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so this POS now has a oil cooler supplied by old mate mark ( god12a) on here

i also shlaped the quick release steering wheel on it

so now i have a wheel and jenna has a wheel to drive it ( i like a dishy one she likes a flat one)

blead the brakes applied stickers for awesome

jenna washed it and shit as well

post-219-0-45956700-1373518710_thumb.jpeg

I dissapear for a bit and now fatz is f**king moby dick, and talking about making shit reliable.

The times, they are a changing

Least Neil still looks like he should be on the grid of the 1976 James Hardie 1000

well wakefield six hour done

car ran well, usual story of filling the catch can over 6k rpm so that was the rev limit for the day

oil cooler worked a treat with oil temps only getting to 105 degrees

rsr rubber is mega shit

was putting around in the 10.5 range and braking very early, changed the pads and bled the brakes and straight down to 1.09 flat and the was at high 1.08 on sunday

quite happy with that id like a low 1.08 before i put decent rubber on

too 200 litres of e85 down and really probably needed 50 more for the day ( did about 100 laps over the two days)

team fat skylines came third last but we all had a ball

pics time

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the whale

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piss bins car

3_zps1813c26d.jpg

Goulburn tradition

4_zps408430d3.jpg

what a crack team

5_zps6d1e3e43.jpg

pissed down at the start

6_zps5efc65c2.jpg

7_zps31ca2cf7.jpg

8_zps66654315.jpg

welllllll!

so i did a cold compression test last night

150,150,150,140,128,150

i will do a hot compression test as well over the weekend

looks like i may have found my excessive blow bye issue

turns out that a 16 year old engine doesnt like thrashing over the last 4 track days

so what am i to do? ( epic 4 year build thread like most people here?, normal skyline owners would put it up for sale and not mention it to the poor new owner)

me ill add a extra catch can and some mines baffels and take her back to the track

i must say i was hoping this thread would go for years prior to unwrapping teh backup motor, but it look like that will be happening sooner, mind you ill back the revs off and boost off and it could go for a another year( touch wood)

welllllll!

so i did a cold compression test last night

150,150,150,140,128,150

i will do a hot compression test as well over the weekend

looks like i may have found my excessive blow bye issue

turns out that a 16 year old engine doesnt like thrashing over the last 4 track days

so what am i to do? ( epic 4 year build thread like most people here?, normal skyline owners would put it up for sale and not mention it to the poor new owner)

me ill add a extra catch can and some mines baffels and take her back to the track

i must say i was hoping this thread would go for years prior to unwrapping teh backup motor, but it look like that will be happening sooner, mind you ill back the revs off and boost off and it could go for a another year( touch wood)

Inspired by your research the other day I ended up getting one of these... http://turbowerx.com/Scavenge_Pumps/page1/page1.html

I'll let you know how it goes, going to run it from my catch can around the back of the block and into rear turbo drain. Switch it on about 5000rpm or so. I'll let you know how it goes :)

Wonder why you have fooked the motor? Were you always running E85 or were you using 98RON?

98 for three track day( running average)

E85 for the last one (running very well)

Will be interesting at the next track day to see if the catch can mods work.

I think the only way to keep this pos running well would be to run the oil scavenge as well as the upgraded catch can setup( at its current compression situation)

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