Jump to content
SAU Community

Recommended Posts

Well ever since my appreciation of Japanese cars started in the early 2000's the R32 GTR was always the ultimate dream car for me but was never quite within reach (that old saying if you can't afford to buy two then don't buy one) boy is that soooo true.

So I've had a few jap cars before purchasing this one.

R32 Gtst which I bought pretty stock, built an RB30 twin cam and had a bit of fun.

Evo VII which was a great piece of kit.

R32 Gtst with a SR20DET which was a wide body track car, great fun but never got to use it enough.

Datsun 1200 sedan, awesome little old school cruiser.

But the bug for speed had started to come back and life's circumstances had brought me to the stage where buying one was more realistic and I figured if I were to get one now was the time as they just seemed to be increasing in price (now even more so with the yanks getting access to them)

So I started searching around January 2015.

Basically wanted to find something local (S.A), late model (93/94) or something with a rebuilt motor.

I ended up after around 4 months of searching finding this 89 model with a fully rebuilt motor.

That probably in hindsight blinded me to its short comings as in 4 months of searching this was the closest to fitting my criteria that I'd come across, I sooner more recently found out that whilst the build was definitely done all the bolt ons and engine fitting was done by the owner and it looks after close inspection to have been a rush job for sale. To which I am now slowly going over and fixing.

I've probably jumped forward a little......So I picked her up the Thursday before Easter and no less than four hours later travelling down the same road I venture at least once a week skippy decides to jump out and give me a nice little surprise resulting in what you see below. Thank god I insured it before picking it up.

After putting it in the shed and going away over Easter it gave me a chance to calm down and see it as a positive, as I mentioned earlier I bought the car mainly due to its rebuilt motor.............the body was certainly not clean, straight but it was certainly showing its age. Insurance ended up covering half the car being resprayed and I decided to get the rest minus the boot/rear resprayed whilst it was in at the shop.

Can't work out how to save this post so i'll come back tomorrow and edit to finish.....

post-16187-0-42703100-1456116970_thumb.jpg

post-16187-0-99455200-1456117029_thumb.jpg

post-16187-0-11004100-1456118159_thumb.jpg

post-16187-0-63449500-1456118185_thumb.jpg

post-16187-0-66390000-1456118350_thumb.jpg

post-16187-0-52086800-1456118391_thumb.jpg

post-16187-0-65246400-1456118431_thumb.jpg

  • Like 3
Link to comment
https://www.sau.com.au/forums/topic/463130-the-ever-evolving-r32-gtr-build/
Share on other sites

r32-25t - ye she certainly did a good job on me, came out of nowhere and I had hardly any time to react.

On the positive side she's basically brand new in the front end now and the paint/body work is looking good.

PranK - not sure about skippy, no sign of her after the accident so I presume she hopped off, tough little bugger.

GHO5T - she's only really gotten back on the road early this year so that's probably why mate.

Edited by mr_rbman

Well I can't edit my first post for some reason, as you can see from my first post my skills behind the pc are fairly amateurish.

So the goodies in/on the motor as I bought it.

Mahle forged pistons

AP rods

Brand new crank

modified sump with baffles

oil restrictors

refreshed head

Greddy cam gears

Sard fuel rail

AI FPR

Sard 650cc injectors

R34 GTR N1 turbos (2860-7's)

Apexi pod filters

Nistune ECU

A 'bitsa' exhaust (standard dumps :-/)

Since getting her fixed up after hitting skippy I then got the famous heater hose leaks :-/ how someone has a motor rebuilt and doesn't replace the heater hoses at the same time is beyond me.......by now rego had run out and I decided to leave it unregistered to tidy up a few things I didn't like when I bought the car.

Firstly I replaced the heater hose leaking and another one which didn't look too healthy (as anyone knows with a 32 GTR this is not fun to do but with the assistance of the old man and mates it got done) I plan to replace all heater hoses later in the year just to be safe.

It also came with Apexi Coilovers....I definitely must be getting older as the harsh ride got old very quick so I luckily found someone chasing Coilovers who had some bilstiens (blue not yellow) we swapped and I definitely prefer their ride now compared to the apexi's, I changed the heights to the recommendations (SK) I think 350mm~ at the rear and 360mm~ at the front.

Once they were done I proceeded to search for a standard fuel rail and airbox as I like the idea of popping the bonnet and it looking standard to the untrained eye. Fuel rail was easy but the airbox was a little more difficult to locate, ended up finding one interstate (NSW) after Australia Post somehow delivered it to Country Victoria I received it about a month later......purchased a K&N filter then happy days, or so I thought :-P In the meantime I'd purchased and wired in Z32 AFM's not clicking that as they were larger in diameter they of course wouldn't mate up to the standard airbox, so they were sold and some Nismo AFM's were purchased to rectify this issue.

I then also purchased a Blitz dual stage boost controller, Walbro 460LPH fuel pump and splitfire coil packs in preparation for the dyno.

After a few teething issues on the dyno (poor initial remap) this was tidied up but she would only make 220rwkws @ 14psi before falling over big time around 5800rpm, I knew my exhaust was going to be a restriction but not this much. It had/has standard dumps, twin 2.5" front pipes, 3" cat, 3.5" to muffler (which was cracked both in and outlet) then 4" to rear cannon. I feel the combination of standard dumps, 3" cat and possibly a fallen apart muffler are my restrictions.

This brings us to today, the car is in currently having a new full custom exhaust built and installed. After a lot of research on here and procrastination I have gone twin split dumps (400mm split before wategate pipe re renters main exhaust) then 3.5" all the way to the end with two mufflers. Whilst it's there its also having the turbo coolant lines replaced with black braided items as they are crimped in areas from the previous owners poor install, so I figure get that sorted whilst its easily accessible.

The aim of this car is to have a neat tidy weekend street car which can do the odd hillclimb and maybe drags.

I'm aiming for a reliable 300rwkws whilst keeping the exterior and under the bonnet looking as standard as possible.

Once these goals are achieved, ever so slowly getting closer...

I'll then start tending to the 4WD, its getting error code 18 so more than likely the expensive pressure sensor :-/

It's had most of the sub frame bushes replaced prior to my purchase which is one thing I didn't know when I bought it along with a Hicas lock bar which just needs the 20kg of crap removing now.

Edited by mr_rbman
  • Like 1

Planning to do a hill climb the first weekend of April, just realised that's only 5 weeks away so I'd better pull my finger out.

Still have to get the car back from the exhaust and then off to the tuners and then hopefully fix the 4WD issue.

Purchased a couple of maintenance items today from Nissan.

Genuine oil filter @ $16.45+ I thought wasn't too bad but the Genuine fuel filter @ $43.23+ was a little more of a shock, I guess at least the fuel filter won't be getting changed as regularly as the oil filter.

post-16187-0-02826800-1456459536_thumb.jpg

Purchased some items to clean up the engine bay once she runs out of rego in late April, really like the ripple paint as a few people seem to have done, thanks to Ants for the 'how to'

Have taken a couple of pics of the engine bay as it looks currently and my CAI.

Car is back from exhaust shop now and very happy with how it feels and the noise it puts out, she's booked in to be tuned next Monday so fingers crossed.

(old exhaust is now in the for sale section for anyone interested.)

Planning to change oil (5W30) filter and fuel filter this weekend prior to Monday's tune. Have noticed just lately a more noticeable 'tappet' sound, hoping an oil change may quieten this down.

post-16187-0-09581500-1456703290_thumb.jpg

post-16187-0-74776200-1456703319_thumb.jpg

post-16187-0-31426200-1456703343_thumb.jpg

post-16187-0-26682100-1456703373_thumb.jpg

post-16187-0-84262300-1456703393_thumb.jpg

  • Like 1
  • 2 weeks later...

Car has now been on the dyno and tuned :yes:

After locating a pesky boost leak I'm pretty happy with the results...

Current motor specs:

Rebuilt forged motor

R34 GTR N1 Turbos

Sard 650cc injectors

Walbro 460lp/h fuel pump (12v direct feed)

Splitfire Coilpacks

Blitz SBC

Nistune ECU

Nismo AFM's

Standard Airbox with K&N panel filter

Greddy adj. cam gears (2deg. advanced on inlet, 4 deg. retard on exhaust)

Full custom exhaust (2.5" twin dumps with separate 1.5" wastegate collector (350mm long split) into 3" collector, into 3.5" cat delete all the way to the end with x2 custom mufflers)

Looking at the graphs and comparing it to other similar setups it looks as though these make full boost a bit later than others?!?!?

Have played with the 'gain' setting on the boost controller and the cam gears helped but still doesn't seem right on paper, the car itself feels amazing though...

post-16187-0-32510100-1457398285_thumb.jpg

post-16187-0-08900000-1457398362_thumb.jpg

post-16187-0-98280100-1457398424_thumb.jpg

BWGTR ye I know this, I'll attach a pic of the ID plate for mine.......thought they were the desirable ones.....

Who knows these days.......saw the motive guys who had -5 cores in theirs......though if that were the case in this instance I'd be thinking more power.....

post-16187-0-64519900-1457402500_thumb.jpg

ye Glyn that's what I'm 'hoping' to avoid (for now anyway) reading through many of the threads on here and removing the plenum appears as though it could open up another can of worms :-/

Motors going to be dropped soon anyway and have all the hoses replaced but I was hoping to get mt alma out the way first.

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • Apologies for the long post, but needed somewhere to lay out the entire timeline of events and actions taken:   I've got an 89 GTR with a R34 RB in it. It's been running great all year, driven probably 500KM in the last month. It's not my daily driver, just a weekend fun car.    Build info: R34 RB26 - HKS 2.7 stroker kit, HKS adjustable cam gears, HKS turbo upgrades, Trust intercooler, R34 factory DENSO 440cc injectors, JUN chipped/tuned R32 ECU. All of this work was performed in Japan back in 2019.    Thursday 10/2/25 - It's a nice day and decided I'll drive it to work, I start it up in the garage and I notice it took a few extra cranks and sounded a bit funny. I figure maybe it was just because it was a pretty chilly morning. I pull it out into the driveway to warm up a bit before leaving. As I leave the driveway, it feels very off and sounds like a misfire. I pull it back in the garage to deal with after work and take the daily to work. I was able to diagnose it as a cylinder 5 misfire with the old spark plug test (unplugging each plug until a sound change with the engine running). I take off the whole ignition system, ignitor, plugs, spark. *Important note, it is still on the R32 ignition system with the separate ignitor system. I test each system with a multi-meter and nothing presents as a smoking gun. I put it all back together and it starts up no issue. I go ahead and order the PRP R35 ignition conversion kit. It should arrive today (10/13/25)   Friday 10/3/25 - Another nice day, car starts up great and drives great all day. Very pleased that everything seems to be OK   Sunday 10/5/25 - Decided I'll take it to play some golf, load up and drive to the course about 25 minutes away. Drives wonderful the whole way there, I pull in the parking lot and the engine completely comes to a stop. I do not recall if it sputtered at all, but just remember all of the sudden the engine was off. I roll it into a parking spot, try to crank it back on and nothing.  It'll crank and crank and not even try to start. End up getting it towed back to my house and push it up into the garage.    Items I have checked: Fuel in the tank Fuel Pump relay Fuel pump fuse  Spark Plugs & gap Coil packs Ignitor    I know the cylinders are getting fuel as the plugs smell like fuel after a start attempt. I tried spraying starter fluid into the manifold and cranking and not even a sputter.    I decided to do the live CAS test (removing the the CAS, ignition on and spinning the CAS stalk to see if the injectors pulse and spark is active). All of the injectors were pulsing and I have spark at the plug. The half-moon end of the CAS did seem very loose, I'm not sure how much play is supposed to be there, but it was more than I expected. There was no in/out play of the shaft, just the tip end that is pinned on had quite a bit of play.    CAS Play video   When I put the CAS back in, I stupidly did not re-time the engine. I know I need to do that tonight, however, I do not think it will start given it seemingly was not the issue. My plan is to do the PRP R35 coil kit and retime the engine at the same time.    I plan on ordering the Haltech Nexus Plug-in ECU once they are available again, but ideally would like to get this sorted before firing the parts cannon at it and potentially adding more variables.    Anything glaring that I am missing here, I'm a bit at a loss?          
    • Get it on a dyno. Get something logging Consult. Run it up and find out what is causing it.
    • Looking for a plenum for rb25 de+t neo  Not looking to push much power maybe 300kw at the wheels, is there much difference in flow for Freddy “Greddy style” compared to original Greddy or options like Proflow or Otaku garage?    I won’t be porting the de Neo head for now as I think it’ll be fine 280-300rwkw but appreciate the help and any experiences anyone has between them and any advice. Thanks  Looking at this plenum for now below 
    • engine wise almost no mods: stock ecu Greddy front mount intercooler Greddy forward facing intake w R33 TB stock fuel system, stock injectors, rail etc. Kakimoto racing hyper 3 inch exhaust system Apexi intake filter New NGK –R BCPRES (.8 gap) plugs  
    • Nice one @Pac - looks like a fair few 1600's there! 
×
×
  • Create New...