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A bit more progress before the end of the year. Manifold fully welded and wastegate added. It didn't quite fit where I initially thought it would but I made something work. The hot spots on the manifold are not from welding (not that my welds are fantastic!). They are from using the torches to move the runners back where they needed to be after welding.

Manifold is now done! Fits with PS, AC, ABS, and no cutting the hood. What a chore. Huge props to those that do this all day everyday. This is only my second manifold and my first with a true collector. I wish I did this more often so I could get better.

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For the charge pipe I wanted to go through the factory hole and fill in the one I made for the first turbo setup. Cut the v-band off the comp housing and tacked on a Plazmaman clamp. It's tight between the housing and the AC lines so I had to cut about 1/4" off each clamp flange and even with a donut it barely clears. I'll do another clamp flush with the factory hole so the entire pipe can come out and it's not in the way when working on the car. Second section of the donut is just held up for reference; not a final piece.

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  • Like 3

Chipping away at it some more. Got the cold side piping finished. I am doing better at aluminum welding and getting more consistent with adding filler. I don't do it often enough to perfect it but progress is progress.

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Started on the downpipe as well. Had to use stainless this time because there is no aluminum available anywhere thanks to good old Joe. Let's go Brandon! 

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Exhaust is on the car again and I'll be connecting it to the downpipe and making the wastegate dump next.

  • Like 1

Turbo system is complete! Downpipe is connected to the exhaust and wastegate dump made. Unfortunately I made a silly mistake and did not bolt up the AC pump lower bolts, just the top bolts. It was not rotated counterclockwise all the way and with the AC lines already bent as much as possible and clearing by a couple mm, they now do not clear with the ump bolted up correctly. Downside of doing things after a long day and trying to hustle I guess. Going to have to remake the top section of intercooler piping.

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This is always the hardest part for me; make two pipes meet in the middle at the same angle and along the same line. Seems to take me a lot of time. Does it take everyone else that much time or am I doing it wrong?

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Also converting to DBW with a 2014+ Hemi Challenger throttle body. Got an IO box for Christmas! We have lots of take-offs from customer cars and the bolt pattern is almost identical to Plazmaman's cable throttle. Cut the throttle and clamp down to match the dimensions of the cable throttle so can switch back if needed with no fabrication. Also makes the conversion easier. Got a 350z pedal from a yard for $25 so I'll try to use that. Apparently it's pretty close to bolt on.
 
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  • Like 1
On 1/16/2022 at 12:14 AM, soviet_merlin said:

If I may ask, with what and how are you taking your photos? They look great! Super crisp and the lighting and details are on point.

Thank you. It's just my phone. Samsung Galaxy S7. We have really bright lights in the shop which is probably why they're crisp. For engine bay shots I use a stick light otherwise they're really blurry.

On 1/16/2022 at 12:21 AM, SRS13 said:

Great work! That turbo is massive! 

Thanks! 

On 1/16/2022 at 12:58 AM, 30ed32 said:

Looks good man, I have the same issue with making pipes up.. just finished most the piping on my build and it's made me want to take a huge break from doing it anytime again.

I feel you there. Very tedious and you can't cut corners on fitment or it'll bite you later. 

  • Thanks 1

Hot side piping chopped up and remade to give lots of AC line clearance. This one really fought me. I already mentioned I seem to struggle with making too tubes meet in the middle. This was even harder in the very short distance between the comp outlet and bulkhead.

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  • 1 month later...

Been a while but I finally got some time to start plucking away at this thing after hours.

Made up a reluctor pickup for the driveshaft speed sensor. Not because it needed it but because I thought of a way to do it and wanted to. 3D printed prototype pictured.

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Then I started on an oil filter relocation. I wanted a larger filter, a common filter, and placed in a spot that didn't get everywhere during changes and, if possible, let me keep the oil drain pain in the same spot when draining the sump. This is a rough draft. We'll see how it goes.

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Next was to strip the bay (not the entire front clip, no time for that) and paint. I also had to fill in the hole I made a few years ago for the turbo outlet. New metal welded in, filler to smooth on the top and bottom. Cleaned, smoothed, and prepped the bay for paint.

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Painted! I'm not a professional and it's not perfect but I think it came out very well for my time input and skill level. 

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Starting reassembly. 

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Edited by OST Micah
  • Like 3
  • 2 weeks later...

Got a bit more assembled. Brake lines are installed. Going to either remake the one or straighten and rebend. It has a goofy bump by the firewall from someone removing these and reinstalled before me. Bugs my OCD but I needed the lines in so no fluid leaked on the paint after I installed the master and ABS pump. All new hardware being used. New brake line clips as well. I'll clean the reservoirs another day.

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Rerouted the body harness in this area. Didn't want to see anything but the turbo parts here.

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  • Like 3

Found some old pictures of what the original brake line routing should look like. Removed the lower two lines, rebent them, and covered some of the nicks in one of the lines with heat shrink. Did the other line to match. So much better!

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Pistons came back from getting the skirts coated and the tops coated. Motor is going to finally start going together!

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  • Like 2
  • 1 month later...

Well the shortblock STILL isn't done. Starting to get a bit impatient. Apparently it's being machined now but that's been the case for a week or two.

In the meantime my cam covers and other parts came back from powder coating. Everything is looks fantastic. Really a shame they're going to get beat up eventually but I'm going to try the best I can to keep them nice. Lots of other parts got coated but I only unwrapped these. Laid my shop's ornament cover on the valley cover and sat my freshly painted CAS on the timing cover. Going to look mint!

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  • Like 2
  • 1 month later...

So after 6+ months of waiting for my motor I threw in the towel. The machine shop did my motor two years ago so I wanted them to do it again and look it over to check for any damage/condition of the parts. They obviously did a good job last time as it held up great. This time however progress was just so slow and ground to a halt when they could not line hone the block due to not having the correct mandrel.

Last week I drove down, picked up my parts, inspected everything, made some corrections, crated everything up, and shipped it to our Hemi engine builder. He bumped me to the front of the line and the day the block arrived it was on the line hone. The next day it was getting the cylinders bored and honed. He measured the rod big ends and mains and bearings will be there Tuesday. What a guy! 

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While he is doing the shortblock, I got to work on the head. It was at the same first machine shop for a crack repair. This did get done and looks to be a good repair. I had them cut the seats and valves as well because there was evidence of valve float and the seats were beat up. Switching to a dual spring to fix this.

Assembled with Supertech dual springs, Supertech guides, Supertech seals (made a tool to get these on), and stock valves. Polished up the buckets on the lathe as well. Then torqued the head to a mock-up block and got the shimming sorted. I'm getting a decent collection of shims now so I only needed to order two. Why torque to a block for shimming? I found that the clearance can change (mostly increase) after torquing. I suspect valve seat distortion.

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Finished up the oil filter relocation.

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Lastly was a new location for the oil drain. Unknowingly, I placed the first drain at the front and on the side. The front wasn't good because in the car the bottom of the oil sump slopes rearward meaning there's probably a quart or so of oil I couldn't drain. On the side was a pain because the oil drains in a long arc and you have to stand there the whole time and keep moving the catch tray as the arc shortens.

Cut a bung down to fit flush with the bottom of the pan. Now welded up in a much more convenient location.

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  • Like 7

It's finally done. What a long road. Time to go back together. So far I've got it out of the crate, inspected, painted, final freeze plugs in, oil pump, windage trays and sump installed, and a couple other smaller bits. Was going to get the head on but got sent the wrong gasket. 

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Deleting the hardlines under the intake but still going to use cabin heat. Turned down this spare cam cover breather for a .004" press fit aided by some loctite. Tapered the first bit to get it to go in nicely.

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Edited by OST Micah
  • Like 2

Hardline for cabin heater finished.

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Factory coolant fitting modified for -10 on the main outlet and the smaller outlet blocked.

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Turbo drain fitting extended. With the new turbo position there is much more room below the turbo and that makes room for this extension. Now getting a wrench on the fitting will be easy since it will be below the comp housing.

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Motor assembly started. One thing I always wanted was access to the tensioner with the damper installed. I feel that Nissan dropped the ball here. Put a hole in the lower cover so I can remove and install the cams more easily in the future because I seem to need to do that a lot. Also switched to a Gates belt. No real need but want to test it out and see if I can reduce some of the changes I implemented to make the factory CAS work.

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All together! Switched to the Outsider Garage billet half moons as well. The cam cover some off all the time and I got tired of piling rtv on the factory ones.

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A photo of how little is under the intake now. Super happy about this! Will make removing the intake easy and no clutter. 

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Cabin heater hose attachment. No clamps! 

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Finally back in the car. Not long now!

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Edited by OST Micah
  • Like 1

Great thinking on some of those convenience changes, we've done a few things for the race car over the years too and it makes a big difference for convenience, speed and frustration. I like the tensioner hole (are you going to put a grommet in there? and the extended turbo drain, they should all be made that way)

As well as your access to the intake, you will find even more helpful is how easy it is to get to the starter from underneath any time you need to take the gearbox or engine out. We don't have a heater any more and have re-routed some other lines, there is so much room there I can get a full size spanner on the starter motor bolts if necessary (although generally I just use a stubby 14)

Thanks, Duncan. I was going to use a Honda tensioner cover because I thought I had one but I can't find it. It has a nice pull tab to remove. I think I will leave a plug out of it as I'm afraid I may accidentally push it through the cover when trying to remove it. I run an undertray on this car so if something gets up into that area of the bay I've got other issues!

Yes, the trans comes out often to check the clutch or change it out. Looking forward to any added speed for that job.

Thank you for the kind words!

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    • Any update on this one? did you manage to get it fixed?    i'm having the same issue with my r34 and i believe its to do with the smart entry (keyless) control module but cant be sure without forking out to get a replacement  
    • So this being my first contribution to the SAU forums, I'd like to present and show how I had to solve probably one of the most annoying fixes on any car I've owned: replacing a speedometer (or "speedo") sensor on my newly acquired Series 1 Stagea 260RS Autech Version. I'm simply documenting how I went about to fix this issue, and as I understand it is relatively rare to happen to this generation of cars, it is a gigantic PITA so I hope this helps serve as reference to anyone else who may encounter this issue. NOTE: Although I say this is meant for the 260RS, because the gearbox/drivetrain is shared with the R33 GTR with the 5-speed manual, the application should be exactly the same. Background So after driving my new-to-me Stagea for about 1500km, one night while driving home the speedometer and odometer suddenly stopped working. No clunking noise, no indication something was broken, the speedometer would just stop reading anything and the odometer stopped going up. This is a huge worry for me, because my car is relatively low mileage (only 45k km when purchased) so although I plan to own the car for a long time, a mismatched odometer reading would be hugely detrimental to resale should the day come to sell the car. Thankfully this only occurred a mile or two from home so it wasn't extremely significant. Also, the OCD part of me would be extremely irked if the numbers that showed on my dash doesn't match the actual ageing of the car. Diagnosing I had been in communication with the well renown GTR shop in the USA, U.P.garage up near University Point in Washington state. After some back and forth they said it could be one of two things: 1) The speedometer sensor that goes into the transfer case is broken 2) The actual cluster has a component that went kaput. They said this is common in older Nissan gauge clusters and that would indicate a rebuild is necessary. 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The signal does NOT go to the ECU first, the wiring goes to the cluster first then the ECU after (or so I'm told).  Problems/Roadblocks I first removed the part from the car on the underside of the transfer case (drain your transfer case fluid/ATF first, guess who found out that the hard way?), and noted the transfer case fluid was EXTREMELY black, most likely never changed on my car. When attempting to turn the gears it felt extremely gritty, as if something was binding the shaft from rotating properly. I got absolutely no voltage reading out of the sensor no matter how fast I turned the shaft. After having to reflow the solder on my AFM sensors based on another SAU guide here, I attempted to disassemble the silicone seal on the back of the sensor to see what happened inside the sensor; turns out, it basically disintegrated itself. Wonderful. Not only had the electrical components destroyed themselves, the magnetic portion on what I thought was on the shaft also chipped and was broken. Solution So solution: find a spare part right? Wrong. Nissan has long discontinued the proper sensor part number 32702-21U19, and it is no longer obtainable either through Nissan NSA or Nissan Japan. I was SOL without proper speed or mileage readings unless I figured out a way to replace this sensor. After tons of Googling and searching on SAU, I found that there IS however a sensor that looks almost exactly like the R33/260RS one: a sensor meant for the R33/R34 GTT and GTS-T with the 5 speed manual. The part number was 25010-21U00, and the body, plug, and shaft all looked exactly the same. The gear was different at the end, but knowing the sensor's gear is held on with a circlip, I figured I could just order the part and swap the gears. Cue me ordering a new part from JustJap down in Kirrawee, NSW, then waiting almost 3 weeks for shipping and customs clearing. The part finally arrives and what did I find? The freaking shaft lengths don't match. $&%* I discussed with Erik how to proceed, and figuring that I basically destroyed the sensor trying to get the shaft out of the damaged sensor from my car. we deemed it too dangerous to try and attempt to swap shafts to the correct length. I had to find a local CNC machinist to help me cut and notch down the shaft. After tons of frantic calling on a Friday afternoon, I managed to get hold of someone and he said he'd be able to do it over half a week. I sent him photos and had him take measurements to match not only the correct length and notch fitment, but also a groove to machine out to hold the retentive circlip. And the end result? *chef's kiss* Perfect. Since I didn't have pliers with me when I picked up the items, I tested the old gear and circlip on. Perfect fit. After that it was simply swapping out the plug bracket to the new sensor, mount it on the transfer case, refill with ATF/Nissan Matic Fluid D, then test out function. Thankfully with the rebuilt cluster and the new sensor, both the speedometer and odometer and now working properly!   And there you have it. About 5-6 weeks of headaches wrapped up in a 15 minute photo essay. As I was told it is rare for sensors of this generation to die so dramatically, but you never know what could go wrong with a 25+ year old car. I HOPE that no one else has to go through this problem like I did, so with my take on a solution I hope it helps others who may encounter this issue in the future. For the TL;DR: 1) Sensor breaks. 2) Find a replacement GTT/GTS-T sensor. 3) Find a CNC machinist to have you cut it down to proper specs. 4) Reinstall then pray to the JDM gods.   Hope this guide/story helps anyone else encountering this problem!
    • So this being my first contribution to the SAU forums, I'd like to present and show how I had to solve probably one of the most annoying fixes on any car I've owned: replacing a speedometer (or "speedo") sensor on my newly acquired Series 1 Stagea 260RS Autech Version. I'm simply documenting how I went about to fix this issue, and as I understand it is relatively rare to happen to this generation of cars, it is a gigantic PITA so I hope this helps serve as reference to anyone else who may encounter this issue. NOTE: Although I say this is meant for the 260RS, because the gearbox/drivetrain is shared with the R33 GTR with the 5-speed manual, the application should be exactly the same. Background So after driving my new-to-me Stagea for about 1500km, one night while driving home the speedometer and odometer suddenly stopped working. No clunking noise, no indication something was broken, the speedometer would just stop reading anything and the odometer stopped going up. This is a huge worry for me, because my car is relatively low mileage (only 45k km when purchased) so although I plan to own the car for a long time, a mismatched odometer reading would be hugely detrimental to resale should the day come to sell the car. Thankfully this only occurred a mile or two from home so it wasn't extremely significant. Also, the OCD part of me would be extremely irked if the numbers that showed on my dash doesn't match the actual ageing of the car. Diagnosing I had been in communication with the well renown GTR shop in the USA, U.P.garage up near University Point in Washington state. After some back and forth they said it could be one of two things: 1) The speedometer sensor that goes into the transfer case is broken 2) The actual cluster has a component that went kaput. They said this is common in older Nissan gauge clusters and that would indicate a rebuild is necessary. As I tried to figure out if it was problem #1, I resolved problem #2 by sending my cluster over to Relentless Motorsports in Dallas, TX, whom is local to me and does cluster and ECU rebuilds. He is a one man operation who meticulously replaces every chip, resistor, capacitor, and electronic component on the PCB's on a wide variety of classic and modern cars. His specialty is Lexus and Toyota, but he came highly recommended by Erik of U.P.garage since he does the rebuilds for them on GTR clusters.  For those that don't know, on R32 and R33 GTR gearboxes, the speedometer sensor is mounted in the transfer case and is purely an analog mini "generator" (opposite of an alternator essentially). Based on the speed the sensor spins it generates an AC sine wave voltage up to 5V, and sends that via two wires up to the cluster which then interprets it via the speedometer dial. The signal does NOT go to the ECU first, the wiring goes to the cluster first then the ECU after (or so I'm told).  Problems/Roadblocks I first removed the part from the car on the underside of the transfer case (drain your transfer case fluid/ATF first, guess who found out that the hard way?), and noted the transfer case fluid was EXTREMELY black, most likely never changed on my car. When attempting to turn the gears it felt extremely gritty, as if shttps://imgur.com/6TQCG3xomething was binding the shaft from rotating properly. After having to reflow the solder on my AFM sensors based on another SAU guide here, I attempted to disassemble the silicone seal on the back of the sensor to see what happened inside the sensor; turns out, it basically disintegrated itself. Wonderful. Not only had the electrical components destroyed themselves, the magnetic portion on what I thought was on the shaft also chipped and was broken. Solution So solution: find a spare part right? Wrong. Nissan has long discontinued the proper sensor part number 32702-21U19, and it is no longer obtainable either through Nissan NSA or Nissan Japan. I was SOL without proper speed or mileage readings unless I figured out a way to replace this sensor. After tons of Googling and searching on SAU, I found that there IS however a sensor that looks almost exactly like the R33/260RS one: a sensor meant for the R33/R34 GTT and GTS-T with the 5 speed manual. The part number was 25010-21U00, and the body, plug, and shaft all looked exactly the same. The gear was different at the end, but knowing the sensor's gear is held on with a circlip, I figured I could just order the part and swap the gears. Cue me ordering a new part from JustJap down in Kirrawee, NSW, then waiting almost 3 weeks for shipping and customs clearing. The part finally arrives and what did I find? The freaking shaft lengths don't match. $&%* I discussed with Erik how to proceed, and figuring that I basically destroyed the sensor trying to get the shaft out of the damaged sensor from my car. we deemed it too dangerous to try and attempt to swap shafts to the correct length. I had to find a local CNC machinist to help me cut and notch down the shaft. After tons of frantic calling on a Friday afternoon, I managed to get hold of someone and he said he'd be able to do it over half a week. I sent him photos and had him take measurements to match not only the correct length and notch fitment, but also a groove to machine out to hold the retentive circlip. And the end result? *chef's kiss* Perfect. Since I didn't have pliers with me when I picked up the items, I tested the old gear and circlip on. Perfect fit. After that it was simply swapping out the plug bracket to the new sensor, mount it on the transfer case, refill with ATF/Nissan Matic Fluid D, then test out function. Thankfully with the rebuilt cluster and the new sensor, both the speedometer and odometer and now working properly!   And there you have it. About 5-6 weeks of headaches wrapped up in a 15 minute photo essay. As I was told it is rare for sensors of this generation to die so dramatically, but you never know what could go wrong with a 25+ year old car. I HOPE that no one else has to go through this problem like I did, so with my take on a solution I hope it helps others who may encounter this issue in the future. For the TL;DR: 1) Sensor breaks. 2) Find a replacement GTT/GTS-T sensor. 3) Find a CNC machinist to have you cut it down to proper specs. 4) Reinstall then pray to the JDM gods.   Hope this guide/story helps anyone else encountering this problem!
    • perhaps i should have mentioned, I plugged the unit in before i handed over to the electronics repair shop to see what damaged had been caused and the unit worked (ac controls, rear demister etc) bar the lights behind the lcd. i would assume that the diode was only to control lighting and didnt harm anything else i got the unit back from the electronics repair shop and all is well (to a point). The lights are back on and ac controls are working. im still paranoid as i beleive the repairer just put in any zener diode he could find and admitted asking chatgpt if its compatible   i do however have another issue... sometimes when i turn the ignition on, the climate control unit now goes through a diagnostics procedure which normally occurs when you disconnect and reconnect but this may be due to the below   to top everything off, and feel free to shoot me as im just about to do it myself anyway, while i was checking the newly repaired board by plugging in the climate control unit bare without the housing, i believe i may have shorted it on the headunit surround. Climate control unit still works but now the keyless entry doesnt work along with the dome light not turning on when you open the door. to add to this tricky situation, when you start the car and remove the key ( i have a turbo timer so car remains on) the keyless entry works. the dome light also works when you switch to the on position. fuses were checked and all ok ive deduced that the short somehow has messed with the smart entry control module as that is what controls the keyless entry and dome light on door opening   you guys wouldnt happen to have any experience with that topic lmao... im only laughing as its all i can do right now my self diagnosed adhd always gets me in a situation as i have no patience and want to get everything done in shortest amount of time as possible often ignoring crucial steps such as disconnecting battery when stuffing around with electronics or even placing a simple rag over the metallic headunit surround when placing a live pcb board on top of it   FML
    • Bit of a pity we don't have good images of the back/front of the PCB ~ that said, I found a YT vid of a teardown to replace dicky clock switches, and got enough of a glimpse to realize this PCB is the front-end to a connected to what I'll call PCBA, and as such this is all digital on this PCB..ergo, battery voltage probably doesn't make an appearance here ; that is, I'd expect them to do something on PCBA wrt power conditioning for the adjustment/display/switch PCB.... ....given what's transpired..ie; some permutation of 12vdc on a 5vdc with or without correct polarity...would explain why the zener said "no" and exploded. The transistor Q5 (M33) is likely to be a digital switching transistor...that is, package has builtin bias resistors to ensure it saturates as soon as base threshold voltage is reached (minimal rise/fall time)....and wrt the question 'what else could've fried?' ....well, I know there's an MCU on this board (display, I/O at a guess), and you hope they isolated it from this scenario...I got my crayons out, it looks a bit like this...   ...not a lot to see, or rather, everything you'd like to see disappears down a via to the other side...base drive for the transistor comes from somewhere else, what this transistor is switching is somewhere else...but the zener circuit is exclusive to all this ~ it's providing a set voltage (current limited by the 1K3 resistor R19)...and disappears somewhere else down the via I marked V out ; if the errant voltage 'jumped' the diode in the millisecond before it exploded, whatever that V out via feeds may have seen a spike... ....I'll just imagine that Q5 was switched off at the time, thus no damage should've been done....but whatever that zener feeds has to be checked... HTH
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