley. Only the M6 extractor bolts hold it in location, use high tensile bolts nipped up tight. I can get up to specified torque on pulley bolt with out the locker self destructing or bolts breaking. I've also used a piece of pipe about 30mm OD with some M10 bolts welded on, these engaged into the  lugs that exist on inner of the Stagea pulley. Not so for my RB20E R33, hasn't got those afore mentioned lugs. That is the crustier looking of the 2 items in photo, bit tighter fit in there on that one. The one with the ring is Stagea and I assume other RB25's.

 

plz8gd.jpg

  • Like 3

Yep, just got the radiator out and I think I'll make a tool to hold the pulley. Forget taking the starter out LOL

Funny that even the Nissan manual specifies a ring gear locking tool that requires taking the starter out.

Feeling a little nervous about those M6 threaded holes. The puller that I have only comes with some imperial bolts and they're all like M10 or M12 equivalent in size.

  • Like 1

Here's the tool I came up with if anyone needs some ideas on making their own. This is using the scrap I had lying around, just happened to have an ideal sized piece of steel pipe. The "teeth" are bits of M12 threaded rod, (obviously unthreaded would be fine too), and spaced out at 120 degrees. Just got the bolt loosened by myself, tightening shouldn't be too much of a hassle now either. 

balancertool.jpg

  • Like 1

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Maf is a question mark but TPS  I have set at 0.47, the fact that I’m getting proper voltage range out of it with the key on leads me to believe it’s functioning properly. I’m getting proper voltages on basically everything. I still need to look up voltage ranges for z32 maf and test that 
    • Honestly no not at all, but it’s a very basic tune, it’s stock injectors q45 tps and z32 maf. Other than that it’s a completely stock base map. The file is from nistune and from my understanding if it was tune related I would be able to unplug maf and tps and it would still start even if it was a really shitty start. I have tried starting it with coolant temp, maf, and tps unplugged none of those 3 togethor or individually changes anything 
    • 🏆 Skyline Supremacy Meets Mount Panorama Magic 🏆 Join SAU NSW as we take the long way to Bathurst, the home of GTR greatness. Saturday 30th August 2025 7:00AM Meeting Hanna Park North Richmond 7:30AM Departure Cruise Via Bells of Line Road 9:00AM Arrival to Stop 1: Golden Poplars Meadow Flat 9:45AM Arrival to Final Destination: Mount Panorama Motor Racing Circuit Meet Location: Hanna Park North Richmond Stop 1: Golden Poplars Meadow Flat Final Destination: Mount Panorama Motor Racing Circuit   *Disclaimer* There will be a lead and follow car so no one should get lost. If you would like to attend or bring others along please put your name down and a +1 as numbers will be needed prior! This is NOT a race and we will all be adhering to all road rules. If this is what you want please come to one of our many track days. This is an official SAU:NSW event and will be run under a CAMS permit. One of the things that really sets our club apart is our commitment to being true enthusiasts. When on normal roads we strive to maintain good relations with the authorities as well as the public in general. When attending one of Skylines Australia NSW events please try to: • Be aware of surrounding environment and act accordingly. • Drive courteously on the state’s roads as a true enthusiast should. • Understand how important it is to maintain the good name of SAU NSW and thus, treat others accordingly. • Any misbehavior will not be tolerated and you will be asked to leave.
    • What does it look like with highway driving? And yes, I had a similar thought as Duncan. It looks quite similar in my Stagea and I have made myself accept it as normal. Might have to look into it some day   Highway gets as low as 10l/100km on my end so I'm not as worried about it being a mechanical issue. More likely just the tune on the haltech.
    • While I was waiting for the new parts to come in for the charge pipe and radiator I decided to do some turbo modification. The drive pressure (exhaust backpressure) was a lot higher that I thought it should be. For 32lbs of boost drive was 55lbs. The turbine housing is a 1.10AR and my turbo builder has suggested to go to a 1.25AR. To test if a larger AR would do anything to reduce drive pressure AND not spend any money I decided to hog out the divider in my current housing. I removed it from the inlet and the whole way through the housing.  After reassembly and testing it doesn't look like this modification did anything for reducing drive pressure or requiring more fuel (making more power). Oh well, it was worth a shot. We'll get some data at the track if it makes it past the 60ft. I also machined a $7 shift knob off Amazon to fit my Stillway shifter since I didn't like the Stillway shift knob. Next on the list was the radiator replacement and fabrication of a new intercooler tube that had no silicon coupler. No pictures of this - I was short on time each night after work to get this done and didn't stop to take pictures.  Next was to get the clutch disks out and replaced. Previously when installing the dogbox I had ordered a set of the same sintered iron disks I had been running because I switched to the 26-spline input shaft. I thought it was odd that they didn't have any markings or brand name on them like all my old disks had but installed them anyway. At the track I could not get the clutch to lock up using my normal strategies. After two track nights I reached out to the clutch manufacturer and ask their thoughts. They said they had to switch the material out because they were having trouble getting the original material and that this new material would not take to being slipped very well.  So out with the first set of 26-spline disks and in with the correct material 26-spline disks. While I had the trans out I added an inspection/service hole. I've wanted one of these for a while. Now I can have a look at things and change the front cover shimming when needed (clutch wear). I hustled and got the clutch change done in a few hours on a Saturday. Hopped in the car and drove home. On the way home I did a 1-3 pull. When shifting from 2nd to 3rd the core plug in the back of the cylinder head popped out and dumped all the coolant. Thankfully I was only 30 seconds from home and coasted it there. Datalog showed nothing unusual and 2.5psi of coolant pressure. That plug has been in there since 1992 but I guess it worked its way out. Pulled the trans AGAIN and replaced the plug, JB welded it in, and made a brace. Also deleted the head drain I had added in during the bearing issue fiasco.  I am currently changing my boost control plumbing to make it cleaner. After that is done I'll make another attempt at getting past the 60.
×
×
  • Create New...