Jump to content
SAU Community

Recommended Posts

We had issues with the config of the EVC to start with. For some reason it had started just delivering 7psi. By the end of the day it was fine and back up to 15psi, but it's pretty obvious that I'll need Scotty's upgraded wastegate spring.

Thats a pretty good result for 7psi. lol.

You did better than my first attempt, good to see the tune is working and the engine runs fine. How does it feel? That's much more important than the power figure...

It feels pretty good. Looking forward to putting the good tyres back on and giving it a spank.

Shifts are a lot firmer, but throttle response isn't as good. Need to check that part of the map :/

Booked the car back in to get a couple of things with the tune fixed. Firstly whatever is causing the fault light and second the shitty throttle response. First thing Tuesday we should be good!

Just finished installing a GT2 FMIC with one hand into my AR-X. Had surgery on my right hand last week, so it is in a cast with titanium pins holding it together! Was a bit of a mission installing the intercooler, but I couldn't wait. Sweet intercooler kit!

Wow, that's dedication!

Got a mate ordering some bushes for me :-)

So much cheaper than retail when you work in the industry

Eg, r31 rack bushes, $15 fish vs around $45-60 on the eBay

Can't wait to have a bit more camber and caster in the front of the Stagea

Booked the car back in to get a couple of things with the tune fixed. Firstly whatever is causing the fault light and second the shitty throttle response. First thing Tuesday we should be good!

i have fault codes (running rich and running lean) 0172 & 0173 i think pop up sometimes but apparently it doesnt mean sh*t its just anoying for us

i have fault codes (running rich and running lean) 0172 & 0173 i think pop up sometimes but apparently it doesnt mean sh*t its just anoying for us

I notice when the code clears itself it comes back on at idle, so we will pull out the code and see whats going on. Shouldn't be doing anything like that.

Just finished installing a GT2 FMIC with one hand into my AR-X. Had surgery on my right hand last week, so it is in a cast with titanium pins holding it together! Was a bit of a mission installing the intercooler, but I couldn't wait. Sweet intercooler kit!

hardest part is the pipe on the drivers side to the intake. Oh I swore at that pipe many a times. good work on your persistance

I notice when the code clears itself it comes back on at idle, so we will pull out the code and see whats going on. Shouldn't be doing anything like that.

yep every time i notice it it happens at idle, as a set of traffic lights

** my tuner reakons its not an issue...............

Edited by WAGON_BOY

Its not an issue because the aftermarket computer is interacting with the stock computer. Theo- I remember when we had yours on the dyno, and we had a good idle AFR, yet when I was reading the stock computer the O2 correction was doing silly things. The data that I was reading was not actually affecting the AFR. So I'd expect to see errors as the stock ECU is trying to use O2 correction, and sensing different things. 125%/75% combination most likely triggers errors.

There is also 3 different O2 feedbacks in the software to look at.... bit confusing.

Thats the way I see it - no doubt Scott will chime in and disagree :P

The stock computer thinks it still has control, and expects to see a result from its o2 cycling. When this doesn't come it throws a fault. The Fcon is trying to trick it but it isn't smart enough obviously. (or not set up correctly)

Either way, it makes no difference as the stock computer is doing nothing with regards to tuning anyway. As long as it stays happy enough to run the throttle and cams you are fine.

Sounds like hooking the wideband up should fix it. Pretty sure my harness is setup to feed that signal back to the stock ECU.

But if that's what it's doing we'll work it out tomorrow and I'll see if we can find a fix.

Is it presenting as left bank lean?

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...