Jump to content
SAU Community

Recommended Posts

Please help me! My 2001 M35 Stagea ARX fitted with the VQ25DEt (all standard aside from a pod filter) is missing badly, pulling back, jerking when coming on boost and you can smell it if you try pushing through it. It's kinda similar to hitting fuel cut.

 

Yet At idle and normal driving it doesn't miss a beat??

 

I've been told it could be wastegate issue (anyone know an appropriate replacement wastegate?) Or ignition related  or even intake related however I've checked all hoses and they seem ok. I've done 55000kms in it myself and it hasn't missed a beat til now.

PLEASE HELP,  and thanks everyone, the info supplied on here is great.

Who told you it could be a waste gate issue?
If waste gate wasn't working properly it would be making too much boost and would pull pretty hard... Not sure it would cut out though.
What do you smell? Fuel?
Does it drive OK off boost?

3 hours ago, Leroy Peterson said:

Who told you it could be a waste gate issue?
If waste gate wasn't working properly it would be making too much boost and would pull pretty hard... Not sure it would cut out though.
What do you smell? Fuel?
Does it drive OK off boost?

Smells like rotten eggs. My Soarer used to smell the same when I'd been flogging it. It's driving fine under light acceleration. The bloke at autobarn advised potential wastegate issue and I read this last night so makes sense. 

If you've driven a turbocharged engine before, you'll easily understand the difference between an engine that is engaging the turbo and one that is not working properly. When you apply throttle pressure to the engine and the turbo does not engage, or the turbo boost gauge does not register a boost level, it's commonly due to the wastegate not functioning correctly or a blockage in the wastegate hose.

If you notice this problem, it's recommended to contact an experienced diesel mechanic with experience in turbocharged systems immediately to repair the problem before additional damage to the turbocharger occurs.

46 minutes ago, GTSBoy said:

Fuel pump.  AFM.  FPR.  Dirty injector.  Blocked fuel filter.  These are the first things to check.  Same as in the 500000000000 other threads that start this way.

Cheers mate, I've spent hours checking hoses etc so far as originally thought intake issue but all seems ok, it's not registering any fault codes either. It idles perfectly, revs clean in neutral etc

If rotten egg smell check the intake box for bird nest.

So the issue is only when on boost?
Does it boost or does power die to nothing?
Has the car got any errors up?
Have you ever replaced the AFM?

Much more info is needed if you want us to help

3 hours ago, Leroy Peterson said:

If rotten egg smell check the intake box for bird nest.

So the issue is only when on boost?
Does it boost or does power die to nothing?
Has the car got any errors up?
Have you ever replaced the AFM?

Much more info is needed if you want us to help

No it's not showing any errors or fault codes and no I've never replaced the afm. If I feather it I can get a little bit of boost if I nail it it's like hitting fuel cut at red line except it's doinf it at like 3.5-4 rpm. Aside from several  oil changes, tyres and a new radiator I'vebarely spent a cent on it. It's been great! It had 105,000 when I got it and now it's at 160,000 ans yes only on med acc you can feel it's not pulling right and hard it pulls back and kinda pops a bit and jerks then smells. 

I did spill some oil while servicing a few weeks ago and degreased the motor as it was a fair spill but I I've had it running really well for about a week after ans I also replaced the batrery in that period. 

 

 

2 hours ago, admS15 said:

Ever changed spark plugs?

Nah I haven't mate. There's so many things it could be making it so much worse and could get real expensive real quick. I'm a fulltime Dad with 2 kids that works 50+ hours per week. My times limited and so is my funding. I need a miracle haha

Thanks everyone, my car is better than ever. The plugs were pretty badly fouled up! However we replaced the fuel filter, and some vacuum lines as well and ran Molli through the fuel tank. Great result, really appreciate the help #backboostin ???

 

And no I didn't film this and it's on the highway ?

20180420_035745.mp4

  • Like 1
On 4/21/2018 at 10:18 AM, Pelican86 said:

Thanks everyone, my car is better than ever. The plugs were pretty badly fouled up! However we replaced the fuel filter, and some vacuum lines as well and ran Molli through the fuel tank. Great result, really appreciate the help #backboostin ???

 

And no I didn't film this and it's on the highway ?

20180420_035745.mp4

Keep an eye on coilpacks also. I experienced all the issues you described earlier on. Replaced plugs, came all good for a week or so and then continued doing it. Found out at least one of the plugs were cooooooked so I replaced them all with OEM replacements and its been good since. 

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now


  • Similar Content

  • Latest Posts

    • Yeop... binned it   This will be a summary will not many pics atm and cbf  Fixed the samsonas - it was totally munched Put a new precision 7675 T4 on with proper split pulse mani Got to Sydney to get to car - drove to canberra to get racecar - drive back to sydney that night Next day all day at Plasmaman putting on new clamps cleaning some things up and adding another large engine oil cooler sitting at the rear above diffuser to keep things cooler Next day - Tuesday - on Dyno - killer wikid awesome pumped out really good numbers - more mid range and on lower boost levels Wednesday - first prac - all day again getting the suspension right - had to borrow front suspension again - out do a lap come in - out do a lap - in - what i had just couldnt handle the load at the more consistent higher speeds - got a lap in at the end of the day that was pretty reasonable  Put it this way that lap wouldve had me in 4th in Pro am for the whole event - with only 700 hp and used tyres Thurs first official prac day - lap out warm up - with above setting and 80% effort took corners 1,2,3 and into 4 car felt awesome -  rear came around out of nowhere bang into the wall near front on at whatever 140 kmph Done, over, gone Just one of those how did that happen apparently as all indications show nothing out of the ordinary Got to spend the rest of the time at the event like I hadnt done before - was actually Ok mainly as I had my family and my boy is 9 and got treated like a rockstar Long trip home, lost a trailer wheel in nowhere land, X5 airbag suspension gave up half way across nullabour and rode on bumps stops (its now completely fine) had to do a 19 hr drive day on day 3 as accommodation got screwed up so just had to keep driving till found a town with some Now to reassess - hopefully the motor and other things are OK but yet to be seen too. There is no easy fix there is no i'll just order that part and get it sent - we'll have a talk to people see what can happen and what the go is but at minimum its rebuild from scratch struts forward and alot of time effort and $ should and if I return and if but maybe/ when  I have the cage tied into the front strut towers - if I didnt have that things couldnt been worse you can say its just a front end but if you know what goes into these cars... you'll know what that actually means in reality   Car was very fast. Disappointing we just didnt get to show it Effort doesnt win you races though     Apparently this is motorsport !  
    • Thanks, will do that.  Thankfully they still feel great.
    • Yeah man, absolutely. You can try pushing me all the way in swapping the R34 for an E9x M3 
    • It's almost certainly going to be some amount of pads compound transfer onto the rotors. It will probably go away after you've run them for a bit. If not, pull it all out, lightly sand the rotors, scuff the pads, and rebed.
    • no one recommending speedtek gearsets?   i'm in the same boat as Cosline but rwd, I am holding boost back in third to 600nm at the hubs to save the gear as i make nearly 750nm at the hubs on a mainline
×
×
  • Create New...