Jump to content
SAU Community

Recommended Posts

Another EFR faluire on EvolutionM forum. Im feeling sorry for the guys that've been waiting for over a year for there turbo to have this in the back of there mind - When i actually get my turbo will it fail. :(

I can say the car is stinking fast. First two sessions of the shake down run were great. Went out for the third session, hit the back straight and see a m3 passing me while at WOT. I'm thinking wait how is that even possible (Nobody could even come close to my backstraight speed.)Look down.... 0 boost and a supercharger like whine. Limped it in to see if it was any easy fix.

Luckliy I had the guys from RRE down doing track support so they checked and found no boost leaks and from the intake side it looks like the wheel started digging in to the inside of the housing. It SO hard to see. Running the car, There is a heavy metalic like whine, and with the intake off and putting your hand over the intake side it definently sucks... no leaks everything bulges like it should. The one interesting thing is that when you stop the car... the wheel just stops instantly... typically I was told on a BB turbo the wheel keeps spining.. this just comes to an abrudt stop.

So the car is headed back down to RRE for the turbo to be removed and inspected... But if it was damaged from the original issue, I'm wondering if that may have been part less then stellar results? I don't really know... but I'm trying my hardest to get a solution together before Tuesday.

So, the turbo is off and as far as RRE can tell the bearings are fine. The turbo does not spin because the shaft is bent. That is making it bind on the bearings. One sise of the compressor wheel has relatively undamaged blades. They do not contact the housing. On the opposite side of the wheel the blades are all ground away. We are pretty sure that it wasn't caused by the prior motor’s death.

To be continued:

Perhaps having such a distance between the bearing races isn't such a good idea then? - Wondering if the heat trapped in the housing is causing warping.

"the car is headed back down to RRE for the turbo to be removed and inspected... But if it was damaged from the original issue, I'm wondering if that may have been part less then stellar results? I don't really know... but I'm trying my hardest to get a solution together before Tuesday. So, the turbo is off and as far as RRE can tell the bearings are fine. The turbo does not spin because the shaft is bent. That is making it bind on the bearings. One sise of the compressor wheel has relatively undamaged blades. They do not contact the housing. On the opposite side of the wheel the blades are all ground away. We are pretty sure that it wasn't caused by the prior motor’s death"

ryan, i have spoken with this owner/driver many times over the last few days.. he has gone through (3) longblocks in 5 months. of course he had no filter in the oil feed line, so it seems possible the turbo might have received oil with pieces of oilpump/thrust bearing/piston fragments in it. FWIW on his brand new fresh motor he only got (1) lap in before the engine grenaded, and it was still fast enough to get him 4th fastest overall. The turbo is still good per his reports, we will get this turbo to BW for analysis - its possible the bent shaft assumption is incorrect and we will find metallic pieces inside of his bearing housing..

It's been an unfortunate series of events to be sure. Had BorgWarner known they were going to run into the production woes from their vendors they certainly would not have launched the product. Fact is, most turbos are holding up just fine. They have determined the culprit of those that have failed and all have derived from one vendor, and the problem only arose AFTER they were mass producing them. We have several that are in use now, taking plenty of abuse and no signs of failure on the horizon. I can say that the turbos we are getting now are solid, but very sparse. It will be another 7-8 months before these turbos are sitting on my shelf, in inventory, waiting for new orders. We see a lot of upside to these turbos, A LOT. It's just been overshadowed by production speed bump after speed bump.

completely agree.

Ominious.... hope this means the blue beasts heart will be getting a new friends soon:)

Yes...It's been on life support for almost a year :wacko:

I will have to wait for the manifold to be finished, as it has just been tacked at the moment to check for fitment, as the BW EFR is a bit different in shape, Then I'll get the manifold and the EFR's exhaust housing HPC coated, and probably the front pipe too.

....Oh and I have a RacePak IQ3 dash coming for it too....:banana:

Well.............

The Mythical White Elephant arrived today!! 9.5mths, It's been longer than making babies!

Serial number #13.....Hope it's lucky for me!

Thanks again to the guys at Full-Race (Geoff,Raffi,Brett,Aaron) for putting up with my constant emails, Just got to wait for the manifold to be finished, and some pipework to be built....Then it's tuning time!

837492IWG.jpg

Well.............

The Mythical White Elephant arrived today!! 9.5mths, It's been longer than making babies!

Serial number #13.....Hope it's lucky for me!

Thanks again to the guys at Full-Race (Geoff,Raffi,Brett,Aaron) for putting up with my constant emails, Just got to wait for the manifold to be finished, and some pipework to be built....Then it's tuning time!

837492IWG.jpg

No worries mate. Good Onya! (that's about all I know)

Awesome Chris, hope all goes well for you - glad its at least finally here :) So what boost level are you tuning for again? Pump gas?

I will only be running 98 pump gas, So will depend on what the tuner manages to get out of it....Hopefully Lots!

I will change to E85 when it becomes available at the pump.

....Oh and the RacePak IQ3 digital dash turned up today! It's like Christmas!:cheers:

Guest
This topic is now closed to further replies.



  • Similar Content

  • Latest Posts

    • Oh, also, forgot to add these photos I believe.
    • Thought i'd update on this. I was able to get in contact with Craig Lieberman and later on Darryl Alison (owner of Kaizo Industries). Darryl was able to help me verify that my car was in fact one of theirs and is helping me find more info on mine !
    • There's restrictor pills in the stock boost control hoses. That's how they set the amount that was bled off and hence the "high" boost setting. The usual mod in the day was to remove it and send the "high" boost setting up to about 14 psi.
    • Thanks Duncan, that's the best info I've read. Furthermore after learning about the PCM programming side controlling the factory boost solenoid, the purpose of the solenoid is to "bleed" boost when pin 25 is earthed, thus allowing spring pressure in the wastegate actuator to overcome diaphragm boost pressure, thus closing or reducing the position of the wastegate flap creating more boost as the turbo is able to spin faster. It's pretty cool to see a designated Pill to do exactly this, would have liked to have seen it with a tiny filter over the end for those moments in vacuum.  The constant bleed pill has now been removed completely from the system and solenoid boost control has been restored once again.   Case closed 😂
    • The wideband reading is meaningless if it's not running. Why are you using shitty old sidefeeds on any engine, let alone a Neo? What manifold and fuel rail are you using to achieve that? Beyond that, can't help you with AEM stuff as I've never been their ECU/CAS combo.
×
×
  • Create New...