Jump to content
SAU Community

Recommended Posts

  • 2 weeks later...

To tight to buy a new thermostat housing, so simple, I just made one.

 

IMGP3319_resize_zpsyhpaygdg.jpg

 

IMGP3320_resize_zpsovcmgtcb.jpg

 

Also started to extend the top timing belt cover, it had a crack and a piece missing so it was easier to cut the small section out and replace it at the same time.

 

IMGP3322_resize_zpsv8sqlae0.jpg

 

IMGP3323_resize_zpse057work.jpg

 

IMGP3324_resize_zps26xsap4w.jpg

 

IMGP3327_resize_zpsxpzrkvdm.jpg

  • Like 4
  • 2 months later...

Bit of an update, had a small side project for my boss in Melbourne which turned into a bigger project fixing a previous dodgy repair.

 

IMGP3335_zpsr0c0x1w6.jpg

 

The front section of the rail had been repaired before and been fully sealed up not letting any water that happened to get into the rail escape out the bottom.

 

So the rail rusted from the inside out. 

 

IMGP3337_zpsuxrq9gl3.jpg

 

IMGP3338_zpsmnt2am93.jpg

 

When i cut the outside of the rail out i found it had a welded inside of the rail on the inner.

 

IMGP3341_zpshcrkl0ti.jpg

 

After removing the inner plate i was left with this.

 

IMGP3343_zps5us4waln.jpg

 

From this point I cut the inner out and fabricated a new rail and repaired a few more rust patches.

 

Sorry no photos of the finished repairs I was to keen to get this thing out of my shed.

 

Now back to the hatch, not a great deal has has happened except planning and procrastinating but I have started seam welding some of the body.

 

IMGP3350_zpsanvatsrj.jpg

 

 

  • Like 3
  • 3 weeks later...

Got a few more things done.

 

Checked it see if the power steering lines could be reused, will need to modify the hose on the power steering pump.

 

IMGP3351_resize_zpsjeniyal0.jpg

 

Replaced the front wheel bearings.

 

IMGP3363_resize_zpslakj8jxp.jpg

 

IMGP3377_resize_zpsgnuyqhge.jpg

 

IMGP3378_resize_zps9ztogzfx.jpg

 

And started getting some of the suspension parts striped for painting.

 

IMGP3379_resize_zps27cme82b.jpg

 

 

  • Like 2
  • 3 weeks later...

Well today I thought I would touch base with the engineer to see at what stage he wanted to see the car next only to be told by the receptionist that 

 

he has recently lost his VASS accreditation. Looks like the $1000 I have spent with him is a total loss and I don't even know if he has any documentation 

 

he can give me to pass onto a new engineer when I find one. So now the search for a new engineer start and hopefully find one that is happy with the 

 

build so far.   :banghead:

Edited by turbo76lx

Shit mate, that's no good. If your current (now ex!) engineer doesn't recommend someone for you PM me and I'll track down the details of another engineer who comes to Shepp fairly regularly. We sold him a Benz not long ago and I spoke to him about engineering my car with the RB30 in it. He was pretty confident he'd get it through whereas others just instantly shit canned the idea so he's at least open to a little lateral interpretation of the VSI regs!

  • 2 weeks later...

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • This is where I share pain with you, @Duncan. The move to change so many cooling system pieces to plastic is a killer! Plastic end tanks and a few plastic hose flanges on my car's fail after so little time.  Curious about the need for a bigger rad, is that just for long sessions in the summer or because the car generally needs more cooling?
    • So, that is it! It is a pretty expensive process with the ATF costing 50-100 per 5 litres, and a mechanic will probably charge plenty because they don't want to do it. Still, considering how dirty my fluid was at 120,000klm I think it would be worth doing more like every 80,000 to keep the trans happy, they are very expensive to replace. The job is not that hard if you have the specialist tools so you can save a bit of money and do it yourself!
    • OK, onto filling. So I don't really have any pics, but will describe the process as best I can. The USDM workshop manual also covers it from TM-285 onwards. First, make sure the drain plug (17mm) is snug. Not too tight yet because it is coming off again. Note it does have a copper washer that you could replace or anneal (heat up with a blow torch) to seal nicely. Remove the fill plug, which has an inhex (I think it was 6mm but didn't check). Then, screw in the fill fitting, making sure it has a suitable o-ring (mine came without but I think it is meant to be supplied). It is important that you only screw it in hand tight. I didn't get a good pic of it, but the fill plug leads to a tube about 70mm long inside the transmission. This sets the factory level for fluid in the trans (above the join line for the pan!) and will take about 3l to fill. You then need to connect your fluid pump to the fitting via a hose, and pump in whatever amount of fluid you removed (maybe 3 litres, in my case 7 litres). If you put in more than 3l, it will spill out when you remove the fitting, so do quickly and with a drain pan underneath. Once you have pumped in the required amount of clean ATF, you start the engine and run it for 3 minutes to let the fluid circulate. Don't run it longer and if possible check the fluid temp is under 40oC (Ecutek shows Auto Trans Fluid temp now, or you could use an infrared temp gun on the bottom of the pan). The manual stresses the bit about fluid temperature because it expands when hot an might result in an underfil. So from here, the factory manual says to do the "spill and fill" again, and I did. That is, put an oil pan under the drain plug and undo it with a 17mm spanner, then watch your expensive fluid fall back out again, you should get about 3 litres.  Then, put the drain plug back in, pump 3 litres back in through the fill plug with the fitting and pump, disconnect the fill fitting and replace the fill plug, start the car and run for another 3 minutes (making sure the temp is still under 40oC). The manual then asks for a 3rd "spill and fill" just like above. I also did that and so had put 13l in by now.  This time they want you to keep the engine running and run the transmission through R and D (I hope the wheels are still off the ground!) for a while, and allow the trans temp to get to 40oC, then engine off. Finally, back under the car and undo the fill plug to let the overfill drain out; it will stop running when fluid is at the top of the levelling tube. According to the factory, that is job done! Post that, I reconnected the fill fitting and pumped in an extra 0.5l. AMS says 1.5l overfill is safe, but I started with less to see how it goes, I will add another 1.0 litres later if I'm still not happy with the hot shifts.
    • OK, so regardless of whether you did Step 1 - Spill Step 2 - Trans pan removal Step 3 - TCM removal we are on to the clean and refill. First, have a good look at the oil pan. While you might see dirty oil and some carbony build up (I did), what you don't want to see is any metal particles on the magnets, or sparkles in the oil (thankfully not). Give it all a good clean, particularly the magnets, and put the new gasket on if you have one (or, just cross your fingers) Replacement of the Valve body (if you removed it) is the "reverse of assembly". Thread the electrical socket back up through the trans case, hold the valve body up and put in the bolts you removed, with the correct lengths in the correct locations Torque for the bolts in 8Nm only so I hope you have that torque wrench handy (it feels really loose). Plug the output speed sensor back in and clip the wiring into the 2 clips, replace the spring clip on the TCM socket and plug it back into the car loom. For the pan, the workshop manual states the following order: Again, the torque is 8Nm only.
    • One other thing to mention from my car before we reassemble and refill. Per that earlier diagram,   There should be 2x B length (40mm) and 6x C length (54mm). So I had incorrectly removed one extra bolt, which I assume was 40mm, but even so I have 4x B and 5x C.  Either, the factory made an assembly error (very unlikely), or someone had been in there before me. I vote for the latter because the TCM part number doesn't match my build date, I suspect the TCM was changed under warranty. This indeed led to much unbolting, rebolting, checking, measuring and swearing under the car.... In the end I left out 1x B bolt and put in a 54mm M6 bolt I already had to make sure it was all correct
×
×
  • Create New...