Jump to content
SAU Community

Recommended Posts

any tips on adjusting preload on actuator?

I usually run around 5mm of preload, or slightly over half the width of the hole. Depending on the spring it will take a bit of effort to pull the actuator back over the wastegate pin. The more preload the less the wastegate will travel, so you may need to dial it back a little if the boost is rising higher up in the revs. (unless that's the boost curve you are going for.)

Don't lose the circlip. ;)

  • Like 2

found this video from Tao, great music choice :thumbsup:

will run approx 3-4mm as advised by Tao. if i adjust actuator, will it affect the tune ?

my turbo 21u hiflow is getting fullboost by 4500~ which is very laggy.

me and toshi tested with no airbox cover on and it help response dramatically but no where near the 35-3700rpm it should be getting fullboost by.

current mods

480cc

21U hiflow

3" turboback jasma apexi superdunk

2,5" cooler

high pressure hypergear actuator @ 19-20psi

unopened rb25det s2 r33

Toshi suggested to run pod with EBC and it will help around 4000rpm but i want the 3500-3700 response that the 21U is supposed to make lol

didnt get change to run on dyno or complete 3rd and 4th gear runs as clutch slipped over 5000

If car is sitting on 1st gear then do expect 20psi over 5000RPM, I would advise of a clutch change and have the car fully tuned before trouble shooting take places, then preload the actuator through actuator bracket if needs to be.

Dude are you elvis? you bought my old turbo?

I had the 20 psi actuator installed with about 1-2mm negative preload on the actuator to bring boost down to about 17psi when i switched to 98. That killed response

Fit the black kinugawa actuator I gave you with about 5mm preload and you will get full boost around 3400rpm in 4th with max boost around 14-15 psi

  • Like 1

yeap

i don't get 17psi, i hit 19-20 lol

perhaps my mechanic may of moved actuator slightly as he installed a circlip to replace your wire you used.

Will do, Cheers Tim!

tao, can you confirm? shouldn't the high pressure actuator have same repsonse>?

Well, If Blackkers is getting good response using the same turbo then you should too. Just make sure the internal gate is shut and preloaded. and yes 20psi is lovely, baby it till it gets tuned, it should be all good :yes: .

  • Like 1

I usually slot the actuator bracket fitting holes, and that makes the actuator pre-loadable. Usually seeing around 15psi of boost once that is done.

Some updates. This is result of a OP6 high flow that I've done for Unique Auto Sports in NSWs.

R33 GTST stock engine with usual bolton supporting mods, PFC, pump 98 fuel. Final result of 278rwkws @ 18psi:

op6hf278rwkwr33.jpg

And a prototype turbo for Jet_R31. its the biggest possible turbo that we can make that fits into a T3x turbine housing. Hopping to see 600rwkws on his built RB30ET engine.

front.jpg

rear.jpg

  • Like 2

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • This. As for your options - I suggest remote mounting the Nissan sensor further away on a length of steel tube. That tube to have a loop in it to handle vibration, etc etc. You will need to either put a tee and a bleed fitting near the sensor, or crack the fitting at the sensor to bleed it full of oil when you first set it up, otherwise you won't get the line filled. But this is a small problem. Just needs enough access to get it done.
    • The time is always correct. Only the date is wrong. It currently thinks it is January 19. Tomorrow it will say it is January 20. The date and time are ( should be ! ) retrieved from the GPS navigation system.
    • Buy yourself a set of easy outs. See if they will get a good bite in and unthread it.   Very very lucky the whole sender didn't let go while on the track and cost you a motor!
    • Well GTSBoy, prepare yourself further. I did a track day with 1/2 a day prep on Friday, inpromptu. The good news is that I got home, and didn't drive the car into a wall. Everything seemed mostly okay. The car was even a little faster than it was last time. I also got to get some good datalog data too. I also noticed a tiny bit of knock which was (luckily?) recorded. All I know is the knock sensors got recalibrated.... and are notorious for false knock. So I don't know if they are too sensitive, not sensitive enough... or some other third option. But I reduced timing anyway. It wasn't every pull through the session either. Think along the lines of -1 degree of timing for say, three instances while at the top of 4th in a 20 minute all-hot-lap session. Unfortunately at the end of session 2... I noticed a little oil. I borrowed some jack stands and a jack and took a look under there, but as is often the case, messing around with it kinda half cleaned it up, it was not conclusive where it was coming from. I decided to give it another go and see how it was. The amount of oil was maybe one/two small drops. I did another 20 minute session and car went well, and I was just starting to get into it and not be terrified of driving on track. I pulled over and checked in the pits and saw this: This is where I called it, packed up and went home as I live ~20 min from the track with a VERY VERY CLOSE EYE on Oil Pressure on the way home. The volume wasn't much but you never know. I checked it today when I had my own space/tools/time to find out what was going on, wanted to clean it up, run the car and see if any of the fittings from around the oil filter were causing it. I have like.. 5 fittings there, so I suspected one was (hopefully?) the culprit. It became immediately apparent as soon as I looked around more closely. 795d266d-a034-4b8c-89c9-d83860f5d00a.mp4       This is the R34 GTT oil sender connected via an adapter to an oil cooler block I have installed which runs AN lines to my cooler (and back). There's also an oil temp sensor on top.  Just after that video, I attempted to unthread the sensor to see if it's loose/worn and it disintegrated in my hand. So yes. I am glad I noticed that oil because it would appear that complete and utter catastrophic engine failure was about 1 second of engine runtime away. I did try to drill the fitting out, and only succeeded in drilling the middle hole much larger and now there's a... smooth hole in there with what looks like a damn sleeve still incredibly tight in there. Not really sure how to proceed from here. My options: 1) Find someone who can remove the stuck fitting, and use a steel adapter so it won't fatigue? (Female BSPT for the R34 sender to 1/8NPT male - HARD to find). IF it isn't possible to remove - Buy a new block ($320) and have someone tap a new 1/8NPT in the top of it ($????) and hope the steel adapter works better. 2) Buy a new block and give up on the OEM pressure sender for the dash entirely, and use the supplied 1/8 NPT for the oil temp sender. Having the oil pressure read 0 in the dash with the warning lamp will give me a lot of anxiety driving around. I do have the actual GM sensor/sender working, but it needs OBD2 as a gauge. If I'm datalogging I don't actually have a readout of what the gauge is currently displaying. 3) Other? Find a new location for the OEM sender? Though I don't know of anywhere that will work. I also don't know if a steel adapter is actually functionally smart here. It's clearly leveraged itself through vibration of the motor and snapped in half. This doesn't seem like a setup a smart person would replicate given the weight of the OEM sender. Still pretty happy being lucky for once and seeing this at the absolute last moment before bye bye motor in a big way, even if an adapter is apparently 6 weeks+ delivery and I have no way to free the current stuck/potentially destroyed threads in the current oil block.
×
×
  • Create New...