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r32-25t

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Everything posted by r32-25t

  1. It’s what pretty much everyone does and is also what everyone has been telling you to do. most people run a new set of wires from the ecu
  2. Just do it properly and put the valve on the other side of the engine bay, block the 2 red hoses off, take the boost source from where you are currently taking it under the plenum then using a t-piece connect port 2 to both of the waste gates and leave port 1 open
  3. The os88 has a habit of breaking the input shaft and it’s generally a 6 month wait to get a new one. They also very agricultural compared to the newer boxes as they were designed in the 90s and haven’t changed much since then
  4. number one port is currently plumbed into the bottom of the plenum which is a boost source
  5. That’s not even close to what people have been telling you to do!!
  6. The stagea has the same tank as the r32 gtr and out of my r32 gtr I used to get around 400-450kms to a tank with standard petrol (gas) and now it’s on e85 is more like 300-320 to a tank
  7. But JDM parts YouTube fame yo
  8. It’s a bit of a weird one considering water isn’t supposed to touch the sleeves in these blocks. I’m just glad they found an issue rather then not finding anything and guessing the head gasket just didn’t seal
  9. Block was tested this week and turns out it’s leaking from number 6 sleeve, been told they’ll strip it down to a bare block and and pull the sleeve out to find out why it’s leaking
  10. Sad 😞 my engine had to come back out and all it had done was Idled 4 or 5 times
  11. The dr30?
  12. Agree, Mondays can eat shit
  13. I’m sure there are cars that don’t follow that rule, then again they may have had the front wiped off and had the front guards replaced
  14. Blue are on na cars and red are on turbo ones, the gold were part of an option pack with gold badges
  15. Pull Belt off and turn pump with a drill, put belt back on and start car
  16. They’re blind holes and they’re designed with a shank on the bottom of the stud to bottom out and make sure the length is correct
  17. So they took the head off pretty much straight away and pressure tested it both hot and cold and confirmed the head is fine, they are going to pressure test the block but don’t believe there is a way that can cause the issue.
  18. The oil splashing on them will probably create a bigger weight discrepancy then you’re trying to shave off
  19. It’s usually the torque from the engine pulls them apart, most people just fit a solid one to the passenger side
  20. An advantage of grub screwing is you can run the pipe cleaners through all the oil galleries
  21. Pull the wire out of the master cylinder and see if it stays off, if so then the sensor is faulty
  22. Looking at it myself there’s only really one thing I believe it could be, I’m just not going to say anything until the machine shop looks at it and gives their opinion
  23. Yeah to the engine shop to find the issue, i supplied the block brand new in a box and let them machine and build it
  24. Sorry it’s taken so long but I haven’t been well (not sure why) Unfortunately it’s not a throw off, while the car was at the fabricator/tuner they noticed an oil leak and said they didn’t want to tune the car until it was rectified. the car was towed to the fab shop that did the sump and put on his hoist and we looked for the leak, we determined where the leak was and what had caused it and the engine needed to come out because he didn’t want to weld it on the car. He then offered me his hoist to pull the engine out which I was very grateful for and the next day arrived tools in hand and remove the engine and gearbox in about 4 hours!! Now, while draining the oil tank I noticed what came out first appeared to be coolant then followed by oil, I undid all the scavenge lines and we noticed there was a milky layer coming out of them as well 😞 once the engine was out and and the sump removed there was clear evidence of coolant in the oil/sump, so the engine was put into my Ute and I took it home to take the manifolds and etc off and dropped to the engine shop. The car was then towed out of the workshop to get it out of the fabricators way
  25. well things took a turn for the worse and then got even worse again. Will update with full story soon
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