Jump to content
SAU Community

Recommended Posts

On 10/12/2022 at 12:50 AM, Kinkstaah said:

I am sorry, antilag is not part of the 'Sensible 300kw package'.

Shhh, lol. 

On 10/12/2022 at 6:27 AM, Dose Pipe Sutututu said:

Lol it is, just too much retard in Bill's case.

Never go full retard, only half retard.

(Single digit ignition retard numbers for next turbo lol).

Yes I'm partially retarded but commo bogan turned me into full retard momentarily. 

I think i had set it at - 40 to 45° 

The other thing I didn't mention is the 2 step part (rev limiter) which is set at 3500rpm didn't activate. So she revved pretty good. Probably my dodgy wiring. 

It is also possible the turbo bearings where on their way out. Anyway turbo is off to hypergear. We'll see what Tao says. 

  • Haha 2
1 hour ago, admS15 said:

Shhh, lol. 

Yes I'm partially retarded but commo bogan turned me into full retard momentarily. 

I think i had set it at - 40 to 45° 

The other thing I didn't mention is the 2 step part (rev limiter) which is set at 3500rpm didn't activate. So she revved pretty good. Probably my dodgy wiring. 

It is also possible the turbo bearings where on their way out. Anyway turbo is off to hypergear. We'll see what Tao says. 

Did you tune this yourself, testing at say 0 degrees, then -5, -10, -20, -30 constantly screaming more bangs! and laughing maniacally? 

I hope so lol. 

  • Like 2
  • Haha 2
On 10/12/2022 at 9:01 AM, Dose Pipe Sutututu said:

Whoaaaa god level lol..

Sensational bang bangs

The bangs where quite good when the rev limiter was active. I just went and double checked my settings was 10% enrich and 35° retard. Pretty sure with the adaptronic that's not absolute. Eg if base timing is 15° advanced then -35 is 20° retarded. Correct me if I'm wrong sir. 

On 10/12/2022 at 9:43 AM, Murray_Calavera said:

Did you tune this yourself, testing at say 0 degrees, then -5, -10, -20, -30 constantly screaming more bangs! and laughing maniacally? 

I hope so lol. 

Of course I did until my across the road neighbour came over yelling and screaming, had to drive to somewhere secluded to continue. -35 was where I settled and was producing 10psi on the 2 step.

The problem here has been the limiter not activating and the turbo making a shit load more boost and heat than 10 psi would. 

  • Like 1

Anyway turbo was dropped off earlier. Tao had a quick look, bearings are still good and he believes either something went through the engine, like a spark plug tip or some sort of debris. I'm just hoping it's not a bit of piston like in dosepipes. Going to check the plugs and do a comp test when I get a chance. 

 

The other theory is excessive heat produced due to tiny 21u exhaust housing and erm anti lag. I'll know more once it's fully stripped. 

He's trying to convince me to moving to a op6 housing with bb core. At this point I'm still wanting to stay with what I had as I couldn't be bothered with redoing my water lines, oil return and retuning again but I may change my mind. 

19 hours ago, admS15 said:

Pretty sure with the adaptronic that's not absolute. Eg if base timing is 15° advanced then -35 is 20° retarded. Correct me if I'm wrong sir. 

You are correct sir! 

Been a while since I've tuned an Adaptronic!

 

And I hope it's not bits of motor that smashed into your turbo, we know how that ended for me.... 

  • Like 1

Spark plugs removed and inspected, all tips present. Compression test done and still have between 150-160psi across all pots on a cold engine. Pretty happy with that. 

Was panicking at one stage when testing cylinder 5 and it showed 90psi, retested and got the same. Was already calculating cost of rebuild and who to go to but after removing and refitting the gauge it read 150psi consistently. Phew, crisis avoided. Gauge tube mustn't have seated properly. 

Unless hypergear finds bits of motor inside the turbo then I'm confident the engine is still healthy and will put everything back together. 

  • Like 4

Turbo is back. New turbine and fresh bearing pack. Thanks to Tao from @hypergearfor getting it done and back to me in 3 business days. Awesome service.

IMG_20221216_165805.thumb.jpg.f27cc06e5b565c28e37059a60e88851d.jpg

 

Overnight parts from goodstate via ebay plus. Have used them guys a few times for genuine Nissan bits and they always seem to have stock and ship fast. Anyway, had a bit of an oil leak from an aftermarket exhaust side rocker cover gasket. Changed both with genuine + fresh half moons with a dab of threebond while I was there. 

IMG_20221216_165054.thumb.jpg.97fac3857da81242204ef53bf43bf0f4.jpg

 

IMG_20221216_162333.thumb.jpg.d2b220dd977d0a61e439f042e4fb6b02.jpg

Also did a bit of degreasing to clean up the leaky mess. 

Will hopefully fit turbo tomorrow morning and then boost off into the sunset. Antilag switch will most likely see the inside of my garbage bin. 

  • Like 4

Went well this morning. 

 

Home 

 

IMG_20221217_123706.thumb.jpg.e5572383d033368f68d3d1bf6f2a9448.jpg

 

 

IMG_20221217_123726.thumb.jpg.2ab00dbd71be7d82b7a35e5ef1b11a54.jpg

And finished product. Oem, it's stock standard officer. 

IMG_20221217_125119.thumb.jpg.deaf864e14b47a149529a7e9759c2b6a.jpg

 

IMG_20221217_125148.thumb.jpg.fdeb4dc287c404599d59f59195f50bb6.jpg

All back together, filled with fresh nulon coolant. Bleeding not required thanks to the ling long swirl pot/breather. 

Managed to fire her up and check for leaks. Thankfully there where none. Engine sounds happy and the horrible turbo whine is gone. Success, sadly there was no time for a drive. Off to do family stuff with the wife and kids. Hopefully take it out for a thrash/test drive later tonight. 

  • Like 4
On 17/12/2022 at 5:57 PM, Dose Pipe Sutututu said:

Ready for Christmas skids ho ho ho 

Just came back from test drive. Can confirm does good skids, spins em off the throttle in 3rd. 

Coolant temp was fluctuating a bit and running 5 degrees above normal. Probably some air still working it's way out of the system. Will check coolant level tomorrow and keep an eye on temp. Happy to have a functioning boat again. 

  • Like 1

Lol, c'mon man. It's only a fan clutch. You've got a long way to go catching up to Greg. 

In other news, checked coolant level this morning. Took another litre and a bit. Went for test drive 2.0. Temp is a rock solid 88° now as indicated by the Android gauges. 

IMG_20221218_115252.thumb.jpg.b1266251b71d6d1bb3db4013a702190a.jpg

 

Gave her a quick wash/hose down for Christmas. Scrubbed up alright for an old girl. 

 

IMG_20221218_120631.thumb.jpg.aaa1d88c3d08069a518b8e0f6e70b5b3.jpg

 

After driving again and checking the peak boost levels on the boost gauge, it appears to be down by a bit over 1 psi. I do remember when removing the turbo, the actuator looked a little bent and was almost touching the outlet. I had filed down one of the bolts in the past for clearance. When the turbo came back the actuator looked perfect. I think Tao must have noticed it and straightened it up and this is possibly the difference in boost. Not sure if I'll tweak the boost control myself or take it back to Trent for a proper check and tweak. 

  • Like 1
On 12/17/2022 at 2:16 PM, admS15 said:

And finished product. Oem, it's stock standard officer. 

IMG_20221217_125119.thumb.jpg.deaf864e14b47a149529a7e9759c2b6a.jpg

 

IMG_20221217_125148.thumb.jpg.fdeb4dc287c404599d59f59195f50bb6.jpg

Drove through a booze bus today, Cop was all "Does that have a 25 Neo in it?" Said "Oh no, it has a LS" and opened the door and pointed to Engineering plate and told him it was all above board officer.

I got a solid thumbs up.

no RB can have that peace of mind! 😛

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Was going to say the car pulls up nicely everywhere, especially going into that last long right hander before the main straight. Looks like a lot of fun.
    • Hey Dave, welcome aboard! Good to see another soon-to-be Stagea owner here. The wagons are awesome — plenty of space, still got that Skyline DNA, and loads of potential if you’re into mods. Definitely post up pics when you get it, everyone here loves seeing new builds. What model/year are you looking at?
    • See if you can thermal epoxy a heatsink or two onto it?
    • The other problem was one of those "oh shit we are going to die moments". Basically the high spec Q50s have a full electric steering rack, and the povo ones had a regular hydraulic rack with an electric pump.  So couple of laps into session 5 as I came into turn 2 (big run off now, happily), the dash turned into a christmas tree and the steering became super heavy and I went well off. I assumed it was a tyre failure so limped to the pits, but everything was OK. But....the master warning light was still on so I checked the DTCs and saw – C13E6 “Heat Protection”. Yes, that bloody steering rack computer sitting where the oil cooler should be has its own sensors and error logic, and decided I was using the steering wheel too much. I really appreciated the helpful information in the manual (my bold) POSSIBLE CAUSE • Continuing the overloading steering (Sports driving in the circuit etc,) “DATA MONITOR” >> “C/M TEMPERATURE”. The rise of steering force motor internal temperature caused the protection function to operate. This is not a system malfunction. INSPECTION END So, basically the electric motor in the steering rack got to 150c, and it decided to shut down without warning for my safety. Didn't feel safe. Short term I'll see if I can duct some air to that motor (the engine bay is sealed pretty tight). Long term, depending on how often this happens, I'll look into swapping the povo spec electric/hydraulic rack in. While the rack should be fine the power supply to the pump will be a pain and might be best to deal with it when I add a PDM.
    • And finally, 2 problems I really need to sort.  Firstly as Matt said the auto trans is not happy as it gets hot - I couldn't log the temps but the gauge showed 90o. On the first day I took it out back in Feb, because the coolant was getting hot I never got to any auto trans issues; but on this day by late session 3 and then really clearly in 4 and 5 as it got hotter it just would not shift up. You can hear the issue really clearly at 12:55 and 16:20 on the vid. So the good news is, literally this week Ecutek finally released tuning for the jatco 7 speed. I'll have a chat to Racebox and see what they can do electrically to keep it cooler and to get the gears, if anything. That will likely take some R&D and can only really happen on track as it never gets even warm with road use. I've also picked up some eye wateringly expensive Redline D6 ATF to try, it had the highest viscosity I could find at 100o so we will see if that helps (just waiting for some oil pan gaskets so I can change it properly). If neither of those work I need to remove the coolant/trans interwarmer and the radiator cooler and go to an external cooler....somewhere.....(goodbye washer reservoir?), and if that fails give up on this mad idea and wait for Nissan to release the manual 400R
×
×
  • Create New...