Jump to content
SAU Community

Recommended Posts

26 minutes ago, IMACUL8 said:

Awesome Benny - love it!

 Thanks mate, good to see you're still keeping an eye on the build!!

Interestingly, the boost controller read 729ps, which must have been before the Prostock build.

The boost controller is now being chucked in the bin in lieu of a MAC VALVE

I can only assume the owner eventually sold it as he realised not having that much power wasn't for him.

I think down the road, we'll all be seeing a big EFR strapped to this lead sled.

14 minutes ago, BakemonoRicer said:

 Thanks mate, good to see you're still keeping an eye on the build!!

Interestingly, the boost controller read 729ps, which must have been before the Prostock build.

The boost controller is now being chucked in the bin in lieu of a MAC VALVE

I can only assume the owner eventually sold it as he realised not having that much power wasn't for him.

I think down the road, we'll all be seeing a big EFR strapped to this lead sled.

Of course - haven't been around much lately - got some work stuff I'm dealing with - but I'm subscribed to your thread as I love the car.....

I'll be posting soon - have a potential project in the garage (car that I imported when I got mine for a guy that has come back to me) ;)

Can't keep both ... so we'll see what happens....

 

Just now, IMACUL8 said:

Of course - haven't been around much lately - got some work stuff I'm dealing with - but I'm subscribed to your thread as I love the car.....

I'll be posting soon - have a potential project in the garage (car that I imported when I got mine for a guy that has come back to me) ;)

Can't keep both ... so we'll see what happens.... 

 

Hmmmm... I wonder if this could be the Bayside Blue Auto Select BNR34.......

HOW COOL DUDE!

Just now, BakemonoRicer said:

Still wish you had of sold me your S3 KR4 GT-R.

I would of saved money compared to the white polar bear LOL

Not for what you wanted to pay ;) ??

  • Haha 1
  • 2 weeks later...

TRP Rigoli have finished working their magic, the don mega fuel system full of their custom bits is done & so is their custom crank trigger setup.

This should pepper the car nicely ready for EFR life down the track....

1VMwDTh.jpg

rrMKUI2.jpg

NX57UXE.jpg

FlZPJDG.jpg

0Q0lXI2.jpg

gRVwpeH.jpg

d00FdqK.jpg

lI9YLsM.jpg

 

  • Like 2

Fuel system and crank trigger bits look good, I also thought that looked like an angle grinder job lol

What's up with all the filth and surface rust in your bay? Consider removing engine when you do the turbo swap and cleaning it all up. will lift the car a lot. 

Slideshow was severely lacking Benny, no dyno runs, no drive bys, no tacho hitting red line etc. Actually... no video content at all 0_0

Image result for son i am disappoint

I was talking about the pic that shows the holes coming through near the subframe but somehow thought that was an engine bay shot? WTF lol

What's the plan for the surface rust underneath gonna clean/paint it all up? Would look amazing done. 

Are they actual bulk head fittings or was there just a hole cut through the sheet metal?

 

Lol hmmm No plans to address surface rust there. If I was buying a car I’d rather see it....As soon as something gets painted over I would think the worst. 

I need to bring the car into the 21st century with more mechanical mods first anyway. Despite the fact the car hasn’t been tuned yet, I’m already saving my pennies for an EFR8374 or EFR8474 setup. 

I also thought Dan had lost his mind... 
The surface rust isn't bad, but i'd be keeping an eye on it, just in cases. 

 

8 minutes ago, BakemonoRicer said:

I’m already saving my pennies for

^^^^Every single GTR owner ever. ?

31 minutes ago, BakemonoRicer said:

Lol hmmm No plans to address surface rust there. If I was buying a car I’d rather see it....As soon as something gets painted over I would think the worst. 

I need to bring the car into the 21st century with more mechanical mods first anyway. Despite the fact the car hasn’t been tuned yet, I’m already saving my pennies for an EFR8374 or EFR8474 setup. 

The longer you leave surface rust the longer it gets the chance to become deep rust. 

Get it cleaned up, painted over, and seal the metal from the elements to prevent further rust. 

 

It also concerns me, you said this was all rebuilt in 2016, yet there is surface rust in a few pictures underneath it. 

My POS has less surface rust under it and it sat in a field, on a farm, for the past 2 years, and also went 1.8M under water in a flood during that time, not to mention just sitting around for years. I'm wondering what the rebuild hid or more so, it's life after the rebuild. Crazy salt roads? 

  • Like 1
  • Haha 1

Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now



  • Similar Content

  • Latest Posts

    • As discussed in the previous post, the bushes in the 110 needed replacing. I took this opportunity to replace the castor bushes, the front lower control arm, lower the car and get the alignment dialled in with new tyres. I took it down to Alignment Motorsports on the GC to get this work done and also get more out of the Shockworks as I felt like I wasn't getting the full use out of them.  To cut a very long story short, it ended up being the case the passenger side castor arm wouldn't accept the brand new bush as the sleeve had worn badly enough to the point you could push the new bush in by hand and completely through. Trying a pair of TRD bushes didn't fix the issue either (I had originally gone with Hardrace bushes). We needed to urgently source another castor arm, and thankfully this was sourced and the guys at the shop worked on my car until 7pm on a Saturday to get everything done. The car rides a lot nicer now with the suspension dialled in properly. Lowered the car a little as well to suit the lower profile front tyres, and just bring the car down generally. Eternally thankful for the guys down at the shop to get the car sorted, we both pulled big favours from our contacts to get it done on the Saturday.  Also plugged in the new Stedi foglights into the S15, and even from a quick test in the garage I'm keen to see how they look out on the road. I had some concerns about the length of the LED body and whether it'd fit in the foglight housing but it's fine.  I've got a small window coming up next month where I'll likely get a little paint work done on the 110 to remove the rear wing, add a boot wing and roof wing, get the side skirt fixed up and colour match the little panel on the tail lights so that I can install some badges that I've kept in storage. I'm also tempted to put in a new pair of headlights on the 110.  Until then, here's some more pictures from Easter this year. 
    • I would put a fuel pressure gauge between the filter and the fuel rail, see if it's maintaining good fuel pressure at idle going up to the point when it stalls. Do you see any strange behavior in commanded fuel leading up to the point when it stalls? You might have to start going through the service manual and doing a long list of sensor tests if it's not the fuel system for whatever reason.
    • Hi,  Just joined the forum so I could share my "fix" of this problem. Might be of use to someone. Had the same hunting at idle issue on my V36 with VQ35HR engine after swapping the engine because the original one got overheated.  While changing the engine I made the mistake of cleaning the throttle bodies and tried all the tricks i could find to do a throttle relearn with no luck. Gave in and took it to a shop and they couldn't sort it. Then took it to my local Nissan dealership and they couldn't get it to idle properly. They said I'd need to replace the throttle bodies and the ecu probably costing more than the car is worth. So I had the idea of replacing the carbon I cleaned out with a thin layer of super glue and it's back to normal idle now. Bit rough but saved the car from the wreckers 🤣
    • After my last update, I went ahead with cleaning and restoring the entire fuel system. This included removing the tank and cleaning it with the Beyond Balistics solution, power washing it multiple times, drying it thoroughly, rinsing with IPA, drying again with heat gun and compressed air. Also, cleaning out the lines, fuel rail, and replacing the fuel pump with an OEM-style one. During the cleaning process, I replaced several hoses - including the breather hose on the fuel tank, which turned out to be the cause of the earlier fuel leak. This is what the old fuel filter looked like: Fuel tank before cleaning: Dirty Fuel Tank.mp4   Fuel tank after cleaning (some staining remains): Clean Fuel Tank.mp4 Both the OEM 270cc and new DeatschWerks 550cc injectors were cleaned professionally by a shop. Before reassembling everything, I tested the fuel flow by running the pump output into a container at the fuel filter location - flow looked good. I then fitted the new fuel filter and reassembled the rest of the system. Fuel Flow Test.mp4 Test 1 - 550cc injectors Ran the new fuel pump with its supplied diagonal strainer (different from OEM’s flat strainer) and my 550cc injectors using the same resized-injector map I had successfully used before. At first, it idled roughly and stalled when I applied throttle. Checked the spark plugs and found that they were fouled with carbon (likely from the earlier overly rich running when the injectors were clogged). After cleaning the plugs, the car started fine. However, it would only idle for 30–60 seconds before stalling, and while driving it would feel like a “fuel cut” after a few seconds - though it wouldn’t fully stall. Test 2 – Strainer swap Suspecting the diagonal strainer might not be reaching the tank bottom, I swapped it for the original flat strainer and filled the tank with ~45L of fuel. The issue persisted exactly the same. Test 3 – OEM injectors To eliminate tuning variables, I reinstalled the OEM 270cc injectors and reverted to the original map. Cleaned the spark plugs again just in-case. The stalling and “fuel cut” still remained.   At this stage, I suspect an intermittent power or connection fault at the fuel pump hanger, caused during the cleaning process. This has led me to look into getting Frenchy’s fuel hanger and replacing the unit entirely. TL;DR: Cleaned and restored the fuel system (tank, lines, rail, pump). Tested 550cc injectors with the same resized-injector map as before, but the car stalls at idle and experiences what feels like “fuel cut” after a few seconds of driving. Swapped back to OEM injectors with original map to rule out tuning, but the issue persists. Now suspecting an intermittent power or connection fault at the fuel pump hanger, possibly cause by the cleaning process.  
×
×
  • Create New...